Monday, November 4. 2013
REVISED Steam Update 11-2-2013 a ... Posted by Nigel Bennett
in Steam Department at
21:08
Comments (2) REVISED Steam Update 11-2-2013 a successful season !Thanks to Phil and Cameron we now have some good photographs of the test running on Sunday. Good to see the weather was a LOT better than the evening of the steam test. Based upon input from Brian Davies, it sounds like a pretty successful week in the steam shop with the major objectives on 1630 for the year now achieved. This is both good and bad from my perspective. I might have hoped for a few problems to fix and test next weekend when I will be back!!. It had been the target to do a little running before the winter to ensure that we were able to identify potential issues to be addressed over winter. That was achieved over the weekend. After the steam test on Wednesday, Brian and others spent the next couple of days adding items such as the petticoat, that were the minimum needed for significant running. There was some disappointment on Saturday when the planned running had to be abandoned when a leak was detected in a steam union in the cab. The rest of the day was spent replacing the unions and, to ensure no further issues, the whole pipe involved. This may have been “over kill” as close inspection of the pipe suggested that it was sound and the leak affected only the threads at the end. However, with a steam engine you cannot be too careful and the objective is to locate and fully correct any issues before next season. With the leak fixed, the locomotive was successfully steamed again on Sunday. Much of the most important testing was around the rear driving axle. It was the work on the axle boxes here that caused her to be stopped in 2005 and she has not run since this was done. The results were good. There had been some concerns about the reduced flexibility when running around the “Y” but, while she is noticeably tighter than in the past, this was not a serious problem. A number of runs were made up and down the main line. This allowed accessories and controls that have not been in routine use for nearly ten years to be exercised normally. The results were good and it also enabled a lot of the team, who have put in so much work, to experience a ride on the result of their efforts.
The new rear axle bearings run warmer than the existing ones but not excessively so. It looks as if these are good and should settle in as more grease works into them with additional running. There are probably a few minor items for the over winter work list but it does not seem that anything major was detected. So, I rather suspect that this will be the last run for 2013 as it is coming time when it would be safer to have the locomotive and water system winterized. The testing was done with some work not completed. Various missing lagging and bare metal is apparent in the photograph but it is a great relief to see her operational on the main line and looking good in the Fall sunshine. Only the essentials for test running were completed in the last few days so, for example, the brick arch and smokebox sheet work and spark arrestor mesh are not yet in place. This is no problem for a few test runs but required before the season. Then of course there is the big job for the winter – the application of a whole lot of paint!!. It looks like a busy winter but the clear expectation that she will be fully ready for the 2014 season. So I am looking forward to getting back to Union and seeing what she looks like after a spectacular month of effort – great work guys!. Nigel Thursday, October 31. 2013Steam Department 10-30-13 Extremes of high and lowSitting in a hotel room overlooking a very windswept Wellington harbour this is about the most poignant blog entry I have ever had to make. After a few days of silence the e-mail has been red hot in the last few hours and the messages contain extreme highs and lows. The key news items are that 1630 was steamed today and passed its FRA inspection but on the same day we heard of the passing of Bill Chyna, a wonderful guy and a stalwart of the department for as long as most of us can remember. I have received input from many people but I do not think I can do better than the following note from Collin: “Today we, as a group, experienced a loss and a triumph of emotional extremes. This morning Bill Chyna passed away. Bill had celebrated his seventy fourth birthday Saturday and was said to have enjoyed the event, spending time with family and friends. He was eating cake, so what is not to be happy about?. Bill spent fifteen years with us, and I cannot remember a major decision he was not a part of; a project he did not contribute to. Bill was the first guy I took direction from-the beginning of many orders!-on the first day I came out to the shop. Bill's understanding of electronics and wiring proved to be an invaluable skill as we set up equipment, repaired broken tools and generally moved projects forward. Bill had an understanding of how things work that comes only with decades of experience. I recently visited Bill at Marianjoy Rehabilitation Center where he was undergoing physical therapy. He was in great spirits and probed with questions of what we were doing on 1630, how we were doing it and what our timeline was. I returned the favor by peppering Bill with questions of home repair projects on which he had considerable knowledge. Bill's passing will create a large hole in our team that will be challenging to fill. 1630 was steamed up today and passed by our FRA inspector. While much work remains to be done Brian, Jason & Tom gagged and tested the safety valves, performed the orifice test and ran the locomotive back and forth to the satisfaction of the officials present. The hard work contributed by all of you over the past few years got us to this point, plain and simple. Over this winter we need to keep up the pace to complete the job but we are well positioned to enter the 2014 season full steam ahead. I think we can all say that it is a curiosity of steam that drew us out to the museum in the first place. But over time it is the people who make the whole thing worthwhile and keep us coming back. Please keep Bill's family in your thoughts and prayers.” Well said Collin. Nigel Tuesday, October 29. 2013
Steam Department Update 10-26-2013 Posted by Nigel Bennett
in Steam Department at
00:49
Comments (0) Steam Department Update 10-26-2013A great deal of work was done in the steam shop during the week and over the weekend. Unfortunately, on Saturday, we hit a snag that may hold us up significantly. The information this week is provided by Phil and Brian as I am far away on vacation. Thanks guys. On 1630, Brian Davies is now working full time and, with JD, Jerry, Cameron, Jeff, Jason and others all spending time working with him during the week the locomotive has seen a lot of changes: · The air system was all back together with the exception of the compressor by Friday. After a few fits, the brakes work! · Mike was working to finish that on Saturday ready for testing. Later in the day the house air was hooked up and the air pump was tested. At first the high pressure steam side moved once and then it froze up. The stuffing boxes were loosened and oil was put on the pistons. A second attempt was made. It worked beautifully. So, it was good to see that something be confirmed as done and working on the locomotive. · All of the sheet metal in the cab is on. Some screws still need to be added. With the exception of attaching and plumbing the stoker jet manifold, the cab is basically complete!! Even the electric is hooked back up pending testing. · Cylinder cocks have been cleaned and inspected, and a new pipe nipple installed after one broke. They should be good to go. · Jim and Brian are added the last little bits of insulation around about the last foot of flexible stays on either side of the wrapper sheet. · Sheet metal, minus the bands, was completed across the barrel. · On Saturday much of the banding was fitted. · The final normal hydro was performed yesterday to hammer stay bolts. This proved good so no issues with these. · The blow down muffler was installed. · Preparations have been made for the steam test including: o Setting up a large steam valve on the pipe coming off of the auxiliary dome lid to allow a gauge to be fitted for testing the safety valves; and o Making two gags that will allow individual valves to be held closed to allow the others to be tested. · Unfortunately the key objective on Saturday, which was to apply hydro pressure to the front end to test the sealing of the super heater elements into the header, ran in to significant problems. This relies upon pressurizing the whole front end (cylinders, valve chambers, exhaust passages etc. with water to about 50 psi). This involves minimizing water leakage thru a whole lot of areas, such as the piston glands, that are not wholly tight under steam and are a lot more problematic using water. · A large team spent the morning preparing for the test and the first filling was carried out in the afternoon. This indicated a lot of leakage around the piston and valve glands as well as the junction where the exhaust steam from the air compressor and stoker enter the cylinder casting. · Water was them lowered so fixes could be made to seal the water better. While some progress was made on the glands it was found that the exhaust steam connection, which is in a really awkward place under the boiler, could not be sealed in a way that allowed a pressure of anything like 50 psi to be achieved. This is a complex threaded assembly on which the threads proved to be damaged. · To progress the test it will now be necessary to machine a replacement part. At the same time further work will be done on the packing glands of the piston and valve rods. After this we can again try to pressurize the front end and test the sealing of the super heater elements. On 428: · Tom has finished most of the machining on the wedges. All that is left to do is to drill several hole in them so that they can be adjusted when they are put on the locomotive. Brian and Cameron made a mount that will align for the drilling of these holes. · The mounting brackets for 428's air compressor received a coat of paint. In other areas: · Stu, Bob, and Jane worked on painting the planer. It looks quite remarkable now that it has green paint on it. Bob also worked on assembly of some more small pipes.
So a lot was accomplished during this week. If we can successfully test pressure test the front end, we are just about ready to steam test. Sitting here in Australia!!, I will wait with bated breath for updates on progress with the front end testing. Nigel
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Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...