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Monday, October 17. 2011
Track 31 Update - October 15-16, 2011 Posted by Robert Kutella
in Track Department at
15:29
Comments (0) Track 31 Update - October 15-16, 2011There was a lot going on this weekend so I will post a few pics and short report on the project to rebuild 31 Track and some work on the turnouts leading there, to start out the posts this week. There was a large track crew on hand, here seen spiking in new switch ties at the first switch in Yard 3. The old ties were pulled out and new ones slid in under the rails. On Sunday a mechanized tamper ventured inside the dark confines of Barn 3 to make the first tamp on the new track and gravel. Adam Robillard was at the controls. Sunday, May 22. 20112011 Mainline Tie Project
This
year, like most years, the museum’s Track Department undertakes a large
tie renewal job. This is a necessity to properly maintain our railroad
and allow for a high quality ride all of our visitors and volunteers
have come to expect. This year, it was decided to undertake one of the
largest tie renewal projects to date, nearly 750. Typical years may see
500 ties replaced anywhere on the property where they’re most needed.
This places a huge strain on us to complete the bulk of the work before
operations ramp up in April and May. Whether it’s the Mainline, Carline
or little used yard track the importance of maintaining our track for
the safety of the public, our volunteers, and the fragile equipment we
operate is always the top priority of the Track Department. Always…
So what does it take to get the job done? This process began last year with the purchase of the 750 brand new ties to be installed. All of which were delivered by truck and unloaded on the property. During this year’s detailed track inspection beginning in the cool month of March we walked up and down the railroad not only inspecting the track, but also marked bad ties to be replaced. Once a majority of the ties were marked for replacement we had to figure out the best way to get the new ties on site. This year, because of the huge quantity of ties, we found it best to load all of them onto a flatcar and roll them out to the site. With our Burro crane we unloaded all of the bundles in the general locations that would be needed. This is not an easy process and most of this work happened during the last half of February and into March. Needless to say there was plenty of ice and snow on the ground to make the job difficult. With the ties all on the ground, the lengthy process of placing each tie in the exact location where it was to be installed began. Mostly, this involved the tie crane and an operator working eight or nine hour days over the weekends. This step took many weekends throughout March and April to complete. While that was happening, we also moved new spikes in locations they could be accessed and continually worked on machine maintenance. Things break, machines wear out, and we spend a lot of time and elbow grease keeping the machines in running condition. With only our small core group of volunteers, and without the necessary equipment to do the actual replacement ourselves, we hired a railroad contractor to truck in their own equipment and swap the bad ties for the new ones. This took a solid week for the contractor to finish the job and then the cleanup of all the material was left to us. As with most tie projects, the work typically disturbs the track severe enough to require a slow order. The problem of support under the ties becomes an issue without being properly tamped. Until that happens, the ties may not have enough ballast underneath which could create an unsafe condition. At this point the race was on to clean up the railroad before the operating season gets into full swing. During this time all of the old ties were collected with the tie crane and placed in one large pile near Johnson Siding where they will eventually be picked up taken away by another railroad contractor. Just like when they were all set out, the job meant the tie crane and operator must spend long days peddling ties back and forth. This year it took us five or six full working days and detailed cleanup still isn’t finished. In addition to all of the ties, other material had to be picked up, such as old line poles and tree limbs. This adds considerable time and energy but needs to be done. With the wood picked up we focused on gathering all of the steel scrap which took the form of 2,800 spikes from the tie job, hundreds of old tie plates and other track material left on the line from years past. This could only have been done quickly and efficiently with our Burro crane and its electromagnet. We took one of our flatcars and ran up and down the line until the flatcar was full of steel and brought it back to the property to be sorted. That brings us to today. The next steps will be to get rid of our huge tie pile at Johnson Siding, and surface the railroad. Surfacing the railroad will be done in house using our ex Amtrak production tamper purchased a few years ago. Contracting an operation such as this would cost the museum another $40,000 and that does not include regulating the railroad afterward to finish the project! All of the work done in house by the Track Dept. easily cuts the total cost of the project in half and in this season alone has already saved the museum roughly $50,000. The alternative to any of what we do in house involves renting and trucking in equivalent machinery and paying contract wages. Work will continue throughout the season to tamp and dress the line working between operations and special events. Follow up maintenance on all of our machines and sorting materials from the line will take many more weekends of work. Without the equipment we have, most of this wouldn’t have been possible. While most of this work goes unseen to a majority of our volunteers and visitors, it is this work that is required for our museum to function as a world class operation. None of this could be done without the dedication of our Track Department working odd hours in all sorts of conditions. Thanks to all who have helped on this project including Frank DeVries, Tom Hunter, Bill Lygiros, Patrick Shea, Jeron Glander, Mitch O'Brien, Bob Olson and Adam Robillard. Also we must thank everyone who supported the work including, but not limited to, the Operating Department granting us track time, Dave Diamond in the Buildings & Grounds Department, and anyone I may have missed. …and that’s what it takes to get the job done More Track Dept. photos from Frank Devries and Adam Robillard can be found in the Member's Photo Site here- http://www.irm.org/gallery/Members-Photos Saturday, April 30. 2011Saturday Track Report
Trying to beat karma to the punch....
The weather was beautiful today... and that was the problem... Today's plan was to get some minor repairs done on the tie crane. We are once again getting ready to go pick up about 720 ties that were changed out by Volkmann a couple weeks ago. So to avoid problems we did a little preventative maintenance. I arrived at the museum about 9AM and found Bill there already. Bill and I started to de-fuel the tie crane. Even though the fuel was out of the sight glass there was still about 10 to 15 gallons of fuel left in the tank. We drained the fuel then took the hose off the tank. We also removed the fuel sight tube to replace that as well. Jeron showed up and we ran to town to grab parts. While I replaced the fuel hose, and sight tube, Jeron replaced the damaged mirror and Bill replaced the windshield wiper. We drained the fuel out of the transfer tank, but that was a drop in the tank so to speak. Unfortunately I left my keys in my winter coat..... at home.... SO no truck key, no fuel key.... Guess I'll fuel the crane in the morning. After that it was time to take in some of the sights of the Illinois Terminal to do. I took a ride (my first I'll add) on the IT B motor, to see how the ride is after our tie change out. It's not perfect, but the 25MPH speed restriction seems to be adequate until we can get the line tamped. While out and about today I did find three more sticks of rail along the ROW, that we need to get picked up and in the gon. One is out near the Big tree, the other two are along the main line just east of the depot. We also need to re-set the whistle post along the main. I think we can just pick it up and add some ballast to hold it up. While all this was going on, Dave and Evan continued work on the 580 Motor car. They have most of the wood off now, and have started to clean old paint and rust off the frame. They bought a couple of wire wheels for my grinder and were using that to clean it up real nice. They were getting ready to spray on some primer when I was leaving for the day. It's looking really nice. I also found one of the brake leaks on a caliper thanks to all the wood being off. Nice work guys! I'll post some pictures to the Members photo section in a few minutes. Frank D. Sunday, April 3. 2011Saturday 4/2 Track report
Today was a new member spectacular!
The day started with myself and new member Keith Ziolkowski joined me and returning new member Bill. We found the model 50 missing it's exhaust circuit, under rebuild by Jeron. So a Plan B was formed. Off to 14-4 track to solve a reverse super elevation problem on the curve to this track off the switch. We gathered jacks, bars, forks, and shovels, onto the tie crane and off to yard 14. We hand jacked the track and hand tampped from about 8:30 to 11:30, picking up the outer rail from "in the mud" to out of stone. A lift of over 6". After lunch we took the regulator back to yard 14 and dragged stone from the north side to the south side to fill in the cribs that were now devoid of stone. A quick broom job and the track was back to a useable status. Before this work, when the diesel department would try to switch cars on this track they had a tendency to derail when being pulled out. Meanwhile back on the main........ Tom showed up later in the morning and fired up the mower for one last trip on the main before it leaves for a job. Tom was able to mow by Karstens crossing, cleaning up some trees that the farmer cut down and pushed over onto the property. He also was able to give a good pass between East switch and West Switch. Third trick was Jeron coming out after work and installing a new exhaust elbow off the turbo. The old 90 degree bend had been previously welded, and subsequently rusted out again, and as Tom put it, made it smoke like a Russian tank. Jeron was able to find a suitable part and had Jamie from the diesel shop weld the flange to the turbo onto the new pipe. The exhaust was then put back on the crane for the Sunday activity. From what I understand it was a real wrestling job to get the exhaust back in. During the wrap up of my tour of duty, Dave, and his young son Evan showed up having just joined the museum, and coming out to see what they can do as a team to help IRM. Work on our motorcar fleet was offered up, and they are eager to get started. Unlike last week, cameras were on hand to record the festivities. Photos from Tom and myself have been posted here: http://www.irm.org/gallery/album155 Frank D. Sunday, March 27. 2011Track Report
First off - not a single photo was taken this weekend, we were all just too busy.
Saturday was a productive day, Adam was a surprise visitor as he had some things to take care of up north for a day, so he joined Frank and we always can use the added help. Frank and Adam worked together taking care of joint repairs, marking ties, fixing one of two pull apart, cleaning the ROW and starting the process of switch lube - all from the Santa Fe hyrail truck. I spent the entire day setting out ties from the big tree to the east end of Johnson, picking up where Jeron left off - the CN gon never arrived of course - we worked until well after dark to get it all done. Sunday was just Mitch and I doing some machine repairs - we pulled the bottom bearing from the mower side bar, and cleaned it up in the car shop. We found out why the bolts broke - the bearing is worn out and caused the housing to wobble breaking the bolts. As it is in a trapped hanger, Mitch and I put it all back together without the bolts (that have been broken for years) and fired it up after sitting by Yard 3 all winter - the mower is now back in machine row at Yard 11. I plan to run it on the ROW some next weekend. We spent some time in the Industrial Brownhoist crane with the steam shop folks who are making it ready for service for the Barn 23 track project. We got a plan together for changing out some grease fittings and will get that one ready in the next few weekends as well. Over the next week Jeron will get the 4 inch long sweep exhaust 90 deg bend for the 50 and we can get that installed - as the CN gon was a no show on Sunday too... soon enough we need to be ready to unload it. A productive weekend for sure - Be Safe out there Tom Sunday, March 20. 2011Weekend Track Report
Long Days and tons of work done... well how about one long day and a day to watch thunderstorms and do some flat car planning...
This weekend we continued where Adam and Jeron had left off the week before, we set up the crane train and set off the last of the tie bundles. It was a long day of hard work - and we were joined by more new folks - and Patrick who it appears that we did not scare off (yet). We were also joined by Mike Potter - it was good to see him out for a day, and good to have him along to make the cuts and couple back up every time we have to set off a bundle close to the crane - as you cannot raise the boom under the wire - For the gang we had Adam for his last day of spring break, Frank, New guy Bill and Patrick - we also had Greg from the electric car join us and of course Mike Potter. At the end of the day Steve joined us as a ground man fresh from the new CP UTU rank. While the gang unloaded the ties between Johnson and the Farm Crossing - Adam spent the day spotting the ties where marked - about 400 of them. We have about 300 more to spot. Frank started marking the rest of the bad wood - and Jeron will dig into the tie crane to spot the rest this week. We hope to get the tie gang out in a month or less to get this done - then we have all the mess of the old ties to pick back up. As soon as we had the last ties off the car, we took a bit of time to set some signal heads with the crane while we were out at Johnson - have to use all the equipment as much as we can for each other. We worked so hard that we did not take any lunch time until after 3P - as we wanted to get all the ties out and give the railroad to the electric car department to train on the CA&E trains. After lunch we set the TTX car back on the interchange and a few of us finished the day off with some scrap loading into the gon with the mag to pick up some more of the scrap around the place. Sunday tuned out to be really rainy with thunderstorms - as we had so much under our belts by then, Frank - Jeron and I just spent some time talking the rest of the summer plans watching the show from Barn 2 - Next weekend the inbound CN OTM car unloading will be the show (if it is here). Be Safe out there Tom |
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Comments
Wed, 04-11-2018 11:28
You mention in the header that you would like to have the Electroliner operational by its birthday. Was it?
Sun, 04-08-2018 20:03
As a child, IRM was always my favorite place to visit. Well, other than grandma's house next to the Geneva Sub. It's been many years since I now [...]
Wed, 04-04-2018 16:01
Those temporary walls could be constructed in a way that allows their reuse after the phase is done to close off the new phases.
Tue, 03-27-2018 03:08
Why did the smoke box cover on the shay need to be replace Do?
Mon, 03-26-2018 16:29
It never ceases to amaze me of the diligence and passion of the current mix of volunteers associated with IRM in 2018. Back when I was a active [...]
Mon, 03-26-2018 11:10
Awesome paint job Jamie!!! I never would of thought with the Rock Island history this locomotive in this scheme would of been preserved. Thanks for [...]
Sun, 03-25-2018 23:56
The Hick's blog lists it as Fruit Grower's Express FGEX #55407. Arrived in Union June 2016.
Sun, 03-25-2018 20:51
Good job on the diesel update 2018. Sincere, Ethan A.
Sun, 03-25-2018 20:45
Good job on the steam update 2018. Sincere, Ethan A.
Sun, 03-25-2018 00:12
Bill, The 1990 Roster has the PFE #68428; this may be the reefer that we saw moved. It is a rare car and deserves a paint job. Ted Miles, [...]
Fri, 03-16-2018 11:10
It would be rather difficult to operate an 11,000 Volt AC locomotive on our 600 Volt DC wire.
Thu, 03-15-2018 05:57
Good job steam update. Sincerely, Ethan A.