Saturday, January 28. 2017Diesel Shop update 1/28/2017Today was a short day in the shop due to a museum planning meeting taking place in the morning. The plan was to repair the hot water cab heaters in the Illinois Terminal 1605. We're not sure how longs it's been since they've been used since we primarily operate in warm weather. Last year while moving one of the unit coal trains, it would have been nice to have in mid April. Anyway, Mark R and I started on replacing the bad hose couplings between the bottom of the heater cores and the supply and return pipes that run through the floor. The conductors side had one replaced while the engineers side had both replaced. Photo: The conductor side, with band clamps removed, shows signs of leaking on the left hose coupling. After replacing the hoses, we checked the motors and found the conductors side not even wired in place and loose bolts holding the motor in place. Dan C joined for a bit to figure out why we didn't have power to the heater breaker, but as it turns out, this GP7 has that wired to the aux gen, so it'll only get power to the cab heat fan motors if the locomotive is running. Jumpering from the battery knife switch temporarily, the motors and switches worked normally. Next up was to replace a 10 inch section of 1 inch pipe on the cab heat supply pipe that had been removed and plugged. Mark worked on removing the plug and union while I cut and threaded the pipe nipple. The rest went together very easily. While showing Mark where the drains were located, we noticed a 1-1/4 inch union that was disconnected near the rear of the locomotive where the cab heat return line goes back into the engine room. The threads on the union were damaged, so it was removed. We did not have a replacement in stock, so that will be finished in a few days. Sunday a few of us plan on reconnecting a number of items to the CNW 411 HEP radiator hatch. If anyone wants to lend a hand, we'll be at the shop by 10:30am. Jamie Thursday, January 26. 2017Diesel Shop update 1/26/2017Just a quick update from last night on Wednesday evening...the batteries recently installed into 7525 were cabled up and everything tested successfully, so that project is complete. Next up on this loco is to go through a very thorough cleaning of the traction motors to improve their megger readings. Last Sunday, Nick D was able to trim the front corner of the 33C's nose that had been previously torch cut and ground everything smooth so the supports and patch can be welded in place very soon. Gregg W was also in the shop yesterday painting many parts for the Union Pacific M-35 doodlebug. While those were drying in other areas, he was sanding some wood pieces for another car he is also working on. This coming Saturday is a meeting day for half the day in the morning, but we still plan on working on some projects in the afternoon and on Sunday. If you would like to volunteer in the shop and help out on the current projects being 7525, 1605, 411 and 33C, let us know! Sunday, January 22. 2017Diesel Shop update 1/22/2017Our goal for Saturday was to get a new set of batteries that arrived a few weeks ago installed into WC 7525 and then get the equipment on shop track 22 ordered differently. The temperature being in the middle 50's made it very nice to work outside in the sun! Mike B and I started by disconnecting the leads from the old bad batteries in 7525. When we were working on the FM side box, it just looked really small compared to the larger size unit batteries at 25 plates per cell that were ordered. As it turns out, the FM side boxes will only take small unit batteries at 19 plate per cell. Luckily we had just put a new set of the smaller ones into 6847 back in December. Our work for the day was doubled as we now planned on moving the new small unit batteries from 6847 into 7525 and installing the new large unit batteries into 6847. After disconnecting the leads in 7525, we tossed a bunch of other tools onto the deck and started CE 15 to move the locos over the crossing at Central Avenue. By this time Colton V joined us and we moved the 7525 and 6847 nose to nose so we could work on both locos at the same time on each side. As I went to borrow the steam departments little forklift, Colton and Mike removed the side panels of the battery boxes on 6847 and disconnected the batteries in it. We removed the old bad battery out of the ENGR side of 7525 and removed the new small battery out of 6847. While I went to get the new large batteries from the shop, Colton and Mike cleaned out the box which had a lot of rotted wood and some rotted steel laying in it. How things typically go at the museum, easy jobs occasionally become much more involved, while getting the second large battery from the shop, the little forklift got stuck as the asphalt pad right behind the barn door broke apart as it was driven over, likely due to the warmer temps and ground thawing. Nick D drove me over to B&G to get the big forklift to pull the little one out and then used the big one to get the battery out of the barn and onto solid ground so the little forklift could be used again. The large unit batteries weigh about 1,600lb each. Nick D also joined us at this point and we worked on the other side, removing the batteries from the FM side of the 7525 and ENGR side of the 6847. Removing the small battery from 7525 was a pain as it fit REAL tight! We had to break apart some of the wood blocking to get it out. One of the new large batteries was installed into 6847 and all the blocking reinstalled, and the small battery removed from 6847 was installed into the 7525 and blocked into place. We went back to the first side and did the same thing with both remaining batteries. Mike, Colton and Nick reconnected the cables in the 6847 and reinstalled the side panels of the battery boxes while I moved the two old batteries to the pile behind the shop and returned the little forklift to the steam shop and the big forklift back to B&G. Colton and Mike moved the locos back over to Barn 2 and pulled BN3 out from the deepest spot in the shop. Mike, Nick and I shoveled a few inches of gravel from between the rails for an SD truck length so a human can get under motors more easily to work on them in this spot on track 22 all the way at the end. The order of the locos was changed and 7525 shoved all the way in first and then 1605, with BN3 and CE 15 going in the west half of track 22. After the switching, Colton and Mike had to leave, Nick and I stuck around and cleaned up the end of the shop more by tracks 22 and 23. Nick continued later working on cleaning up the inside of 33C and was planning some work on making some smooth edges on the nose to weld in some steel in the future. That's all for the day, until next time... |
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Comments
Wed, 04-01-2026 09:01
Good job on the barn 15
Wed, 03-25-2026 18:21
Exciting to see a new barn going up! What's next, after the RAIL project is complete?
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?