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Thursday, December 31. 2015Diesel Shop update from 12/30On Wednesday, more work continued on UP 1848 and CB&Q 504. Dan C was out to the shop during the day to begin repairing and changing some rectifier modules that had failed on 1848 a few weeks ago when moving the coal trains in for storage. We had a number of parts in stock that we acquired from some other B40-8's that were being scrapped. Those modules were in great shape and were used to replace the two failed ones. He also made some repairs to the 504, disassembling, cleaning and reassembling the isolation switch which was getting very sticky in the cold weather. And repaired a couple broken wires on some contactor interlocks that was caused by a raccoon that had worked its way into the electrical cabinet. Jeron and I started working on the cab heat pipes of 504, removing some marman couplings, cleaning the pipes, clamps and rubber. To do this, we spend a while fixing the sandblasting cabinet, new media, screen protector, cleaning filters, etc. After getting the pipes and couplings together in the side sill, we opened the cab heat return valve at the expansion tank to charge the cab heat pipes. Everything underneath was in pretty good shape at this point. However, the firemans side heater had a number of issues. We spent a good amount of time removing three bad rubber hose couplings and one marman coupling. There isn't much clearance under the heater to get everything out easily without separating every connection. All those fittings were cleaned and everything is ready to go back together once new rubber and gaskets arrive. The brushes in the motor were stuck as well, so those were removed, one of which by having to take the entire motor apart. Cleaned those up and reassembled, now it's working great. A few other odds and ends, Jeron starting testing a bunch of radios we had in stock that were not working, but had no labels as to what was wrong with them. We'll see if we can make some good ones out of a few bad ones. We also tried out a new portable battery charger ARMS, Inc. It has a built in battery energizer as well. It is a very nice unit, and much easier to move around than the huge LaMarche units we have that really aren't mobile at all. Jeron located new sockets and a light shade to repair the ground lights the next time around. Hope everyone has a safe and Happy New Year! Tuesday, December 29. 2015
Holiday lights, Holiday trains, ... Posted by Roger Kramer
in Passenger Car Department at
19:05
Comments (0) Holiday lights, Holiday trains, Holiday decorations
Here is a pictorial about the Holiday Train event. IRM had a very successful Holiday Train event this year using for the first time, a diesel powered three CNW bilevel consist. This two weekend event was under the leadership of Paul Cronin, Coach department curator. It was so successful that we are increasing it to three December weekends in 2016. More planning is needed but already we are looking for volunteers to help expand our campus decorations. Anyone who likes to put up a Christmas tree and decorate it with all the lights and ornaments is invited to talk to Paul. We have a great opportunity to make Irm a beautiful 2016 Christmas wonderland! The possibilities are boundless! HO! HO! HO!
Looking West towards barn 9 as the Holiday Train moves out of the yard and onto the main line with the children and Santa Claus An interior view with a young family enjoying the train underneath the Christmas tree. Henry, you did a great job setting up the train. Now if we only had a building to house all those model trains. The new trolley buses were operating on the loop bring our guests from the parking lot to the Holiday train. This worked out real well. This gave our customers another ride while providing a warm environment. Sunday, December 27. 2015Steam Update December 2015
Another year draws to a close and there is a lot of activity in the steam shop. I had expected the day after Christmas to be fairly quiet but there was a good turnout and work proceeded on many fronts.
On #1630 we are progressing along what is now the standard plan for the Winter with the normal annual inspection work, which is substantially boiler focused, running in parallel with “catch up” work to improve the overall mechanical condition of the locomotive.
Aside from some smaller items, the major focus this Winter is on the valves. It has been apparent for some time that there is wear in the valves leading to lower efficiency and leakage that can be demonstrated when the valves are set in specific positions with steam applied. As with most backlog work, the initial hope that we could get away with a quicker and simpler repair has proved sadly misplaced!. Guess we should not be too surprised. When doing the initial stripping we found some tags set behind the valve chest nuts that indicate when last stripped for overhaul – SLSF Springfield shops 1947!. You really have to question the quality of the work when we have to do it again after only 68 years!!.
The findings so far are a mixture of good and bad news.
In parallel with the valve work, a lot of other tasks have been progressed.
On the Shay, work proceeds steadily.
On #428
On shop services, the large compressor is now fully plumbed in. As soon as we can get the power connected to it we can test and adjust it ready for the state inspection. With luck this will be ready when we want to rivet the smokebox of the Shay.
So a lot of activity but a whole lot more to be done if we are to be ready for running at the start of the season. So, Happy New Year to all and watch this space!.
Nigel
Thursday, December 24. 2015
Diesel Shop update from 12/19 and 12/23 Posted by James Kolanowski
in Diesel Department at
14:32
Comments (3) Diesel Shop update from 12/19 and 12/23While the 504 and 1848 were still in the heated shop to keep them from freezing, Jeron and I decided to work on a few little things that have needed attention. On the 19th, Jeron removed, cleaned, and reassembled the automatic air drains on the main reservoirs, and along the way found out that one of them to have a small crack in the housing near the manual part of the valve. It will be replaced later this winter. He also tracked some some other small air leaks, repairing some and noting some others for future repairs. There was a copper pipe on the drain side of an auto drain that had a split to it, that was soldered shut and put it back in place. Meanwhile, I started working on the air brakes. An issue started to occur where the independent brake would not stay bailed off. The fix here was to replace the 26-F quick release valve and the control valve which had a slight leak to it. At the same time a couple of filters on the air system were replaced. There is one more issue where we are waiting for a valve to ship from PABCO. Last night we spent a couple hours at the shop doing a little more TLC work on 504 and 1848. On 504, the platform crosswalk lights never had the lenses put in from when the restoration was completed years ago. They were just blanked over for the painting. I used one of the old fogged lexan windows from the bilevels and cut out a couple squares with the sawzall for the front and rear. Screwed and sealed it with some clear silicone so water won't get into it, let it dry and screwed the plates, with lenses, back in right before leaving for the night. The radio had quit working earlier this year, but we never had the time to troubleshoot why. A little bit of looking this time found no voltage at the radio rack and nothing at the radio breaker. Traced the wires back further into the cabinet only to find a broken one near the knife switch. Placed a butt splice on that and the radio works again. Jeron replaced a bulb on the transmit indicator as well. On the 1848, Jeron rebuilt one of the rear sander magnet valves that was sticking and leaking a bit. There is still more to do on these after some rebuild kits are ordered. We also straitened out one of the rear break away stanchions for the crosswalk safety chains that was not exactly straight. Over the next couple weeks, some other items will be done on both units before they get moved out of the shop and other equipment comes in for work.
Wednesday, December 9. 2015Barns 13 and 14 updateHere is the latest pictorial news concerning barns 13 and 14. The last two weeks a contractor has been working to install all eight new roll-up doors on the eastern end both barns. His work should be completed by the time you read this blog. Next on the schedule is the installation of power and lights to both barns. Max Timms is constructing the main electrical panel here in barn 14. What a professional job. Thanks Max! Want to help make the next barn 15, a reality? Please send your year end donation in and mark it NEW BARN 15 CONSTRUCTION! Thanks Roger |
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Comments
Tue, 01-19-2021 20:11
Dear, IRM The N and W 611 is coming to the IRM 2021 NHS. OK IRM.
Fri, 01-15-2021 10:20
Hello Jason. Your comments are very much appreciated. Yes, there is much hard work that goes into all our restorations and maintenance here at the [...]
Fri, 01-15-2021 10:13
Hello Jack Yes, It will be one of our most impressive cars that we have at IRM when its completed. Thanks for the pat on the back! Roger.
Thu, 01-14-2021 21:05
Those cars look great so far guys! Man I wish I had the time to volunteer and become a member at IRM that looks like so much fun especially with how [...]
Tue, 01-12-2021 16:30
the pawnee is looking great a pat on the back to all involved
Wed, 01-06-2021 10:14
Good job on coach updates January 5, 2021. Sincerely, Ethan A.
Mon, 01-04-2021 12:31
Hello Jack Happy New Year from IRM. To my knowledge there was no damage from the minor ice storm that we had in late December, 2020. Some [...]
Sun, 01-03-2021 20:12
the museum area had lots of ice storms in area did the museum get a lot of damage
Thu, 12-24-2020 13:27
roger, Thank you to all of the Passenger car department volunteers. The #109 is going to be a great car when all done! Ted miles, [...]
Sun, 12-06-2020 08:46
Hello Ted We havenot finished lettering the 975 but we are well on the way. Look for a few blogs from me now that the wearther is colder and the [...]
Sat, 12-05-2020 18:36
i watched crew replace switch by diesel shop on dec 5. its good to see museum have equipment to do job and save money
Fri, 12-04-2020 14:56
It has been a long time with no news; have you finished lettering the Southern Pacific locomotive? Please post a picture. Ted Miles, IRM Member