Monday, April 19. 2010Track Department report April 19Sunday's gang consisted of myself and Tom Hunter. Jeron Glander joined later in the day. Riding off the success at Four Mile Siding last weekend Tom and I prepped tools and material on the crane, flat and caboose combo and headed East to finish building the siding. We didn't waste any time when we got there pulling the storage cars from the siding and using the crane to connect the last two track panels. I realized we had forgotten lock washers to finish bolting them together but all of the joints have a bolt on each side until we can pop a few more in. After finishing off the second panel an investigation into a low oil pressure issue was found to be a hot engine... A little Too hot. It looks like the water pump has failed or the radiator is severely clogged. But with no coolant flow on the top of the radiator it brought our crane use to a severe halt. With the crane shut down Tom and I moved on to spiking up all the remaining ties in the section we had installed the rail in last week. Using track jacks, air compressor and spiking gun we had one entire side spiked up in no time. Prepacked lunch followed in the 529 and then onto spiking the other side.... After restarting the air compressor, without fail, it sputtered off and wouldn't restart. Upon investigation of this issue we figure a bad fuel pump. Fuel in, no fuel out... How about some hand spiking to ease the frustration? Of course! We spiked up the entire other side by hand just in time for Jeron to arrive with the Ballast Regulator. We set the panels in a rough line and Jeron, who reinstalled the rebuilt hydraulic cylinder earlier in the day, plowed stone from the siding into the new track. Getting late in the day we called up for a 'tow' back to the property not risking an engine failure without coolant..and were grateful to see Joel Ahrendt, Warren Lloyd and Kyle Merkel arrive with the ComEd 4 electric steeplecab to help us back. While waiting, Jeron managed to drag nearly enough stone for a first lift on the new track to the very end of track. The end will need somewhere around 12-18" raise but it's very close to complete as is. The 'in service' trackage was officially extended roughly 80' and the last of it will be extended another 80' once we make a good raise and tamp. Sunday, April 11. 2010Track Department report April 11The day started with Brian Harp and Tom Hunter refilling the hydraulic tank in the Amtrak Regulator. It drank roughly 40 gallons of fluid severely depleting our 55gal drum of oil. We'll have to get more soon.. After I arrived and met up with Steve L. we prepped for a day at Four Mile Siding. Tom ran the crane with work train with Brian as the conductor and headed east to switch out the siding, while Steve and I switched Barn 2 to retrieve the Hydraulic power pack and motorcar. We followed east and began by moving trees with the crane. BIG trees. The biggest tree we had to slide down the track on two ties and teeter it off with the crane into a wide clearing. The tree maxed out the crane's capacity at near 10,000 lbs but Tom managed to set it off very nicely. A few more large limbs were moved out of the way as well before we had the room to begin building track. We cut, drilled and installed a stick of 112lb rail and gaged the track to set everything up for the first panel to be hooked up. We gage spiked a few ties under the new rail for the crane to roll onto to hook up the first panel Jeron Glander arrived via the North Shore 714 with a gift of bottled water and helped us out for the rest of the day. We lifted the first track panel out of the way first to clear the ground of limbs and sticks to get a relatively smooth foundation for the new track. Tom then set the new panel in place and we bolted it all up with relatively little difficulty. We cleaned up and headed back to the property around 4 o'clock. All that is left is the hookup of the next two panels and finish spiking 12 or so ties. One more day and we'll be ready for the regulator and brush cutter to begin their work. Thanks to Brian Harp for joining us this weekend. I hope he can join us again in all of the festivities before next year's annual meeting. On a bad note- the J585 refuses to start now. The starter problem has gotten much worse and it no longer spins the engine over to crank.. Flywheel replacement time? Looks like a return of the 580 is imminent. Sunday, March 28. 2010
Track Dept Weekend Report Mar 27, 28 Posted by Adam Robillard
in Track Department at
23:02
Comments (0) Track Dept Weekend Report Mar 27, 28Saturday Report --- The day's primary project was the joint effort with the Signal Dept to get the very large Corwith Tower lever machine into our Spaulding Tower. This proved to be no easy task. The entire lever machine is roughly 20 ft in length and weighs nearly 9000lbs... The signal dept can report further on its future but our part was the heavy lifting with the Model 50 Burro crane to get it into the lower level- through the doorway. Tom Hunter ran the crane and after a few test lifts near Barn 9, we lifted the machine near the station and ran it into the Tower very slowly and carefully. We were successful in getting it in the building around 2PM and hit lunch. Lets hope that machine never has to leave the tower again! After lunch, the crew of Tom Hunter, Tyler Hunter, Frank Devries, Jeron Glander and myself, Adam Robillard split into a few groups. Jeron and Tyler ran to Napa and picked up new fuel filters for the Burro crane and along with Tom Hunter replaced the filters in the crane and fueled up the machines in yard 11. Jeron did some wonderful electrical work on the Amtrak regulator and also broomed a yard track in Yard 10 to test the functions. All which appear to be working well. Nice job Jeron! Meanwhile Frank and myself were at Track 24 pulling the bad vibrator motor out of the Switch Tamper and prepping the install of the new one Tom had stored in his garage. We managed to get the new motor in and wired up but it hasn't been tested yet. That's for another day. The next project was to relocate
the brush trimmer that has been stored in one of the electric
carbarns. It cannot be left in the open near the public beginning next
weekend so we needed to switch it back into Track 24. Tom and the gang
took the EJ&E 585 motorcar to retrieve it only to have the entire
machine derail on the Yard 6 lead.... Call in the Model 50! While
Frank, Tom & Tyler took time to rerail the cutter, Jeron and I
headed onto the carline to weld traction bonds. The portion of track
we surfaced over the last few weeks revealed three joints with broken
or non existing bonds. Some quick work with our stick welder resolved
that problem and the two of us went back to Tk24 to clear all the
machines out of the Barn. When the cutter was rerailed, now well after
dark, we shimmied it into the back of Tk24 and switched everything back
in the Barn. We called it a night around 9PM. Wow, what a day. |
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Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]