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Sunday, October 28. 2012
Steam Department Update 10-27-2012 Posted by Nigel Bennett
in Steam Department at
12:04
Comments (4) Steam Department Update 10-27-2012It was another day of progress in the steam shop. As mentioned last week, the objective is quite a few weeks of "more of the same". The focus was on re-tubing 1630 and this week saw steady progress: · a further bale of 37 new tubes was brought into the shop. This means that more than half the total (about 170) are now in the shop; · Jerry had cleaned off the swaged ends on the batch that were swaged last week. These were annealed at the other end and moved up to the locomotive; · 28 tubes from the new bale were swaged. This takes us to about 45% of the total swaged. At least this now seems to be a "production" process. We were doing one every 2 -2 1/2 minutes yesterday. The limitation is space. It is not safe to stack a whole bale (37 tubes) on the "hot" side. 28 was found to be about the safe maximum; Here you can see the actual swaging operation as the red hot end of a tube is hammered between the jaws · Ed continued work on the ferrules by cleaning the rough edges on those that are cut. He also confirmed with the electric car shop that they have an operational annealing oven that is suitable. So next weekend he will aim to anneal the ferrules so that we have a large supply ready for installation; · Master tubes were cut to each of 5 standard lengths and the inside boiler team (Eric and Collin) test fitted these to the boiler. The results were good. Each tube provides the required projection at front and rear when fitted to holes identified for that color; · Later in the day the master tubes were used to cut the first 10 tubes ready for fitting. For those of you visiting the shop there is now a clear progression. New tubes are brought in at the South end, swaged and annealed. Once this is done they move up to a stack on the engineer's side of the locomotive. From here they are taken to the chop saw, cut to one of the standard lengths and then stacked on the fireman's side. From here they will be lifted into the boiler and placed in the tube sheets. On the patch we encountered a, hopefully minor, set-back. When fitting the new plate it became clear that two additional rivets will be too close to the weld line and so will have to be removed and refitted. With the 11 that are already out, this will bring to 13 the number that have to be replaced and refitted. A nuisance as these 7/8th rivets are tricky beasts and require a good deal of work to get out. In other areas · the new air tank was fitted with plugs and connections so that it is now water tight. A pressure gauge was fitted and it was filled with water. This will allow the water that we need to hydro-test it to warm up in the shop during the week and also serve as a reservoir when testing the super heater flues. (Hydro tests need to be done with warm water). · good progress was made on cleaning out the valve block for the planer. This has now been freed of gunge and the valve passages polished. I am leaving tonight for a 10 day business trip to the UK so will not be at the shop next Saturday. So there will not be an update next weekend. Nigel Sunday, October 21. 2012
Steam Department Update 10-20-2012 Posted by Nigel Bennett
in Steam Department at
21:19
Comments (0) Steam Department Update 10-20-2012This was a productive day in the steam shop but may sound rather dull from the blog perspective. In essence successful progress toward having 1630 running next year will depend upon doing the same repetitive tasks for much of the next month or two. The question is often asked - will 1630 be running next year?. The answer is that we sure hope that it will and are doing our best to ensure that it does. One thing that will have a major effect is funding. While we have the major materials in hand, we are now pretty much out of funds on both 1630 and 428. There will be steps where we can save time by having some work done by specialists but we currently do not have that option. So .................. please consider donations to the 1630 or 428 funds. The next major milestone is to have the boiler water tight again. To do this we must refit about 180 fire tubes plus 16 super heater flues and fit the patch in the firebox. Once the boiler is proved water tight we can move on the last leg which is to refit super heater elements, accessories and lagging before carrying out the hydrostatic and steam tests that will prove fitness to run. Fitting each tube has several steps · the tube is first swaged, which means reducing the diameter of the 2 inch tube to 1 7/8th at the end which will be fitted into the rear tube sheet. This is done by heating and then hammering in the dies of the swaging machine. · the tube is then cut accurately to a length that will allow 1/4 inch projection at the rear tube sheet and 1/4 to 3/8th at the front. Since there is a variation of close to 1/2 inch between the longest and shortest tune, this requires matching of tubes to specific locations. · copper ferrules are then expanded into the holes in the rear tube sheet to make a better seal between the tube and the tube sheet. · tubes are then placed into position and the process of fitting can begin. The fitting is itself a multistage process consisting of: o expanding the tube, using a set of rollers, so that it is a tight fit into the tube sheet; o rolling over the projecting end of all the tubes in the fire box and some in the smoke box o further expanding the tube just behind the tube sheet to provide a second level of sealing. Each step will not be completed for all tubes in sequence as, for example, we do not have sufficient space to have 180 17 foot tubes in the shop. So some will need to be located in the boiler before we can swage more. Thanks to Eric Olson for the photographs below, which show the swaging operation. Shots of this operation were hard to come by as I am busy playing with a red hot tube rather than a camera!!. Step 1 - the end of the tube is heated in the oil fired furnace: Step 2 - a wire brush is used to remove mill scale from the surface of the tube which the hammer might drive into the metal causing surface damage: Step 3 - the tube is briefly re-heated, then the end is placed into the swaging hammer. The tube must be turned steadily while the hammer is working to get a smooth surface and even reduction in diameter. One of the learnings is that, while I have loaded the tube and am operating the swager, Jeff is turning the tube. The tube is so darned hot where I am that you cannot grip it to turn smoothly even with heat resisting gloves. Step 4 - The tube then joins the stack of swaged tubes to cool while we move on to the next one: This week, within this overall process: · we completed marking the tube sheets so that we can now clearly see which length of tube is required for each hole and into which hole in the rear tube sheet the tube must run from each hole in the front tube sheet. · after encountering a few problems with the swaging machine, we established a good "production" process and swaged a further 20 tubes so we are now up to about 45 swaged. · calculated the length of tube required to correspond to the measured lengths between tube sheets and cut the first of the standard lengths. The game plan will be to ensure thru test fitting that a standard tube of each length correctly fits a sample of the holes in the tube sheets for that length and then use these as a pattern from which to start "mass producing" tubes of each required length. · in addition to the work on the tubes, the patch for the firebox was bent on the McCabe and, when I left, there were some fairly positive mutterings coming from inside the firebox where Mike was offering it up to its location. Having the patch accurately formed to the mud ring will be a big step forward on that activity. This provided an interesting demonstration of the power of the McCabe flanger. This is 1/2 inch thick steel boiler plate. The flat section of plate is clamped into the jaws: As air is applied to the main cylinder the jaws move down and bend the plate. The startling thing when operating the machine is that there is no noticeable change in tone or speed of movement as it contacts the plate. You have to watch carefully to see when you start the bend as the machine shows no load at all when bending this thick plate. ... and in very little time you have the full right angle bend. In other areas: · Ed and Bob further cleaned the valve block for the planer after a week in the cleaning tank. The flow of "black goo" now seems to have ceased and the internal passages look pretty clean. So hopefully that is now getting close to the point where it can be reassembled and refitted. · The "new" air reservoir was moved to the South end of the shop to set up for hydro testing. This raised some interesting questions about what sort of air filter was in place when it was used by the Milwaukee Road. Jerry removed the most incredible amount of debris from the bottom of the tank which seemed to consist of general dirt and dust held into substantial blocks by compressor oil !. So a productive weekend in the steam shop. Nigel Sunday, October 14. 2012
Steam Department Update 10-13-2012 Posted by Nigel Bennett
in Steam Department at
14:48
Comments (5) Steam Department Update 10-13-2012It was a satisfying day at the steam shop as we generally achieved what we planned for the day. Before getting down to the main tasks we had a small job for the track department. One of our less obvious roles for the museum as a whole is as "removers of unwanted bends from large lumps of metal". Our large antique press will bend (or break !!) almost any piece of metal. In this case it was parts of the switch mechanism from Johnson's siding that had suffered during a switching mishap. This was very satisfying as both pieces straightened well without breaking. The track team took them back to refit and knew we had the best of the deal as they headed back into the pouring rain and we worked on indoors. Well done guys !. On 1630, the key tasks were measuring the tubes for refitting and producing ferrules. · For the tube measuring we had two pairs of "inside" workers, Collin and Jeff in the morning with Eric and Jason in the afternoon with Rick marking in the smoke box. This shows the technique. The wooden beam is moved from one tube position to the next by the two guys inside the boiler, pulled tight against the hooked end in the firebox, and the colored ring shows how long the tube needs to be. The hole is then marked with the color of the first ring that projects beyond the sheet. Tubes will be cut to 4 lengths matching the colors and fitted to the appropriately colored holes. The other marking (A1 etc.) is identifying how the tube will be fitted between front and rear tube sheets. The guy in the boiler marks the rear tube sheet with the same number so that we can thread the tubes into the matching holes. This would not normally be necessary as front and rear tube sheets would have the same patterns so you could simply count across and down to match. Somehow, when the rear sheet was replaced 70 years ago, 1630 received a rear tube sheet in which the pattern does not fully match the front. You can see more evidence of this at the bottom center of the picture where there is a plug where once there was a tube. The rear sheet was set up for less tubes than were originally fitted so a number of holes in the front sheet were plugged. The complexity of matching from front to back caused some delay but, by end of day, the entire fireman's side and the area below the super heater flues was complete. So we should be able to finish this exercise quickly next Saturday. · Richard did great work on the tedious job of cutting ferrules. He worked at this all day so that we now have all that we need cut and many cleaned up on the wire brush ready to fit. The ones in the box are ready for use and the ones on the right await wire brushing. · Glenn and Jerry made improvements to the swaging area. This involved setting up rigid holders to keep the tube square to the machine while swaging. At the first run, it was difficult to ensure that the tube was at right angles to the hammer jaws so this should give us better accuracy. · We were also relieved to find, when we arrived, that the welding contractor had completed the safe ending of the flues. With this done we can go ahead and pressure test them before the weather gets too cold. In other areas: · Stu, Ed and Bob continued the rebuild of the planer. The hydraulic pump is now complete .... .............. and the now for the valve block. This shows it in position before removal. This critical component takes the output from the pump and feeds it to the planer to move the huge table to and fro against the cutting heads. The initial results of removing it and soaking in the degreasing tank were disappointing. There is a lot of muck and sludge in the valve block so they had to remove all the plugs and a good deal more soaking and cleaning will be required to bring this into a workable condition. · Bruce started on measuring up the axle boxes for 428 to plan the machining that must be done to create the new bearing faces. · Terry worked with Tom and Stu to plan the water supply changes. Hopefully we can borrow some flow measuring equipment before the weather turns so that we can design the means to inject water treatment chemicals into the flow as we fill the locomotive. · We set up the B&G water tank on the department truck ready for pressure testing next weekend. Weather permitting we will aim to test the flues and new air tank next week. So overall good progress. Nigel Sunday, October 7. 2012
Steam Department Update 10-06-2012 Posted by Nigel Bennett
in Steam Department at
12:16
Comments (2) Steam Department Update 10-06-2012A day of steady progress in the steam shop. The main focus was on refitting the tubes into 1630. At the moment it is all preparatory work to ensure that we can establish a "production line" process when we do the actual fitting. · The major step, with considerable assistance from Bob and Joel in the wood shop, was the production of a measuring beam. This is based upon Tom's experience from the last overhaul. The problem is that the distance between the front and rear tube sheets is about 17 feet and the sheets are not perfectly even. Each tube needs to have a fairly accurate 1/4 inch projection beyond the tube sheet each end and the variation between the shortest and longest, due to the variation is the sheets, is around 1/2 inch. So, to cut all to a standard length and grind down to the exact length would be a VERY slow process. Also test fitting each tube into the boiler in order to mark where to cut is very hard work. So, based upon Tom's experience the beam provides a much simpler approach. It was made with a hook at the rear end which, when passed thru the hole in the rear sheet, will hold the beam accurately to the face of that sheet. (Don't worry, this was taken before the hook was finally tighted onto the beam!) The other end is marked with colored bands at 1/8th inch spacing. We simply note which band is visible at the front tube sheet, mark the hole with that color, and repeat for 180 holes. We can then cut tubes to 4 lengths (1/2 inch longer than the measurement) and fit to the holes based upon the color codes. It will take some time to mark up the whole tube sheet but will save a great deal of time overall.
The other challenge that we confirmed in this exercise is a little anomaly with 1630. Normally the pattern of holes in the front and rear tube sheets is the same, which means that you can simply count vertically and horizontally to match where to place a tube. Snag !. Somewhere along the line, probably when the rear sheet was replaced in the late 1930's, 1630 acquired sheets that do not match front to back in some areas. This means that we have to be very careful in matching the holes when measuring and then number them at each so that we can place the tubes correctly later. It will be a LOT easier to make sure we have everything matched using a timber beam than to try and match using heavy steel tubes !. · Production of ferrules continued steadily. We produced about 40 so we should have the supply in hand by the time the length measurements are complete. The objective will be to place all the ferrules in the back sheet in a single exercise once we have done the measurements; · Glenn and Jerry cleaned up the ends of the tubes that we swaged last week. This points up a learning. The mill scale on the new tubes is a lot more difficult to remove once it has been heated and swaged. So, in future, we need to wire brush the new tubes before we swage. In other areas: · Work progressed on the set up of the "new" house air compressor. New is a relative term as it is an EMD locomotive compressor of 1950's build acquired from a Milwaukee Road shop. However it is an important pre-winter task as we will use a lot of air in tube fitting and riveting the patch. The existing compressor is getting "tired" and past experience is that digging the Sullair out of a snow drift and starting that up makes for a slow start to work on a winter morning. This is a major enhancement that is being funded from the annual Sanfilippo benefit. The compressor site has now been cleared and work is starting on set up. The site is subject to review. There are concerns that the compressor will be too noisy when running in the shop and it may be best to site it outside. However that could not be done until Spring to coordinate with B&G work on the shop. As very little change would be needed to piping or electrics between the two locations, we will set up inside now and decide, based upon experience over winter, if this is the permanent location. · Bob and Stu worked on the wiring for the water supply that we need to change to make it more readily usable next year. (It was a little embarrassing that the Leviathan team ended up using a fire truck to get water as the water system was so tricky to start). So a reasonable day of progress on several fronts. Nigel |
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Comments
Thu, 05-16-2013 21:52
Looking good Bob! I hope to come out soon once I'm done with school.
Wed, 05-15-2013 21:28
I was not around at the time. General discussion suggests that it was "pretty marginal" in a number of areas. Nigel
Mon, 05-13-2013 11:08
"THUMBS UP!"
Fri, 05-10-2013 02:15
No, it will not be necessary to hold any of the work waiting for the plow to be turned, end for end. Weather will be the major factor, but there will [...]
Thu, 05-09-2013 19:54
The CGW X-38 plow is really coming to life. Bob Kutella and Vic and crew need to be very proud of your collective efforts. I am very appreciative of [...]
Thu, 05-09-2013 15:20
The snowplow looks great! Are you going to apply the door and upper windows befor it is turned to continue work?
Thu, 05-09-2013 09:09
Max, Is there any progress to report yet, in regards to the installation of the poles and overhead wires? Have a good day, sir.
Wed, 05-08-2013 18:40
Thanks for the update! I still don't understand why Commonwealth #5 was removed from service. Do you know why?
Tue, 05-07-2013 09:28
Mr. Kolanowski.....I was just wondering if the Spaulding webcam will be up and running soon for us stay-at-homes. Thanks!2FP
Mon, 05-06-2013 23:04
Max, Has work begun yet on the construction phase of erecting the poles and putting up the wire? Wish I could be there to watch it happen.
Mon, 05-06-2013 23:02
Keep up the good work, Bob. Wish I could be there to help!!!!!!!
Sun, 05-05-2013 18:53
Ah yes, I have made such Jibs myself. If it were me, I would add in each corner an angled piece from the base to the Jib to act as sway bracing. [...]