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Sunday, March 13. 2011
The late GB&W 2407 update Posted by James Kolanowski
in Atchison, Topeka & Santa Fe 841 at
23:12
Comments (0) The late GB&W 2407 updateHere is a very late update on the progress on GB&W 2407 from February 12th, I had drafted it before I went on vacation for a couple of weeks and forgot to publish it. We had a pretty large group out Saturday afternoon, including Frank DeVries, Marcus Ruef, Warren Lloyd, Kyle Merkel, Kevin Hennessy, Greg Ceurvorst, Dave Fullarton, Jeron Glander, Jim West, Dan Currens, Rich Schauer, and myself. The main tasks were to get the rest of the water system tight. The previous weekend and during the week we had made a number of repairs, but did not have a chance to water it again. The electrical system, governor, and air compressor were also worked on. Dan Currens started by digging into the electrical system, verifying everything was connected and functioning properly in the cabinet, and with the governor and such. Kyle and Jim worked on refilling the governor and pump with oil. We will have to flush the system again at a later date. There was some minor raccoon damage, but the majority of the electrical system was in pretty good shape. Meanwhile Dave and Kevin were working on checking all the injection pumps, seeing which ones were free and which were sticking. They found a bunch that were very tight and began working on lubricating and freeing them up. Warren, Kyle and Rich joined in as well. Frank and Marcus made a gasket to replace the leaking one on a cover on the air compressor, and then changed the oil in the compressor. We started watering again to verify the latest repairs and was very surprised at how well it was holding water. We did mark a few more water elbows that we had not marked the last time, along with some additional pipe couplings. Frank noticed a crack on a low pressure cylinder liner that was leaking water. There were a number of other leaks in this area the last time, so we didn't notice it. We are looking into some ways to fix this without changing the liner as it looks like the only damage is this area on the outside of the water jacket. Greg joined Marcus and Frank, and they made some more gaskets to replace the leaking ones along with some hoses on a few of the water elbows on the engineers side after draining the water. They made enough for all the ones that were leaking on both sides. Warren replaced two of them on one side of the loco while Marcus and Frank replaced a few on the engineers side. While draining, we noticed that the compressor and water cooled intercooler on the compressor did not have a drain as the pipe that should have gone to the main drain valve was removed and plugged. This was done sometime when it was on the railroad, and is probably why there were water problems on the compressor. We'll have to thoroughly check out the intercooler as well. It was a very productive day and I'd like to thank everyone that helped out to move this project much further along. Be sure to visit the Photo Gallery of the current work going on. Also, donations to the RSD15 are still needed and appreciated. Sunday, March 13. 2011Saturday Track Report
Saturday's plan involved a two pronged attack. One group was to finish walking the mainline, the second team was to load the mainline ties onto a flatcar, so they can be peddled out for install in the coming weeks.
Again, I picked up Marcus at Aurora Transportation Center, and we drove up to Marengo Cafe for breakfast. After Breakfast we met a new volunteer to our group, Patrick Shea. Adam joined us at the caboose on 110 track and the plans were set in motion. Marcus and I walked track. We started with the stretch from East switch to Karstens, so the diesel department could use the east switch as head room for fueling diesels. We then continued out to signal 201 with no significant defects found. The walk continued from East switch to West before we broke for lunch. After lunch we finished off the West end finding one broken bar. The total repairs for this spring, two pull aparts east of 4 mile siding, which is still out of service, One broken bar on the main between 201 and 251. One broken bar at West switch. We intend to have the two broken bars fixed before the start of the season. The pull aparts depend on getting some warm sunny weather to get the rails to expand enough to get new bolts in the rail. Adam and Patrick grabbed the fork lift and started loading bundles of ties onto the TTX flat car that the Camp Grant arrived on. All the other IRM flats are in use, so we pressed this one into service since it was just taking up space in the siding. The diesel department was kind enough to retrieve it and bring it to along barn 9 for us. In short order Adam and Patrick had the flat loaded up and ready for Sunday's distribution party. A break for a brief meeting, and we were back at it putting the train together. Tom joined us for this phase of the job. Tom finished off getting the four part hook put back on the crane. The hook was taken off last year to rig up the clam shell for loading stone. Tom, Marcus, and I, then got the 529 caboose moved over and the loaded flat car onto track 112, while Adam and Patrick loaded a couple more bundles of ties onto tie flats with the tie crane. The tie crane was tied down in yard 10 for the night. Tomorrow's projects, go out and peddle ties where we marked ties for replacement. A few photos have been posted here: http://www.irm.org/gallery/album271 Frank D. Sunday, March 13. 2011Wood Shop Update - March 12, 2011Greg Ceurvorst, John Faulhaber, and Fred Zimmerman are discussing the days work - what else - more windows! Greg was doing some finish sanding on the new Villa Falls windows. Earlier, he, Fred and Victor Humphreys moved some structural steel from the Barn 4 floor to inside the B&O boxcar. Fred and Victor were repairing another step well for the ATSF caboose. Fred is all suited up and the sparks are flying! Randy Hicks has just completed some tricky notches for a new poplar window sill for the IT cars undergoing repairs in Barn 4. Earlier, Randy completed post repairs on the IT 277. There was a lot of woodwork and tricky parts to replace rotted members, under that wide window post steel plate. Or rather - sign box of the times. Mike Stauber and Frank Sirinek have removed the front signbox from the Kansas City PCC and they had it in the shop. Disassembly, cleanup and repairs ensued. Done with that stage, it is ready for primer and repainting. Sunday, March 13. 2011
Trolley Bus Department Update - ... Posted by Ray Piesciuk
in Trolley Bus Department at
11:07
Comments (5) Trolley Bus Department Update - 03/13/2011A few years ago, the drag link on Chicago Marmon 9553 failed. At the time we decided to swap the remaining good on from Chicago Marmon 9631 to keep 9553 in service until we could fabricate repairs. During this past week, Richard Schauer and I decided that it was time to get this done. We weren’t sure how long this project would take, but it might be a significant amount of time. So, to prevent the 9553 from blocking service coaches during this period, we began the day by doing a switch move, swapping the Dayton Flyer 925 with the 9553. To accomplish this we had to move the two coaches in front of them, Seattle Twin 633 and Edmonton BBC 181.
We then got to work removing the good drag link from the 9553. After easily removing the front part (under the driver’s seat), the back section (behind the front wheels) gave us real difficulty. With limited space and leverage under the coach, we decided that turning the front wheels a little would give us a better angle at loosening the connection. Since the coach was stationary, turning the wheels puts a big strain on the drag link. Unfortunately it proved a little too much and the good drag link began to fail. To prevent a total failure we immediately stopped and returned to removing the rear section. With the help of Warren Lloyd, we finally accomplished the task.
We brought it over to the Car Shop to remove all the parts and clean it up. Luckily Car Dept. Superintendent Rod Turner was there and took a look at it. He came up with a couple ideas on how it and the second one could be repaired. No time like the present, so we set out to make the repairs on the “good” one. Rod and Diesel Dept. Superintendent Jamie Kolanowski gave us a good deal of their time and expertise, and by the evening the job was done! We’ll need to do some additional work to get the second one fixed, but a job that might have taken a very long time and possible be very costly, is well on its way toward completion.
Another great example of departments working together. Rod and Jamie, we owe you guys big time for this one – THANKS!!!!!
On another front, preliminary work on the west loop project continues. B&G Superintendent Dave Diamond has a quote for paving. We spent some time discussing the project with Dave and we decided that we will start staking out the road once the weather and ground condition permits.
Don’t forget about the Snowflake Special coming up on March 27th. Tickets sales are brisk so don’t be left out! Click on the link from the IRM home page and buy your tickets online now!!! Sunday, March 13. 2011CTS 4223 - March 12, 2011Our Cleveland Transit PCC car came outdoors yesterday in a move from Barn 2 to Barn 8. THANKS to Randy Hicks who shared these images of his. As you can see remarkable progress has been made during recent months to get this car painted in Cleveland colors - for the first time in decades! As you can see the interior still needs a little work. Thanks again Randy for the eye candy! I wonder where he gets all that energy? |
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Comments
Fri, 11-08-2019 12:47
what is the status of me 18 I thought this unit was operable? if not is something wrong that's a major problem. I remember watching this unit go by my [...]
Fri, 11-01-2019 09:04
I hope they named the kitten "Gigi".
Fri, 11-01-2019 05:36
An update will be coming soon. But yes, the rails have gone in--we are still working on connecting them to the outside world though.
Tue, 10-22-2019 16:01
August was a long time ago; how about an update on the pit project? Are the rails in place yet? Ted Miles, IRM Member
Wed, 09-11-2019 06:37
Sam--I'll shoot you an e-mail with more information. -Chris
Tue, 09-10-2019 21:16
Exciting news about your new pit! We at Shelburne Falls Trolley Museum are planning a pit in our Car Barn extension project. Any information that you [...]
Tue, 09-10-2019 16:25
The Shay will be running both days. Thanks for checking!
Tue, 09-10-2019 07:32
Hello! I'm coming in for the big event this Saturday and had one quick question: On the Showcase event page it says the Shay will be on a caboose [...]
Thu, 08-22-2019 16:35
Very nice things indeed for IRM. The new model train and archive building is done, the Shay came back, you've got a new U-boat to play with (and [...]
Sun, 06-30-2019 12:45
Eighty feet if I remember right.
Sun, 06-23-2019 11:40
How long is the pit going to be? Ted Miles, IRM Member
Tue, 04-23-2019 01:12
One Step closer to recreating "The Varsity" Circa 1950's.