It was a day of great progress and one very significant milestone in the steam shop yesterday.
The activity was largely on 1630:
· Fitting of the small tubes progressed very well using the methods established last week, with teams working both ends at the same time.
o Collin and Eric ground the projecting ends in the firebox and all of these are now ready to flare once they are sealed into the front sheet. As noted below, work on tubes in the firebox ceased for very good reasons in the afternoon;
o Phil cut replacements for the two tubes that had hit problems and these were fitted and expanded. So all the small tubes, other than the few that are in between the super heater flues and must be fitted as part of installing the flues, are now in place;
o Most of the ends that are to be beaded in the smokebox were also ground to length.
At times Brian and Eric were working simultaneously on this with an impressive rate of progress. Just a few on the fireman's side remain to be ground to length.
o Brian is rapidly becoming our expert on the tube roller.
Once the grinding of the engineer's side was complete he started again with the tube roller and worked steadily to the point that we are now substantially more than 50% complete in rolling tubes in the smokebox. Everything on the engineer's side and much of the lower area is now done.
· With installation of the small tubes nearing completion, Phil made good the paint (actually a specialized boiler treatment) on the 16 super heater flues to ensure that these are ready for installation.
· Phil also spent a couple of hours on the sand blast cabinet in the car shop cleaning up some of the rivets needed for the patch. ........... which brings us to the major landmark of the week;
· Dennis returned after a couple of weeks absence, due to illness in the family, and work restarted in earnest on the firebox patch. The tube fitting team moved out to allow full access to fit the patch.
o The patch was bolted into place, the last two rivet holes were drilled and bolts fitted thru them.
o After more cleaning, degreasing and tightening, the patch was finally secured in place and Dennis was preparing to weld when I left for the Soiree.
o I later received pictures from Phil. By the end of day the patch was fully welded into the inner firebox sheet !!.
o This is a huge step forward in correcting the problem that caused the locomotive to be pulled from service. It mean that we now have one more really tricky job to do before the repair is complete. All the bolts currently holding the patch must be replaced by rivets, which are 7/8 diameter and about 6 inches long. This will be a "fun" exercise but, once this is done, we will be close to the point where this part of the boiler is ready for hydro testing.
In other areas:
· Dennis completed welding the gear for the back head mechanism on the wheel lathe. Once the holes are drilled out and bolts fitted we should be able to assemble this part of the lathe and test it.
· Bob continued work on the planer;
· Dave machined new parts for the spring hangers on 428; and
· Jeff was able to install the first sections of the new compressed air supply to the South shop.
So, overall a very significant day for the steam shop.
No update next week as I am going to the UK on business. However, a lot is now in progress so I hope that there will be a lot more to report in two weeks time. I am hoping that there may be the opportunity to see some steam activity in the UK while I am there.
Nigel
Comments
Thu, 05-16-2013 21:52
Looking good Bob! I hope to come out soon once I'm done with school.
Wed, 05-15-2013 21:28
I was not around at the time. General discussion suggests that it was "pretty marginal" in a number of areas. Nigel
Mon, 05-13-2013 11:08
"THUMBS UP!"
Fri, 05-10-2013 02:15
No, it will not be necessary to hold any of the work waiting for the plow to be turned, end for end. Weather will be the major factor, but there will [...]
Thu, 05-09-2013 19:54
The CGW X-38 plow is really coming to life. Bob Kutella and Vic and crew need to be very proud of your collective efforts. I am very appreciative of [...]
Thu, 05-09-2013 15:20
The snowplow looks great! Are you going to apply the door and upper windows befor it is turned to continue work?
Thu, 05-09-2013 09:09
Max, Is there any progress to report yet, in regards to the installation of the poles and overhead wires? Have a good day, sir.
Wed, 05-08-2013 18:40
Thanks for the update! I still don't understand why Commonwealth #5 was removed from service. Do you know why?
Tue, 05-07-2013 09:28
Mr. Kolanowski.....I was just wondering if the Spaulding webcam will be up and running soon for us stay-at-homes. Thanks!2FP
Mon, 05-06-2013 23:04
Max, Has work begun yet on the construction phase of erecting the poles and putting up the wire? Wish I could be there to watch it happen.
Mon, 05-06-2013 23:02
Keep up the good work, Bob. Wish I could be there to help!!!!!!!
Sun, 05-05-2013 18:53
Ah yes, I have made such Jibs myself. If it were me, I would add in each corner an angled piece from the base to the Jib to act as sway bracing. [...]