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Monday, March 14. 2011Sunday's Track ReportRiding on the success of yesterday's progress today our two goals for the day were to clean a few machines with the pressure washer, and unload the ties loaded onto the flatcar yesterday along the mainline. The short version of the story is that both jobs were completed but not without a little excitement in between. The crew today was myself, Tom Hunter, Jeron Glander, and a new volunteer, Patrick Shea. We started right away with the rented 3000psi heated pressure washer and cleaned up the tie crane, regulator and Model 50 Burro crane. After cleaning the radiators on the burro it ran significantly better now that it has proper air flow drastically minimizing the possibility of overheating the engine. We picked up our loaded flat car of ties and the EJ&E 529 caboose and headed out onto the carline. The rest of the day was spent unloading around 400 ties along the mainline. Tom expertly ran the crane while Jeron, Patrick and myself hooked and unhooked the bundles along the line, mostly between Seeman Rd and Four Mile Siding. We'll come back out with the tie crane sometime soon and distribute the ties where they'll be installed. It was an incredibly productive day and called it quits after tying up shortly before sunset in Yard 11. This week the rest of the ties (~250) should get loaded onto the flatcar which should allow us to repeat the job again next weekend. Thanks again to Patrick for joining us for a second day in a row. Hope we didn't scare him away. Adam RobillardIRM Track Dept Sunday, March 13. 2011Saturday Track Report
Saturday's plan involved a two pronged attack. One group was to finish walking the mainline, the second team was to load the mainline ties onto a flatcar, so they can be peddled out for install in the coming weeks.
Again, I picked up Marcus at Aurora Transportation Center, and we drove up to Marengo Cafe for breakfast. After Breakfast we met a new volunteer to our group, Patrick Shea. Adam joined us at the caboose on 110 track and the plans were set in motion. Marcus and I walked track. We started with the stretch from East switch to Karstens, so the diesel department could use the east switch as head room for fueling diesels. We then continued out to signal 201 with no significant defects found. The walk continued from East switch to West before we broke for lunch. After lunch we finished off the West end finding one broken bar. The total repairs for this spring, two pull aparts east of 4 mile siding, which is still out of service, One broken bar on the main between 201 and 251. One broken bar at West switch. We intend to have the two broken bars fixed before the start of the season. The pull aparts depend on getting some warm sunny weather to get the rails to expand enough to get new bolts in the rail. Adam and Patrick grabbed the fork lift and started loading bundles of ties onto the TTX flat car that the Camp Grant arrived on. All the other IRM flats are in use, so we pressed this one into service since it was just taking up space in the siding. The diesel department was kind enough to retrieve it and bring it to along barn 9 for us. In short order Adam and Patrick had the flat loaded up and ready for Sunday's distribution party. A break for a brief meeting, and we were back at it putting the train together. Tom joined us for this phase of the job. Tom finished off getting the four part hook put back on the crane. The hook was taken off last year to rig up the clam shell for loading stone. Tom, Marcus, and I, then got the 529 caboose moved over and the loaded flat car onto track 112, while Adam and Patrick loaded a couple more bundles of ties onto tie flats with the tie crane. The tie crane was tied down in yard 10 for the night. Tomorrow's projects, go out and peddle ties where we marked ties for replacement. A few photos have been posted here: http://www.irm.org/gallery/album271 Frank D. Saturday, March 5. 2011Saturday's Track Report
Today unofficially marked the beginning of 'the busy season' by inspecting the first portions of the mainline for its return to revenue service in the coming weeks.
Food started off the morning in Marengo with Frank Devries and myself. After arriving to the property we were joined by Bob Olson and began walking track from Seeman Rd working East. The priority was to walk and mark ties to be replaced this year as well as inspect for the usual defects; joint bars, bolts, breaks, culverts and anything else that isn't quite right. We walked a few hours before calling it lunch at Subway. Tom Hunter met us there and we were off for a few more hours of inspection. We officially walked from Signal 201/202 all the way to the east end of the line. A few hard miles in full winter gear. Totals from the day include 387 ties marked for renewal between West Switch Johnson to Four Mile Siding (+ a few more not yet marked), one center broken joint bar and two pull aparts. At least another 100 ties will be marked once we clear ballast off the track between Poles 39-46ish. The goal is 700 ties on the mainline this year which we will begin to distribute next weekend. Slow orders and O.O.S. bulletins ARE posted and will stay in place until repaired. We called it a day with dinner at Joe's and wrapped up a lot of loose ends. Frank will be out tomorrow and next weekend we'll begin loading flat cars with ties for distribution and probably working on repairs as well as continued inspection. Come out and join the fun! ***If you're interested in helping out give me a shout at lzeje657@msn.com or find any one of us on most weekend and we'll get you hooked up! Adam Robillard IRM Roadmaster lzeje657@msn.com Sunday, January 16. 2011January 15th Track Report
Today's track report starts with a trip to the Aurora Transportation Center to pick up Marcus. Marcus has not been out for quite some time, and was suffering IRM Withdrawl, so I agreed to pick him up at the ATC and bring him up.
Proper track work requires proper sustenance, so the next stop was the Marengo cafe for breakfast. After breakfast we ran to Napa for a case of antifreeze for the model 50 burro. Later we would realize the value of this stop for another purpose... more on that later. Next stop was a conference with Julie on budgetary and trackwork for 2011. This conference turned into a long discussion that got slightly off topic but was fun even if not totally productive. When this conference finished, it was time for lunch. Yea.. long conference. Upon return from lunch, we got the 50 fired up and yes, the tranny was frozen up again. Attempts to thaw her out failed, so we left her running and went to work on something else. Almost on cue, Julie called and advised the block heater that Adam had ordered for the tie crane had arrived. Plan B was hatched. Marcus and I got the old heater off, and quickly realized we would have to re-use the mount since it had a hose mount off of it that was absent from the new mount.. not a big thing. As we were working on this task we were joined by David Fullarton. He helped us finish off the filling of the radiator since we had a full case of new anti freeze from earlier in the day. So we return to our idling 50 and find the tranny is finally ready to work. We put Marcus in the crane, swing over and pick up the scrap gon, and go mag some diamond parts. About half way through the pick up, we put David in the hot seat and had him work the magnet. I hung off the side of the cabin, for the first few pics talking him through the steps. David picked up running the crane fairly quick, so I got back on the ground to help with the picks since some of the derbis was frozen. After about a half hour we had the pile picked up. The last pick a big chunk did not want to fall off the magnet. So we talked David through scraping the mag across the top of the car to knock it off. After that David ran the crane back to the crane's home and put her away. Last thing of the day was to check on the block heater of the tie crane. We confirmed we had heat from the new block heater, and attempted a start. No joy, still too cold. I'm guessing with a little more time on the block heater, and a little time on a battery charger, she will fire right up. We cleaned up for the day, then Marcus and I made a run to the Roundhouse in Aurora for dinner, before Marcus caught a train back to the city. Photos of the days activities are here: http://www.irm.org/gallery/album266 Frank D. Sunday, December 5. 2010
Track Department Report, December 5, ... Posted by Frank DeVries
in Track Department at
20:06
Comments (0) Track Department Report, December 5, 2010
Again, today's primary function is to protect the Santa Trains. Again, Today's cast of track department characters, was again, Me, Myself, and I. Tom Arrived around 1400 but was engaged in conversation for the duration of his visit.
Since mother nature finished with the white stuff yesterday, and the snow wasn't really drifting. So a quick sweep of the snow, and the switches were in service. Since there wasn't much to keeping the trains running, it was off to the barn where, as always, there is a plethora of work to do. This wasn't such a bad thing as the temps were hovering in the teens for the duration of the day. To start with, I replaced handles on a couple of spike mauls, and a sledge that all had met an untimely fate. Next up was to continue working on our hanger queen - the switch tamper. When last we left our heroes the switch tamper had a motor fail, as well as a power cable to another motor. There was also a hydraulic leak due to a failed crimp on one of the new hoses. Only on track machines can you do a 100% hose replacement, and still get failed hoses!!!!! So I found the old hose,and re-installed it to take care of the leak. Next up, was to re-wire the cable. The old cable was held into it's mount with some caulk and some press fittings. Fortunately we had replacement SOOW cable on the shelf, as well as the mounting lugs, so a repair was in order. All was going well until I went to wire the cable back on the machine. Apparently when the cable was taken off, one of the screws was lost. A small search was mounted and a suitable replacement was found. Next up was to remove the failed motor. Four bolts and a few minutes later, a small push and the motor was on the ground. About this time, it was time for a thaw break. Off towards the silver cars I went, when I was told of the festivities in barn 4. So some chit chat, some food and some awesome apple cider. Of course that about did it for work for the day. A tour of the KC PCC car by Frank S., one last throw of the switch for the winter trains, and it was time to call it a day. All that is left on the Switch tamper is to mount a replacement motor on the machine, and we should (again) be ready to work. Another big project for this winter is to "ring out" the wiring on the 6000 tamper and verify we don't have a wiring problem on that machine. Frank D. Saturday, December 4. 2010Track Department Report
Today's activity was to protect the Winter trains. Today's track department consisted of me, myself, and I.
Continuing the tradition, we have had snow for each and every IRM winter train season. The track department had prepared earlier in the fall for these trains, and in fact prepared a third switch for smudge pots to keep our switches clear of snow during these trains. Adam prepared the East Wye switch, and I prepared the two switches used previously, South Wye, and 50th ave. I arrived around 09:30 and it was still snowing. I loaded up a snow broom and shovel, and started work clearing switches. In about an hour and a half, I had the switches cleared of the 2 to 3 inches of snow, and the pots all lit. A quick trip to Karstens crossing to make sure the crossing wasn't iced in, and a quick lunch. Upon returning from lunch, I started to search for the clamps we use on the switch stand by Depot Street. I searched and searched without success. I figured I would do some creative engineering to get it through the day. When I arrived to hook up the battery, I pulled the end of the cable out from under the switch stand and found someone had already attached said clamps to the lamp. I hooked up the battery, then went to run an extension cord for the switch lamp at South Wye. I have no idea why one was wired for 12V and the other for 110VAC. We do need to take them down in spring and remove the wasp nests in both. The rest of the day was tending to the East wye switch, and keeping the pots lit. We had a couple that just did not seem to want to keep going. I wound up changing out a couple wicks and they were off to the races. The last train ran at 4PM. I made one more round to fuel the smaller pots, and put them out for the night. With no more snow in the forecast, we probably won't need the pots tomorrow. I will post some photos to the IRM Members page a little later. Frank D. Sunday, May 23. 2010
Saturday Track Report - The early ... Posted by Frank DeVries
in Track Department at
12:33
Comments (0) Saturday Track Report - The early edition....Thanks to the CN, and a malfunctioning crossing, I was up and out of the house by 5AM arriving at IRM at 6AM. |
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Comments
Sun, 05-19-2013 22:13
Hello again. I had an idea that was (somewhat rudely, mid-sentence) dismissed in talking to a museum volunteer a few years back, but here it goes [...]
Thu, 05-16-2013 21:52
Looking good Bob! I hope to come out soon once I'm done with school.
Wed, 05-15-2013 21:28
I was not around at the time. General discussion suggests that it was "pretty marginal" in a number of areas. Nigel
Mon, 05-13-2013 11:08
"THUMBS UP!"
Fri, 05-10-2013 02:15
No, it will not be necessary to hold any of the work waiting for the plow to be turned, end for end. Weather will be the major factor, but there will [...]
Thu, 05-09-2013 19:54
The CGW X-38 plow is really coming to life. Bob Kutella and Vic and crew need to be very proud of your collective efforts. I am very appreciative of [...]
Thu, 05-09-2013 15:20
The snowplow looks great! Are you going to apply the door and upper windows befor it is turned to continue work?
Thu, 05-09-2013 09:09
Max, Is there any progress to report yet, in regards to the installation of the poles and overhead wires? Have a good day, sir.
Wed, 05-08-2013 18:40
Thanks for the update! I still don't understand why Commonwealth #5 was removed from service. Do you know why?
Tue, 05-07-2013 09:28
Mr. Kolanowski.....I was just wondering if the Spaulding webcam will be up and running soon for us stay-at-homes. Thanks!2FP
Mon, 05-06-2013 23:04
Max, Has work begun yet on the construction phase of erecting the poles and putting up the wire? Wish I could be there to watch it happen.
Mon, 05-06-2013 23:02
Keep up the good work, Bob. Wish I could be there to help!!!!!!!