The heat this weekend reminded me just how much I like early spring and
late fall... anything over 65 degrees is just too hot. But the high
humidity Saturday didn't stop us from working. The gang this weekend
was Tom H, Steph J, Steve L, myself and special guests JD Marzec, Greg
Frech both from the steam shop and John from the carshop who was
attending for regular membership. As advertised, most of us arrived on
time and prepped for a trip to Four Mile Siding to replace the
switchpoint on the turnout side of the new power switch. We split into
two groups to start out. Steve, Steph and John got the J580 A8
Motorcar, Welding cart and hydraulic cart switched out of Barn 2 while
Tom, JD and Greg got the Model 50 Burro, CNW flat and EJ&E 529
caboose together in Yard 11. I ran around gathering fuel, water and
ice and got the forklift out to load the new switch point onto the
flatcar.
We made it out to Four Mile and were joined by Julie
J and Bob O from the signal dept to replace the point. We made quick
work out of the job and had the new rods on, including the 'new' #2 rod
within an hour. It seems this point is indeed correct and will work
fine. We made the slow trek back to the property a bit after 1PM and
had everything put away around 2PM. I'm glad to report that all of our
machines worked very well and the only thing that required a jump start
was the forklift...sigh
The rest of the day we spent mostly in
Yard 11 cleaning off the C&NW flatcar and continuing to load our
scrap gondola. The old switchpoint was set up near B&G for
Volkmann. JD was able to cut frog bolts with our oxy/ acetelyne torch
making quick work out of that. Everyone did a very good job and I
appreciate all of the help. I think everyone had an enjoyable day but
I've been known to be wrong..
Sunday was only slightly lower
key. Tom, Steph and I made up the Track Dept while Steve L spent the
day helping the Electric car shop in Barn 4. The goal was to cut brush
near Karsten's crossing with the Amtrak brushcutter before operations
got underway. Tom and Steph arrived on time and got the machine out
and on the rail early. After the Electric car shop finished testing of
the overhead on the main it was our turn to get on the line. I showed
up just as they were finishing up the first section of cutting and just
as the machine developed an air leak... An old air line under the
machine came loose from its fitting which put us out of service on the
main until we could come up with a fix. An hour or so later, after
numerous trips to the property and failed attempts at a repair we ended
up changing the entire hose. We got ourselves back in service and
cleared the mainline for revenue service shortly after. There is still
a little bit of cutting left to do near Karsten's but the worst area
has been taken care of. It was a warm weekend and proved how important
it is to carry water with us on the line. We have a cooler in Barn 2,
lets remember to keep it full.
In the next few weeks we will
need to take care of some housekeeping chores. The fire inspector will
be coming soon and we have a list of things to clean up ASAP. All of
the plastic hanging from the ceiling in Tk24 will need to come down and
the aisles need to be clear.
Until next time...
Adam Robillard
Roadmaster
lzeje657@msn.com
Comments
Thu, 05-16-2013 21:52
Looking good Bob! I hope to come out soon once I'm done with school.
Wed, 05-15-2013 21:28
I was not around at the time. General discussion suggests that it was "pretty marginal" in a number of areas. Nigel
Mon, 05-13-2013 11:08
"THUMBS UP!"
Fri, 05-10-2013 02:15
No, it will not be necessary to hold any of the work waiting for the plow to be turned, end for end. Weather will be the major factor, but there will [...]
Thu, 05-09-2013 19:54
The CGW X-38 plow is really coming to life. Bob Kutella and Vic and crew need to be very proud of your collective efforts. I am very appreciative of [...]
Thu, 05-09-2013 15:20
The snowplow looks great! Are you going to apply the door and upper windows befor it is turned to continue work?
Thu, 05-09-2013 09:09
Max, Is there any progress to report yet, in regards to the installation of the poles and overhead wires? Have a good day, sir.
Wed, 05-08-2013 18:40
Thanks for the update! I still don't understand why Commonwealth #5 was removed from service. Do you know why?
Tue, 05-07-2013 09:28
Mr. Kolanowski.....I was just wondering if the Spaulding webcam will be up and running soon for us stay-at-homes. Thanks!2FP
Mon, 05-06-2013 23:04
Max, Has work begun yet on the construction phase of erecting the poles and putting up the wire? Wish I could be there to watch it happen.
Mon, 05-06-2013 23:02
Keep up the good work, Bob. Wish I could be there to help!!!!!!!
Sun, 05-05-2013 18:53
Ah yes, I have made such Jibs myself. If it were me, I would add in each corner an angled piece from the base to the Jib to act as sway bracing. [...]