Sunday, July 7. 2013
Steam Department Update 07-06-2013 Posted by Nigel Bennett
in Steam Department at
19:23
Comments (9) Steam Department Update 07-06-2013
A brief update courtesy of Phil as I was not at the steam shop this weekend.
On 1630 a major milestone is achieved. The firebox corner that was the cause of her withdrawl from service is now completely restored.
· The stays were fully fitted, cut to length and then formed with the air hammer. They can now be seen fully fitted into the patch and ready for service;
· Jason instructed Collin, Phil and others in the use of the gauge testing equipment. The boiler pressure gauges were successfully tested and can now be finally fitted in the cab;
· Phil and Jerry carried out a tricky "fishing exercise" and managed to extract two ferrules that had dropped into the bottom of the boiler barrel during tube fitting. Not absolutely essential but a great deal better that they are not loose in the bottom of the boiler;
· Work is progressing on refitting the remaining flexible stay caps were loose following removal for inspection and cleaning of the stays;
· Brian, Paul and David made good progress on stripping the air tanks.
Meanwhile Bob is starting to install the ducting to provide a permanent power supply to the planer.
.............. and lastly a reminder. IF YOU DO NOT ALREADY HAVE YOUR TICKETS FOR THE STEAM DEPARTMENT BENEFIT next Sunday (14th) at the San Filippo Estate- THERE ARE STILL A FEW AVAILABLE. They can be booked from the link the IRM website. Hope to see you there.
Nigel
Friday, July 5. 2013
Steam Department Update 07-03-2013 Posted by Nigel Bennett
in Steam Department at
09:37
Comments (0) Steam Department Update 07-03-2013An interim update this week as I was at the shop on Wednesday with my son who is visiting from the UK. With additional work sessions Sunday and Wednesday a lot was achieved. On 1630 the primary focus is on the remaining tasks to get the boiler water tight for initial testing. · Phil has now finished caulking the rivets inside the firebox so the rivets are now complete subject to hydro testing; · The major remaining task is fitting the two new flexible stays into the patch. These are steel rods with domed heads that must be threaded into the inner firebox and tightened so that the domed head makes a seal with the socket in the outer firebox. Here
you can see the holes in the inner firebox into which the stays will be
screwed. The end of the thread cutter is
projecting from the right hand hole.
Viewed
from the outside we can see the two sockets.
The one on the right is empty and, thru the socket, you can see the hole
in the inner firebox into which the thread will be cut. The guide and cutter are in place in the left
hand socket ready to start cutting.
Here
Tom is setting up one of the stays to cut the thread on the stay itself.
Here
the thread is being cut. This also gives
a good view of the overall shape of the stay with the thread being cut at one
end and the ball, nearest to the camera, which will seat into the socket. The slot in the ball is essential to allow
the stay to be screwed into the threads in the inner firebox.
Here
Michael is manually cutting the thread into the inner firebox sheet. Good progress was made and by evening the stays were being screwed into place. This is not a "one-time" operation as the threads must be carefully adjusted so that they are tight but not excessively so in the threads of the inner firebox when firmly in contact with the socket. Once this is achieved the inner end is to be peaned over and caulked to complete the sealing Another major task completed Wednesday was the hammer and hydro-testing of the three air tanks. All were successfully tested to 180 psi and have now been partially stripped of paint. Paint stripping will continue so that they can be repainted before fitting. A lot of preparatory work was required for the hydro-testing, which has commissioned and tested the equipment needed for the boiler testing in the next few weeks. The water for testing both tanks and boiler must be warm. The heating is achieved by circulating thru a pool heater. Preparing the pump and heater system for use after winterization requires several hours work. This was successfully achieved and the system is now tested and ready for use in the boiler testing. I will not be at Union this Saturday so will look forward to an update myself on Sunday ! NigelMonday, July 1. 2013
Steam Department Update 06-29-2013 Posted by Nigel Bennett
in Steam Department at
09:00
Comments (2) Steam Department Update 06-29-2013
A bit of a delay in posting the blog this week as we are
busy with my son Michael over from the UK this week. However he is keen to work in the shop while he
is here. It has been another week of
intense activity focused on 1630 and getting to the point where we can carry
out the first test of the tubes with water in the boiler.
We keep pushing
forward on 1630.
·
The replacement
valves had arrived and Richard, Michael and others fitted them to the milk car.
By lunchtime it had been filled with
water and it was then moved back to the shop by the operating crew at end of
day. So we have the water supply in
place;
·
Phil had worked
during the week on caulking the rivets.
This is a tough job with the air hammer carefully sealing the edges of the
rivets into the sheet of the boiler. He
had worked on this during the week and finished the outside on Saturday.
By
evening he was working on the rivet ends inside the firebox. Access to the area around the patch remains
the limiting factor in getting the boiler water tight. Two stays have to be fitted to complete the
repair. The holes are drilled and the
stays ready. We must now cut the threads
into the inner firebox sheet, screw then
into place and then caulk the projecting end.
However, this is not possible at the same time as the rivet caulking;
·
Eric worked all day
on the smokebox ends of the super heater flues.
Having trimmed these to exact length, the ends need to be slightly
flared to improve the seal ahead of the water test and in preparation for
beading. By end of day, after a lot of hard
work, these were all done;
·
During the week, Tom
had measured the throttle seat in the boiler and ordered the steel to make a
blanking plate to seal this during hydro testing. The blanking plate should make a better seal
than the throttle valve itself during hydro testing and should make inspection
a great deal easier. After the hydro
test the braces must be inspected. It
will be easier to get thru the dome and onto the top of the tubes without the
large body of the throttle to crawl around.
Hopefully the plate will be available for the Wednesday working session;
·
The gauge plates in
the cab were given a final coat of black paint so that gauges can be
permanently fitted as soon as they have been tested, which we hope to do next
Saturday;
·
One very awkward job
was lapping the seat of the main turret shut off valve. This critical valve is located at the very
top of the turret at the highest point of the firebox in the cab. It can only be accessed thru a hatch in the
cab roof and by threading wrenches in between other fittings on top of the
firebox in the cab. This shows the
location with the valve body removed.
Its
purpose is to enable the turret, from which all auxiliary devices are supplied
with steam, to be isolated from the boiler in an emergency. While it is seldom closed when the locomotive
is complete, it will be important as the intent is that the first tests will be
done without letting water into the turret.
It is also important that the valve should shut correctly when required.
Michael
and Brian had great fun with this. However,
with a good deal of hard work the objective was achieved. The valve body was removed from its seat in the
turret and rigidly attached to a shaft that would guide it accurately onto the
seat and allow it to be turned repeatedly against the seat. The guys worked for several hours working the
valve head against the seat with increasingly fine grades of abrasive lapping
compound until an even seal was achieved all around. Here Michael displays the end result !.
Then
everything was reassembled. At the end
of the day everything looks as it did before.
Only those involved know that a lot of work was put in and we now have
confidence that this key valve is in good shape.
Aside from work to
seal the boiler for first testing, one very visible achievement was the removal
of the fireman's side air tanks. These
are now with the engineer's side tank on the floor of the shop and have been
marked up for hammer testing. If no
issues are apparent from hammer testing, they will be hydro tested then cleaned
and painted ready for service.
On other areas:
· Bob made good progress on setting up the power supply for the planer;
· The mounting brackets for the air pump were test fitted to 428. This was a revealing exercise. When she was stripped many years ago the additional brackets were found mounted between the casting that secures the pump to the boiler and the pump itself. With some measurement it is now clear that this was an essential modification at some stage in the life of 428. Absent these extensions, which set the pump out and lower than if it were directly mounted to the bracket, the top of the pump would foul the feed from the injector to the boiler.
So continuing progress. The plan is now for quite a few people to work on Wednesday.
Nigel
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Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...