As expected, the completion of the spraying last weekend opened
up a frenzy of activity. Work got under
way Tuesday and Wednesday once the paint was thoroughly dry. Almost all activity was on 1630 and she now
looks a very different locomotive from last weekend. Even so, much of the critical progress is not
visible.
On Tuesday and Wednesday work focused on preparing the boiler
for hydro testing. This involved fitting
the various water connections, valves and gauges to allow the boiler to be
completely filled with water and then pressurized.
In addition the large copper pipe, that connects from the
top of the firebox to the water column in the cab, had to be refitted. Once all this was done, the boiler was filled
and water circulated thru the pool heater to bring the boiler up to around 100F
for the pressure testing.
While this was being done Jerry and his son made huge progress
in fitting the banding that secures the edges of the sheet metal on the barrel
and firebox.
On Wednesday a pressure test was carried out. People have asked why this was necessary as
#1630 was hydro and steam tested last year.
What is happening now is not a full hydro test of the boiler shell
(which requires testing at operating plus 25%) but rather checking for any
leaks that may have developed as connections have been separated and remade
over the Winter. For this we test only at
operating pressure. The test served its
purpose!. On Wednesday we found leakage
around the connections of the pipe to the water column at both the first test
and an attempt to re-seal it.
However, while this was going on, Phil and I made progress in
refitting the injector starter valves.
Clearly on Saturday the first priority was to fix the
connections of the offending pipe. Eric,
Brian and others spent a lot of time thoroughly cleaning the seats and pipe
ends of the connections, annealing new copper washers and then carefully
re-fitting the pipe. It is a bear to fit
as it is long, bent to fit around other equipment and fitted between two rigid
seats. So, if it not exactly aligned,
the seals at one or both ends do not seat correctly and leak.
Anyway, all the effort paid off and, during the afternoon,
she was successfully pressure tested at 180 psi. This allows us to go ahead with the final
steps to remove the hydro connections and install the remaining parts needed
for operation (safety valves, brick arch etc.).
A lot of other work progressed in parallel with the pressure
testing:
The biggest and nastiest job was refitting the two big air
tanks under the walkways. These tanks
weigh about 300 lbs and are each suspended by three “U” shaped steel rings the open ends of which pass thru the
walkways to be secured by nuts.
The fitting is a “masterpiece” of the pipefitter’s art. The tanks must be squeezed into a confined
space above the valve gear. The tanks
are wider than the walkways so the supports are not simple “U”’s that could be
passed around the tank .
Then change in a few days since the picture further up in
this note is substantial.
The shape of each support is unique to its location and
mixing then up can lead to the need to pull back the tank and start over again!. By evening they were both in place although
the frustration during the day had reached considerable heights!.
The job of spotting and making good areas missed in painting
continued. A lot more of this will hopefully
happen next weekend when we expect to move the locomotive at least a little and
reveal areas of the wheels that have so far been hidden.
The fireman’s gauge glass, that has been thoroughly cleaned
and rebuilt, was refitted and showed no leakage under pressure.
The injector starter valves and their large connecting pipes
were largely re-installed.
Front sander discharge pipes were re-installed.
Work progressed steadily on the smoke box. This is probably the area that most threatens
our target to run on May 17th.
Dennis, assisted by Christian and Jason completed the adjustment of the new
steel sheet sections around the blast pipe.
By end of day the sheet sections were being finally installed on to the
mountings that had been welded into the smoke box and work was progressing on
the mesh sections and the welded mounts that will attach these to the smoke box
and complete the spark arrestor assembly.
The unexpected task that may cause a delay is in the smoke
box front casting itself. Close
inspection of this has indicated hairline cracks between the studs that secure
the bell mounting. These will need to be
weld filled, ground down and then the
holes for the studs re-drilled and tapped before we can remount the front of the
smoke box. It will be a busy two weeks.
So, we are close. A
couple of key tasks will determine if we can steam in two weeks as planned.
I am away next weekend so will follow the action with great
interest!.
Nigel