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Tuesday, March 15. 2011
GB&W 2407 progress Posted by James Kolanowski
in Atchison, Topeka & Santa Fe 841 at
01:29
Comments (11) GB&W 2407 progressThe progress on 2407 continues as a lot of people volunteer their time. We are likely just a few weeks away from being able to start its 2,400HP engine for the first time in over 15 years. About a week ago, Jeron Glander and I finished cleaning out the bottom of the oil filter box of sludge and debris, and installed new oil filters. This past Saturday, Scott Nauer and I cleared track 22 so the Cleveland PCC could be moved out to make room for the next painting project. Once the PCC was moved, we moved the 2407 out of the way so the NSL 714, the next to get a paint job, could go all the way east. We spotted the 2407 after the 714, that way we can move the Alligator in and out as needed without interfering with the work on 714. On Sunday we had Roger Broms, Jim West, Warren Lloyd and myself. The main tasks were to free up the last of the injection pumps that were stuck and drain more contaminated fuel and refill the tank partially. We started on the fuel injection pumps, Warren checked all the ones on the engineers side and made sure they were all still free as they were the last time. There were 4 on the firemans side that were still stuck, or were very sticky to move. The method was to simply work the rack in and out on each, using a block of wood to tap it in, and a bar to slide it back out. Eventually they would move by hand and then after more lubricating and exercise they would return to no fuel with its own return spring as it should. After a few hours of this, we broke for lunch. After lunch we drained another 50 gallons of fuel out of the tank and pumped it into a 55 gallon drum. We spend a little time finding a way to break into the tank to see how much fuel was actually in it. After finding a cover over a 1.5" hole, we found there was about 4 or 5 inches of fuel left in it which we later found out to be about 250 gallons. We began to transfer about 300 gallons of fuel from the 5383 into the 2407. The 5383 and a few other locos had been filled the day before as we decided to stock pile a truck load of fuel for the year while prices were somewhat reasonable. Jim West removed the fuel gauges to see if they were complete and working, both of them had been painted over some time ago. One side had the float rod broken, and the other was complete and working, but it had been sandblasted and painted over, so the glass will need to be changed. Its temporarily back in place without its glass. We spent some time on the fuel pump and relief valve. The way its plumbed is causing some issues with priming the system, we are gonna make a few changes to where the bypass dumps to so this problem can be resolved. We are also looking into changing the fuel filter element to one that is common with other locos that we run. The last few items that we need to work on next time are to add some oil to the engine, during prelubing it is running a little low. We'll need to change the fuel filter type and replumb the fuel relief bypass valve directly to the tank via the existing return lines. We can then move it outside to try to start and idle in order to do some running checks. There is still a long way to go to make it operational, but just getting it started will be one huge accomplishment for everyone. Be sure to visit the Photo Gallery of the current work going on. Also, donations to the RSD15 are still needed and appreciated. Monday, March 14. 2011Sunday's Track ReportRiding on the success of yesterday's progress today our two goals for the day were to clean a few machines with the pressure washer, and unload the ties loaded onto the flatcar yesterday along the mainline. The short version of the story is that both jobs were completed but not without a little excitement in between. The crew today was myself, Tom Hunter, Jeron Glander, and a new volunteer, Patrick Shea. We started right away with the rented 3000psi heated pressure washer and cleaned up the tie crane, regulator and Model 50 Burro crane. After cleaning the radiators on the burro it ran significantly better now that it has proper air flow drastically minimizing the possibility of overheating the engine. We picked up our loaded flat car of ties and the EJ&E 529 caboose and headed out onto the carline. The rest of the day was spent unloading around 400 ties along the mainline. Tom expertly ran the crane while Jeron, Patrick and myself hooked and unhooked the bundles along the line, mostly between Seeman Rd and Four Mile Siding. We'll come back out with the tie crane sometime soon and distribute the ties where they'll be installed. It was an incredibly productive day and called it quits after tying up shortly before sunset in Yard 11. This week the rest of the ties (~250) should get loaded onto the flatcar which should allow us to repeat the job again next weekend. Thanks again to Patrick for joining us for a second day in a row. Hope we didn't scare him away. Adam RobillardIRM Track Dept Sunday, March 13. 2011
The late GB&W 2407 update Posted by James Kolanowski
in Atchison, Topeka & Santa Fe 841 at
23:12
Comments (0) The late GB&W 2407 updateHere is a very late update on the progress on GB&W 2407 from February 12th, I had drafted it before I went on vacation for a couple of weeks and forgot to publish it. We had a pretty large group out Saturday afternoon, including Frank DeVries, Marcus Ruef, Warren Lloyd, Kyle Merkel, Kevin Hennessy, Greg Ceurvorst, Dave Fullarton, Jeron Glander, Jim West, Dan Currens, Rich Schauer, and myself. The main tasks were to get the rest of the water system tight. The previous weekend and during the week we had made a number of repairs, but did not have a chance to water it again. The electrical system, governor, and air compressor were also worked on. Dan Currens started by digging into the electrical system, verifying everything was connected and functioning properly in the cabinet, and with the governor and such. Kyle and Jim worked on refilling the governor and pump with oil. We will have to flush the system again at a later date. There was some minor raccoon damage, but the majority of the electrical system was in pretty good shape. Meanwhile Dave and Kevin were working on checking all the injection pumps, seeing which ones were free and which were sticking. They found a bunch that were very tight and began working on lubricating and freeing them up. Warren, Kyle and Rich joined in as well. Frank and Marcus made a gasket to replace the leaking one on a cover on the air compressor, and then changed the oil in the compressor. We started watering again to verify the latest repairs and was very surprised at how well it was holding water. We did mark a few more water elbows that we had not marked the last time, along with some additional pipe couplings. Frank noticed a crack on a low pressure cylinder liner that was leaking water. There were a number of other leaks in this area the last time, so we didn't notice it. We are looking into some ways to fix this without changing the liner as it looks like the only damage is this area on the outside of the water jacket. Greg joined Marcus and Frank, and they made some more gaskets to replace the leaking ones along with some hoses on a few of the water elbows on the engineers side after draining the water. They made enough for all the ones that were leaking on both sides. Warren replaced two of them on one side of the loco while Marcus and Frank replaced a few on the engineers side. While draining, we noticed that the compressor and water cooled intercooler on the compressor did not have a drain as the pipe that should have gone to the main drain valve was removed and plugged. This was done sometime when it was on the railroad, and is probably why there were water problems on the compressor. We'll have to thoroughly check out the intercooler as well. It was a very productive day and I'd like to thank everyone that helped out to move this project much further along. Be sure to visit the Photo Gallery of the current work going on. Also, donations to the RSD15 are still needed and appreciated. Sunday, March 13. 2011Saturday Track Report
Saturday's plan involved a two pronged attack. One group was to finish walking the mainline, the second team was to load the mainline ties onto a flatcar, so they can be peddled out for install in the coming weeks.
Again, I picked up Marcus at Aurora Transportation Center, and we drove up to Marengo Cafe for breakfast. After Breakfast we met a new volunteer to our group, Patrick Shea. Adam joined us at the caboose on 110 track and the plans were set in motion. Marcus and I walked track. We started with the stretch from East switch to Karstens, so the diesel department could use the east switch as head room for fueling diesels. We then continued out to signal 201 with no significant defects found. The walk continued from East switch to West before we broke for lunch. After lunch we finished off the West end finding one broken bar. The total repairs for this spring, two pull aparts east of 4 mile siding, which is still out of service, One broken bar on the main between 201 and 251. One broken bar at West switch. We intend to have the two broken bars fixed before the start of the season. The pull aparts depend on getting some warm sunny weather to get the rails to expand enough to get new bolts in the rail. Adam and Patrick grabbed the fork lift and started loading bundles of ties onto the TTX flat car that the Camp Grant arrived on. All the other IRM flats are in use, so we pressed this one into service since it was just taking up space in the siding. The diesel department was kind enough to retrieve it and bring it to along barn 9 for us. In short order Adam and Patrick had the flat loaded up and ready for Sunday's distribution party. A break for a brief meeting, and we were back at it putting the train together. Tom joined us for this phase of the job. Tom finished off getting the four part hook put back on the crane. The hook was taken off last year to rig up the clam shell for loading stone. Tom, Marcus, and I, then got the 529 caboose moved over and the loaded flat car onto track 112, while Adam and Patrick loaded a couple more bundles of ties onto tie flats with the tie crane. The tie crane was tied down in yard 10 for the night. Tomorrow's projects, go out and peddle ties where we marked ties for replacement. A few photos have been posted here: http://www.irm.org/gallery/album271 Frank D. Sunday, March 13. 2011Wood Shop Update - March 12, 2011Greg Ceurvorst, John Faulhaber, and Fred Zimmerman are discussing the days work - what else - more windows! Greg was doing some finish sanding on the new Villa Falls windows. Earlier, he, Fred and Victor Humphreys moved some structural steel from the Barn 4 floor to inside the B&O boxcar. Fred and Victor were repairing another step well for the ATSF caboose. Fred is all suited up and the sparks are flying! Randy Hicks has just completed some tricky notches for a new poplar window sill for the IT cars undergoing repairs in Barn 4. Earlier, Randy completed post repairs on the IT 277. There was a lot of woodwork and tricky parts to replace rotted members, under that wide window post steel plate. Or rather - sign box of the times. Mike Stauber and Frank Sirinek have removed the front signbox from the Kansas City PCC and they had it in the shop. Disassembly, cleanup and repairs ensued. Done with that stage, it is ready for primer and repainting. Sunday, March 13. 2011
Trolley Bus Department Update - ... Posted by Ray Piesciuk
in Trolley Bus Department at
11:07
Comments (5) Trolley Bus Department Update - 03/13/2011A few years ago, the drag link on Chicago Marmon 9553 failed. At the time we decided to swap the remaining good on from Chicago Marmon 9631 to keep 9553 in service until we could fabricate repairs. During this past week, Richard Schauer and I decided that it was time to get this done. We weren’t sure how long this project would take, but it might be a significant amount of time. So, to prevent the 9553 from blocking service coaches during this period, we began the day by doing a switch move, swapping the Dayton Flyer 925 with the 9553. To accomplish this we had to move the two coaches in front of them, Seattle Twin 633 and Edmonton BBC 181.
We then got to work removing the good drag link from the 9553. After easily removing the front part (under the driver’s seat), the back section (behind the front wheels) gave us real difficulty. With limited space and leverage under the coach, we decided that turning the front wheels a little would give us a better angle at loosening the connection. Since the coach was stationary, turning the wheels puts a big strain on the drag link. Unfortunately it proved a little too much and the good drag link began to fail. To prevent a total failure we immediately stopped and returned to removing the rear section. With the help of Warren Lloyd, we finally accomplished the task.
We brought it over to the Car Shop to remove all the parts and clean it up. Luckily Car Dept. Superintendent Rod Turner was there and took a look at it. He came up with a couple ideas on how it and the second one could be repaired. No time like the present, so we set out to make the repairs on the “good” one. Rod and Diesel Dept. Superintendent Jamie Kolanowski gave us a good deal of their time and expertise, and by the evening the job was done! We’ll need to do some additional work to get the second one fixed, but a job that might have taken a very long time and possible be very costly, is well on its way toward completion.
Another great example of departments working together. Rod and Jamie, we owe you guys big time for this one – THANKS!!!!!
On another front, preliminary work on the west loop project continues. B&G Superintendent Dave Diamond has a quote for paving and DC Line Superintendent Max Tyms has a quote for trolley wire and is working on one for poles. We spent some time discussing the project with Dave and we decided that we will start staking out the road once the weather and ground condition permits. Don’t forget about the Snowflake Special coming up on March 27th. Tickets sales are brisk so don’t be left out! Click on the link from the IRM home page and buy your tickets online now!!! Sunday, March 13. 2011CTS 4223 - March 12, 2011Our Cleveland Transit PCC car came outdoors yesterday in a move from Barn 2 to Barn 8. THANKS to Randy Hicks who shared these images of his. As you can see remarkable progress has been made during recent months to get this car painted in Cleveland colors - for the first time in decades! As you can see the interior still needs a little work. Thanks again Randy for the eye candy! I wonder where he gets all that energy? |
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Comments
Mon, 06-17-2013 09:50
Wish I could be there to help.
Fri, 06-14-2013 16:50
Matthew, Any special event is the decision of the museum Board. My personal opinion is that it is likely that there would be a special event to [...]
Thu, 06-13-2013 18:33
Hi, I have a question, if or when she is restored and back up and running this or next year. Will their be a special event set up for the return of [...]
Tue, 06-11-2013 22:36
The whistle 1630 wore for a while that you're thinking of was a Frisco 6 chime donated by a former member of the steam shop. It was on it a few times [...]
Tue, 06-11-2013 18:03
You are talking here about something well before my time !. I have not seen her with anything other than the whistle she now carries. If she [...]
Mon, 06-10-2013 16:17
i'm curious here. Will 1630 ever wear the ATSF 6 chime she had on for a while? Better defines her, I love the deep whistle she has now but the higher [...]
Sat, 06-08-2013 15:15
Many many many many many thanks for getting the Spaulding webcam working!!!!!
Fri, 06-07-2013 16:55
The donation was to the museum as a whole. How it is used and whether any comes to steam department projects will be the decision of the museum [...]
Fri, 06-07-2013 16:53
Basically the plan is "ONLY" reassembly. As far as we know she is is reasonable mechanical shape. The big mechanical problem that stopped her (slack [...]
Fri, 06-07-2013 16:28
Nigel I read you guys got a one million dollar check donation!!! Will this be used to finish 1630 ,428, 5 and get started on the others next in line?
Fri, 06-07-2013 16:16
So does 1630 basically only need reassembly? With the boiler in particular. Does her tender or running gear need any work before she's ready for the [...]
Fri, 06-07-2013 12:00
Hello.. The voltage we are using and presumed the RR also used is 120 vac. The system is a little unique because the lite bulbs are each 60 volts. [...]