I had one day back at Union this Saturday before I leave for
my trip to Australia and New Zealand. I
am glad to say that a lot was achieved on 1630.
Everything was focused around fitting the throttle back into
the dome. It is essential that this be
in place and adjusted so that a pressure test can be carried out on the front
end. This will ensure that the super
heater elements are correctly fitted and have no leaks in the joints between
the elements and the header.
·
a lot of lagging has
been applied but little sheet metal was in place over it. Since you cannot stand on the lagging (as it
will disintegrate quickly if you do) placing a lot of sheet metal was
essential.
Most
of us were heavily involved during the morning, under Eric's guidance, to place
the sheet metal on the top of the boiler.
By
lunch time, as you can see below, she looked a lot more like a locomotive as
she was moved outside with steel sheeting covering most of the boiler.
Unfortunately
this is not as complete as it appears!.
The steel sheet consists of rings made up of 4 sheets and linked by
threaded rods at top and bottom. Just
below the walk way the top and bottom sections are joined . Both sheets have folded ends that can be
interlocked so that each side effectively becomes a single piece. Another challenge is that, where pipes and
brackets must pass thru the sheet, it is usually necessary that the hole in the
main sheet is over size and one or more smaller "infill" pieces must
be located behind the main sheet to fit tightly around the projecting
object. So it is one large and unwieldy
jigsaw!.
At
present only the upper sheets are in place with a few lower ones temporarily
fitted. A lot of work remains to
properly fit and adjust all the sheet metal.
However, with the top sheets in place, we were ready to fit the
throttle.
·
In parallel with the
barrel lagging, Collin and Phil fitted the throttle lever and quadrant onto the
back head. Ed also threaded the
remaining pipes that will enable the back head sheet metal to be completed.
·
Shortly after lunch
1630 moved out into the light of day for the first time in a while.
This,
in itself, was a significant piece of work.
A number of the team were working much of the morning to clear wires,
tools, steps and anything else that would be a danger when she moved. Finally debris had to be cleared from the
cross heads and lubricant applied for the move.
Thanks
to Jamie for the availability of the Army switcher and to JD for operating it. The move was achieved smoothly with one
alarm. The eye screwed into the dome
cover, to allow it to be lifted, becomes the highest pint of the loco and is
just foul of the shop door. This
resulted in a sudden stop and quick removal of the offending piece.
Anyway
the shop looked very empty and the opportunity was taken to clean the area and
recover a few small objects that had fallen over the last few months and not
been found under the loco.
·
Once outside the we
set about fitting the throttle. Collin
had borrowed and operated the B&G boom truck for the lifting.
First
the auxiliary hatch and dome covers were removed.
1630
is relatively unusual in having an auxiliary hatch and in it being difficult if
not impossible to adjust the throttle linkage thru the dome alone. Tom tells us that this is arose from the
original Russian specification which had a steam dryer in an extra tall dome,
making access to the throttle control rod (which is under the throttle above
the tubes in the boiler barrel) "tricky" unless you are n extremely
thin 6 foot person with extra long arms prepared to work suspend upside down in
the dome.
So
Jason, Vince and Eric worked the top of the dome and Phil, who was not taking a
week off as the pictures might suggest, spent much of the afternoon on the
cramped space on top of the tubes. Here
he was doing the critical work of guiding parts in from below and then adjusting
the control rod.
The
critical adjustment is to ensure that the valve sits tightly on its seat when
the throttle lever is forward as far as it normally goes on the back head and
that there is a lift of about 1 1/8th inch off the seat when pulled fully toward
the engineer. This is adjusted by
turning a threaded section of the control rod in the boiler to increase or
decrease its overall length. To do this,
Phil spent a lot of time stuck in the confined space of the boiler while the
rest of us worked the throttle lever and observed the movement of the thimble
in its seat in the valve body.
Here
you can see the throttle in position in the dome. The thimble is now seated in the throttle
body and the shaft at the center is connected to the control rod below and
adjusted. At the top of this view you
can see nuts on two bolts inserted from below.
These are securing the throttle body by means of the projection that can
be seen on the right hand side of the casting in the previous picture.
The
open pipe on the left is the entry to the auxiliary dry pipe that takes steam
back to the turret on top of the firebox in the cab from which are fed the
injectors, air compressor and all other accessories.
By
the time that we fitted the dome lid, Phil could be released from his prison
and allowed into the daylight.
·
While the locomotive
was outside we had the opportunity to remove a lot of the dust and loose
insulating material that had accumulated all over it. Jerry did a great job with the air line and
by the time we pushed her back in she looks a great deal cleaner.
So, by late
afternoon, we were able to push her back into the shop and, as my last
contribution for a while, I spent an hour fitting the 30 odd large nuts and
washers that hold down the dome lid.
Now I must follow work
with great interest from a considerable distance over the next few weeks and
provide updates as best I can based upon input from the guys. Hopefully I will be able to see a working
locomotive when I get back to Union in November !.
Nigel