This was a BIG DEAL, and a problem we have wrestled with over the last six weeks. That is - how to replace the coupler at one end. Oh, the old one was removed easily enough, but getting its replacement in was a bit more involved. The car has an unusual draft gear, some sort of early development with cushioning features. So it had to be compressed in order to make the attachments and complete the installation. After trying unsuccessfully several weeks, and consulting with other members and folks in industry, it was time for the next trial.
This whole adventure could not have been done without a lot of interdepartmental cooperation. First, the Internal Combustion boys moved the caboose from its Track 40 resting place to track 41 just east of Barn 4.
Next, thanks go to Dave Diamond and Jerry Lynn. Jerry came over with the bobcat and helped lift and insert the replacement coupler into the pocket. Elapsed time maybe 10 minutes - we have done this enough to be good at it.
The US army engine was used to pull the caboose clear and MILW 760 came into Track 41.
The 760 was to act as an 'anchor' and we would put a big squeeze on the coupler draft gear using another locomotive on the east end.
In short order, the caboose and the Army engine came in. We fussed and pushed all to no avail. Once we gave the set a bump and the 760 actually slid a small amount from the impact - but the draft gear also moved a bit, before springing back out.
The next part of the adventure was deciding more weight was needed and larger locomotives would provide that. The work site migrated to the West end of Barn 2. (All following photos by James Kolanowski.)
SP 1518 and MILW 760 went in first to act as the anchors. Brakes set up and substantial amount of weight there. The caboose next, and then CB&Q 504. So now we had just short of ONE MILLION pounds of locomotives, and and THIRTY FOUR wheels on the rail, ready to make the squeeze. Even at that the 504 slipped a bit before the gear went into place, and the brakes were locked to hold it there.
Roger Broms is dropping the anchor bolts on the train line to provide clearance.
With everything in alignment a cross key is inserted to attach the coupler shank to the yoke.
The key is in and the tab on this end gets three more pieces to prevent it from working loose in service.
From the top, the shank is about two inches inward from where we started - you will have to take my word for it.
So there you have it. The caboose was brought back to Track 40 and Victor Humphreys and I hung the uncoupling bar, cotter key, cross key anchor dogs, re hung the train line and reconnected and anchored an air line to the conductors platform brake valve. Simple, huh?
None of this would have been remotely possible without the outstanding cooperation and participation of Jamie Kolanowski and Roger Broms. They helped complete a project in house at minimum expense - which would have been significant had we hired an outside contractor. That is, if we could find one - several calls were made.
So this fine restoration is now released for service and this represents two cabooses completed in the last four days. We did not plan it that way, and have been working on both of them, sometimes things happen right.
Comments
Mon, 06-17-2013 09:50
Wish I could be there to help.
Fri, 06-14-2013 16:50
Matthew, Any special event is the decision of the museum Board. My personal opinion is that it is likely that there would be a special event to [...]
Thu, 06-13-2013 18:33
Hi, I have a question, if or when she is restored and back up and running this or next year. Will their be a special event set up for the return of [...]
Tue, 06-11-2013 22:36
The whistle 1630 wore for a while that you're thinking of was a Frisco 6 chime donated by a former member of the steam shop. It was on it a few times [...]
Tue, 06-11-2013 18:03
You are talking here about something well before my time !. I have not seen her with anything other than the whistle she now carries. If she [...]
Mon, 06-10-2013 16:17
i'm curious here. Will 1630 ever wear the ATSF 6 chime she had on for a while? Better defines her, I love the deep whistle she has now but the higher [...]
Sat, 06-08-2013 15:15
Many many many many many thanks for getting the Spaulding webcam working!!!!!
Fri, 06-07-2013 16:55
The donation was to the museum as a whole. How it is used and whether any comes to steam department projects will be the decision of the museum [...]
Fri, 06-07-2013 16:53
Basically the plan is "ONLY" reassembly. As far as we know she is is reasonable mechanical shape. The big mechanical problem that stopped her (slack [...]
Fri, 06-07-2013 16:28
Nigel I read you guys got a one million dollar check donation!!! Will this be used to finish 1630 ,428, 5 and get started on the others next in line?
Fri, 06-07-2013 16:16
So does 1630 basically only need reassembly? With the boiler in particular. Does her tender or running gear need any work before she's ready for the [...]
Fri, 06-07-2013 12:00
Hello.. The voltage we are using and presumed the RR also used is 120 vac. The system is a little unique because the lite bulbs are each 60 volts. [...]