Sunday, August 5. 2012
Steam Department Update 08-04-2012 Posted by Nigel Bennett
in Steam Department at
12:13
Comments (0) Steam Department Update 08-04-2012It was one of those days when casual observation could suggest that the steam department had done nothing !. However we made steady progress on some critical work although the visible effect does not look much. On 1630: · we have now agreed terms with the boiler welding specialist for the back tube sheet and super heater flue work. Hopefully that will be done shortly. It should only take 4 days once he is on site. · the pipe to replace the corroded runs along sides of the boiler has been located and ordered. This in itself gave some quite surprising results. The small diameter heavy gauge steel pipe used on a steam locomotive now has few uses and is made in small quantities. Price is therefore driven by batch sizes and availability rather than the weight so we have larger tube costing less than larger and seamless costing less than seamed in some cases. · Collin finished the inside of the front tube sheet, so internally we now only have the contract welding of the rear tube sheet to do. · Mike and Bob continued forming the test sheet for the firebox patch. The activity this week was focused on forming the shape to match the sloping front tube sheet while retaining an accurate match to the curve of the mud ring. · the major activity was the continuing battle with the smoke box bolts. These apparently insignificant 3/4 inch bolts occupied a number of us all day. Looking at the locomotive in service they are simply the bolts onto which the nuts, that you see in a circle around the edge of the smoke box front sheet, are threaded. Although they appear at first sight to be studs, they are actually "T" headed bolts, unthreaded in the length that passes thru the front ring, that are driven into the ring from the rear. The snag is that they cannot be a really tight fit on the front sheet so there is a hidden cavity behind the nut in which moisture and gases attack the bolt. In service the smoke box is under vacuum and any leakage causes loss of efficiency and rapid corrosion as air is sucked past heated metal. We want to ensure that, once we do this overhaul, we have reasonable confidence that 1630 will be good for the next 15 years so we are working on the basis that these bolts should be replaced where they are wasted to less than 5/8th inch. This means removing 11 bolts. It is clear that the bolts at the top and bottom, which are subject to greatest wear, have been replaced at some stage as most of the 11 are at the sides. The documented way of removing these bolts is to hammer them from the front, potentially having heated the ring to assist the process. The bolts on 1630 do not seem to have heard of this process !!. None have proved possible to hammer out anything like whole. They are so firmly in place that hammering expands the bolt in the hole and makes it impossible to remove. The technique evolved during the day is to grind off the head of the bolt (which we think may in some cases have been welded during repairs at some time), very carefully drill a hole centered on the bolt and enlarge it to allow an air hammer bit to be inserted. This allows the air hammer to be used with less expansion of the bolt. If this does not work you have to collapse the sides of the bolt into the hole, re drill and try again. We now have 5 out. They are very variable. The last and worst did not come out until we had done this multiple times and reduced the length for 2 1/4 inch to 3/4. The huge frustration is that, when they eventually come out, it is just a plain smooth plug with nothing to indicate why it would have been so difficult to move. Here you can see the bolts. The green paint marks indicate good. The red marks and gaps those that are to be or have been removed. Here we are working on the last one on the engineers side, which proved to be the worst so far. Late on we called in reinforcements and received full support from the IRM Board. Thank you Jim !!. Any way , 6 more on the fireman's side for next weekend, then we can think about putting in the new ones.
Elsewhere Phil removed the lugs from the back of one of the axle boxes for 428 so that it can be mounted on the Bullard turret lathe to machine the bearing face. The plan will be to fit brass bearing faces, similar to those fitted to 1630, rather than poured babbit faces previously used. I will not be at Union next Saturday as my son is getting married. I do hope to be there Sunday so hopefully I will be able to report on a lot that the team has been able to get done without me getting in the way!. Nigel Sunday, July 29. 2012
Steam Department Update 07-28-2012 Posted by Nigel Bennett
in Steam Department at
16:26
Comments (10) Steam Department Update 07-28-2012Another good week in which we were able to move a lot forward on 1630. Various tasks support the overall work plan. First we must finalize preparation for the inspection of the boiler shell. Not much remains to be done to enable this so the next focus is on the tasks that will enable us to make the boiler water tight again. For this, we are preparing all the flues and materials that we need to refit the tubes and also to complete the patching of the firebox. Finally, whenever possible, we work on ensuring that parts that can be fitted once the boiler is watertight and passes its first hydro test are cleaned and ready to be fitted quickly when required. · During the week Jeff and Jerry managed to complete the cleaning and hydro testing of the super heater elements. The conclusions were good. 24 passed the pressure test at 1000 psi with no issues and are back in the box car ready for refitting when the boiler is ready. 1 passed the pressure test but has some minor damage to the protective shield (a simple sheet metal construction that is wrapped around the element to protect the most exposed areas from erosion by cinders flying thru the flue) and only 2 failed. The last 2 will require the attention of the boiler welding specialist when he comes in to safe end the flues. · Phil and Collin cleaned up the front tube sheet in preparation for re-tubing. · Eric did a great job clearing the medium from around the firebox. This is important so that everything is clear and visible for the upcoming inspection. The blasting medium is deceptive stuff!. We knew that there was some still on top of the firebox. The initial comment in the morning was "don't think there's much there". Having used an air line to blow it off the firebox crown and the stays at the sides of the firebox so that it settled into the bottom of the firebox water legs, Eric sucked it out with long pipes on the vacuum cleaner. By end of day we have a clear view along the bottom of all the water legs .......... and probably 80 lbs of medium extracted !. · After a lot of adjustment to get the settings right the McCabe was used to bend a test sheet for the firebox patch. Past experience with the Shay has demonstrated the importance of proving exactly how the patch will be formed using an old piece of steel before we do it "for real" with an expensive piece of new boiler plate. Considerable progress was made. The McCabe was used to bend the sheet
........... and the radius formed proved to be an excellent match to the critical curve in the mud ring. Having been cut to the template, the piece is a pretty good fit to the firebox and can be used to make minor adjustments to the template for the final patch. The next step is to form the piece to fit the slope of the front tube sheet. · Ed and Jim identified and measured the pipe work to be replaced along the boiler and this can now be ordered. · Phil, Jeff and I started another job that looks like it will be a lot more "fun" than we had hoped!. A number of the bolts that project from the front ring of the smoke box to secure the smoke box door sheet are wasted and need to be replaced. In theory they can be driven out by hammering them back (towards the boiler). In practice the effect of 60+ years of heat and rust on bolts that were a tight push fit to begin with is "interesting". After 90 minutes of effort with a heating torch and air hammer we have one out. Only another 15 or so to go !!. · Bob Hunter has now finished the computations and supporting documentation for the form #4 submission. This is the engineering assessment of the boiler which confirms that, having regard both to original design and subsequent wear as now measured, it is suitable for the intended operating pressure. This is now ready for submission. Nigel Sunday, July 22. 2012
Steam Department Update 07-21-2012 Posted by Nigel Bennett
in Steam Department at
17:36
Comments (0) Steam Department Update 07-21-2012I guess we must be becoming more adapted to the heat. There is not much choice this summer !!. A lot was achieved in the steam shop this Saturday and we are now moving toward the key step of the FRA inspection of the interior of the boiler. We have a few more minor tasks to complete inside but are now close enough to schedule the appointment. This is critical to our ongoing schedule. If the inspector is satisfied with the boiler interior we will be able to progress to painting the interior and refitting tubes. If any additional work is required that impacts the timetable. A number of tasks were progressed on 1630 · Chris and George from Curtis Boiler Service came in to scope and quote for the specialized welding of the safe ends on the super heater flues. George has done this work on several of our other locomotives over many years. He will also do the work on the rear tube sheet. · Work progressed well on the super heater elements. After the initial shock last weekend, when the first one failed, we now have 9 that have proved sound at the full 1000 psi pressure, have been cleaned and prepped and are now back in the boxcar where they will stored ready for refitting. Another 9 are outside the shop to be cleaned and tested during the week and next weekend. That leaves 8 more to complete the total of 27. (How does 1630 have an odd number of elements?. Because decades ago one position on the header was damaged and plugged so at IRM she has always had one less super heater than she was built with.) The process of cleaning and testing the elements is quite complex so I have made some notes below. · Mike has recovered and was back at the shop. He is in process of grinding the mud ring to ensure a smooth fit for the patch. · Glenn finished the McCabe and we took the first steps toward getting comfortable with using it and setting up to produce a test sheet that we can use to prove we have the correct radius to accurately fit the mud ring before we bend the rather expensive boiler plate. It looks as if Ralph has some doubts about what that lever does ! Phil working to set the test sheet in the jaws of the flanger. This provides a good view of the way in which the McCabe operates. The sheet slides between the flat surface on which Phil is setting it and the clamping head above it. It projects back toward the machine and extends over the curved die (the dark grey curved surface that can be seen below the light grey clamping head) into the space below the press head. The press head is at about 25 degrees to the horizontal in this view but would be drawn up to the horizontal to allow the sheet to be pushed into place. With the sheet clamped, the press head is driven down by stages bending the sheet to the radius of the curved die. The machine is hugely powerful, well able to bend 3/4 inch steel plate, and has few "fail safes". Only care by the operator ensures that it does not apply the force incorrectly and severely damage the machine itself.
· Ed thoroughly brushed off the various small pipes that run along the boiler feeding the lubricators and accessories such as the bell. The object was to determine if they should be replaced and the conclusion was that we should do this. Based upon examples such as this it seems safer to replace the pipes now. None were actually leaking but the objective is wherever possible to aim for a long spell of incident free operation and these have the potential to be a real nuisance. Once the locomotive is complete, these will be buried under insulation and lagging sheets. If one failed then it would probably damage the insulation and a lot of sheet metal would need to be removed to get to it. In other areas: · Tom has machined the spring retainers for the Shay so we can get those welded into place on the bolster fitted next time Dennis is in the shop. · Stu and Bob continued the assembly of the planer. Jeff had arranged for the department's BrownHoist crane to run in the Diesel Days parade and here it is running thru the depot road.
and comes to rest in the depot to be described. It must be a long time since she has been out of the shop and barn area. Cleaning and testing super heater elements Each element has been located in a flue thru which pass heat and debris from the fire. So they are thoroughly covered in soot and rust that must be removed before it can be inspected and tested. What Phil is doing here can be referred to as cleaning but most of us who have done it see it rather more as transferring the dusty muck from the tube to the operator !! The test rig must then be fitted to the element. The element has balled ends that, in service, are a dry fit into balled sockets in the super heater header. These must be carefully cleaned with emery cloth to remove pitting. A thin rubberized fabric washer is fitted between the test rig and the ends of the element. If this survives the 1000 psi test pressure the balls are in reasonable shape to make a seal with the header when they are refitted. Once in place the element ready for testing looks something like this. (Actually in this view the element is ready for the final step, after successful testing, when air is blown back thru the tubing to ensure that it is thoroughly dry and ready for storage in the boxcar. For testing the water supply is connected to the right hand side to the test rig). The rig is then connected to our high tech water pump. Joking aside, this may be old but is a very effective and critical piece of equipment that can pressurize the elements to 1000 psi and the whole boiler to more than 200 psi when carrying out a hydro test.
The loan of this tank from B&G overcame a significant problem last weekend. The pump operated very unevenly and Tom recognized that the problem was that the pump exerted sufficient suction to close the valve on the well if it is directly connected, even thru 100 ft of hose. Provided with an unrestricted supply the pump builds pressure evenly.
The pressure is raised to 1000 psi and the pump valve closed. If the pressure holds we have success. The most common problem is that a leak develops around the ball joints necessitating more work with the emery cloth and/or refitting of the test rig. Once an element has passed the pressure test, high pressure air is blown back thru it to make sure it is free of water. The rings that hold it to the header are carefully cleaned and sprayed with WD-40 to protect them and the element is then ready to go back to storage with confidence that it ready to fit into the header, hopefully during this winter. Nigel |
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Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...