A few of us have managed a couple of mid-week work sessions over the Christmas period. The significant visible progress is that Eric and Chris did a great job on cleaning out the interior of the boiler on 1630. After all the cutting of tubes there was a mass of debris in the boiler that they spent most of Monday clearing with brushes, rods, magnets and vacuum. Thanks to their efforts we now have a good basis for preparing the surfaces for inspection.
A step that we need to carry out soon is the sand blasting of the firebox tube sheet. We have the sand blast equipment, breathing helmet and supply hoses BUT - no really suitable breathable air pump. If anyone has access to a suitable pump - (oil-less, about 10 c.f.m. at 5 p.s.i.) please let me know. Otherwise we are facing a cost of about $1000 for such a pump.
I had the chance to photograph the firebox with the defective corner cut out:
.............. and the piece removed:
Interesting that it is very much in line with the problem suspected by the specialist who attempted the temporary repair in May. This was that, when a replacement tube sheet was fitted (believe in the late 1930's), it may have been fractionally narrow and pulled into place by the rivets causing stress cracks in the corner. Looking now at what is the inside (water side) of the corner you can see the welded joint between the "new" tube sheet (on the right) and the original firebox. This runs thru the last rivet hole on the left in the top row. Sure enough you can see that the tube sheet is fractionally set back from the original firebox side. The crack that resulted can be seen running from the second rivet in the top row. (They look a lot worse now as a good deal of metal was ground away from the other side of the plate when removing the rivets). These cracks would have formed over many years as water worked on the weaknesses caused by the stress in the corner of the new tube plate.
The other major work in these sessions was unplanned!. Initial testing of the swager disclosed several problems. The large dies that actually compress the pipe proved to be jammed. Several of us spent a day removing, carefully cleaning and polishing the guides and refitting these. Sounds easy but each weighs about 100lbs and they are linked by 4 inch long 1 1/2 inch steel guide rods that must be a tight fit - but not jammed!. Good thing there were not too many around to hear the language on the occasions when we put them together, found they still jammed, and had to get them apart again!. Still, they are now back in place ......... and it is clear that there are also issues with the air control valve. So that is the next step.
Nigel Bennett
Comments
Mon, 06-17-2013 09:50
Wish I could be there to help.
Fri, 06-14-2013 16:50
Matthew, Any special event is the decision of the museum Board. My personal opinion is that it is likely that there would be a special event to [...]
Thu, 06-13-2013 18:33
Hi, I have a question, if or when she is restored and back up and running this or next year. Will their be a special event set up for the return of [...]
Tue, 06-11-2013 22:36
The whistle 1630 wore for a while that you're thinking of was a Frisco 6 chime donated by a former member of the steam shop. It was on it a few times [...]
Tue, 06-11-2013 18:03
You are talking here about something well before my time !. I have not seen her with anything other than the whistle she now carries. If she [...]
Mon, 06-10-2013 16:17
i'm curious here. Will 1630 ever wear the ATSF 6 chime she had on for a while? Better defines her, I love the deep whistle she has now but the higher [...]
Sat, 06-08-2013 15:15
Many many many many many thanks for getting the Spaulding webcam working!!!!!
Fri, 06-07-2013 16:55
The donation was to the museum as a whole. How it is used and whether any comes to steam department projects will be the decision of the museum [...]
Fri, 06-07-2013 16:53
Basically the plan is "ONLY" reassembly. As far as we know she is is reasonable mechanical shape. The big mechanical problem that stopped her (slack [...]
Fri, 06-07-2013 16:28
Nigel I read you guys got a one million dollar check donation!!! Will this be used to finish 1630 ,428, 5 and get started on the others next in line?
Fri, 06-07-2013 16:16
So does 1630 basically only need reassembly? With the boiler in particular. Does her tender or running gear need any work before she's ready for the [...]
Fri, 06-07-2013 12:00
Hello.. The voltage we are using and presumed the RR also used is 120 vac. The system is a little unique because the lite bulbs are each 60 volts. [...]