At least I was able to get back to Union this weekend although mainly as a nuisance to others as I cannot lift anything much!!. Some key milestones were achieved.
On 1630 we reached the important milestone that has been our objective for several weeks
· All the measurements of boiler sheet thickness for the form 4 have now been completed. We owe an enormous thank you to Tom Huber of ECE Global who spent a second day crawling in and over the boiler with the UT testing equipment to complete a comprehensive set of measurements of every part of the pressure vessel. Collin, Phil and several others from the team supported him in locating points, cleaning and recording. We now just have to plot all the final measurements on diagrams of the sheets to complete a major part of the form 4.
· Dennis cut back and welded a small crack we found in the dome lid securing ring. We had been wondering how a crack this shape could form and now we know. It resulted from a small inclusion (defect) in the casting when it was made 95 years ago !. So it is now better than it has ever been.
· The flexible stays where the caps have been removed were thoroughly cleaned and are now ready for hammer testing;
· A lot of progress has been made toward safe ending the super heater flues.
A rigid measuring bar was made from used boiler tube to allow exact lengths to be confirmed;
Glenn Traced the problem with the Sullair to a broken fuel pump so we can hope to sand blast the material needed for the safe ends once the replacement fuel pump arrives next week;
Phil and Cameron have made substantial progress on chamfering the ends of the flues to accept the safe ends;
One flues that was found on inspection to have an existing weld was shortened to allow a new end to be fitted.
· We will probably do some work over the next couple of weekends in an attempt to clarify one anomaly. 1630 has been restricted in recent years to a 160 psi boiler pressure as opposed to the 180 at which it ran during its service with the Frisco and Eagle Pitcher. The reason for this is not wear but an apparent anomaly in the design. Drawings of the boiler consistently show the back head braced by a mixture of 1 3/8 and smaller diameter 1 1/4 diameter braces. The reason for this is unclear as, even by the standards when built, inclusion of the smaller braces brought stresses at 180 psi close to the limit in this one area when all other areas of the boiler show substantial reserve.
As shown a couple of weeks ago, these braces, particularly the ones shown in the drawing as 1 1/4, are extremely difficult to access. However, yesterday for the first time we did manage to get a measuring tool to one shown in the drawing as 1 1/4. The strange thing is that it does not appear to be smaller. So the big question we will try to answer is whether the braces are actually bigger than the drawing shows.
Paul reached a milestone on the truck for the Shay. This has now been needle chipped to the point at which we should be able to give it a final application of degreaser then a final steam clean and be ready to inspect and repaint. Given the large number of visitors to be expected next weekend for the UP event, steam cleaning will be scheduled two weeks out. This is not something you would want to be doing with many visitors passing by!.
Nigel
Comments
Sun, 05-19-2013 22:13
Hello again. I had an idea that was (somewhat rudely, mid-sentence) dismissed in talking to a museum volunteer a few years back, but here it goes [...]
Thu, 05-16-2013 21:52
Looking good Bob! I hope to come out soon once I'm done with school.
Wed, 05-15-2013 21:28
I was not around at the time. General discussion suggests that it was "pretty marginal" in a number of areas. Nigel
Mon, 05-13-2013 11:08
"THUMBS UP!"
Fri, 05-10-2013 02:15
No, it will not be necessary to hold any of the work waiting for the plow to be turned, end for end. Weather will be the major factor, but there will [...]
Thu, 05-09-2013 19:54
The CGW X-38 plow is really coming to life. Bob Kutella and Vic and crew need to be very proud of your collective efforts. I am very appreciative of [...]
Thu, 05-09-2013 15:20
The snowplow looks great! Are you going to apply the door and upper windows befor it is turned to continue work?
Thu, 05-09-2013 09:09
Max, Is there any progress to report yet, in regards to the installation of the poles and overhead wires? Have a good day, sir.
Wed, 05-08-2013 18:40
Thanks for the update! I still don't understand why Commonwealth #5 was removed from service. Do you know why?
Tue, 05-07-2013 09:28
Mr. Kolanowski.....I was just wondering if the Spaulding webcam will be up and running soon for us stay-at-homes. Thanks!2FP
Mon, 05-06-2013 23:04
Max, Has work begun yet on the construction phase of erecting the poles and putting up the wire? Wish I could be there to watch it happen.
Mon, 05-06-2013 23:02
Keep up the good work, Bob. Wish I could be there to help!!!!!!!