A lot of people have pointed out
that it is an awfully long time since there was a Steam Department blog
update. In my defense I plead that work
in my role as Museum Treasurer has been nearly full time (sounds better that
pleading idleness or incompetence!). So
here we are, an update of several months of work in the department.
Doesn’t time fly!. It seems like only yesterday that we were
working all night to get ready for the pre-season inspection. Now the operating season is over and the
Winter work program is well under way.
#1630 is back in the shop and we are busily crawling over and into her
to so what must be done before next season.
It was a very successful season
overall. We only missed one scheduled
day due to mechanical problems. (Unfortunately
Father’s Day when we had to fix a leaking valve).
It was rather challenging to
begin with. She seemed to use a lot of
coal to keep steam up but, once we reached fresh coal, she ran a great deal
better. I guess it should not be a great
surprise. Coal that has been lying
around for years has lost quite a lot of the flammable material so you shovel a
lot more for the same effect!.
Late in the season we had a
scheduled weekend out of service and this provided the opportunity for a good
clean. Aside from the usual coaling and
watering, the boiler was drained and refilled with fresh water, the paintwork
was washed and the rods cleaned and oiled.
After all the work she looked a
lot better. The dust was gone from the
top of the boiler but she is developing a “working” look as the condensation
from the safety valves and generator slowly discolors the paint on the firebox
sheet metal.
I fired the last two
Sundays. That is quite an experience to
really be part of the working locomotive after so long crawling in, over and
around her as a dead object in the shop.
#1630 certainly is different from other locomotives I have fired. I was working out that it is about 50 years
since I first fired a locomotive (Prince on the Festiniog Railway). The box is a lot longer and wider than
anything I have fired before. So a good
deal more throwing. However, on the
demonstration line, she is only running for a few minutes at a fraction of her
real load capability. Very different
from a small locomotive working flat out for a long time. You would certainly have extreme difficulty
keeping up with #1630 if she had a full freight load behind her unless the
stoker was operating. In museum service
the trick is to achieve a relatively thin fire without any gaps when you are
operating and not to have too much at the end of each run. Having a significant amount of hot fire when
you get back to Union can lead to a noisy lay-over!.
So what has been going on in the
shop and what is planned?. Obviously
#1630 will be first priority for Winter work and a lot must be done this Winter
to have her running for Memorial Day next year.
She is due for both the 30 day
inspection and annual inspections which amount to quite a lot of work. The annual inspection requires the drawbars
to be removed, checked and annealed.
While the tender is separated and the drawbar removed, we will do the
inspection and testing of the stays under the footplate. In addition we want to thoroughly examine the
rear axle bearings and rods. There was a
tendency to run warm in the rod bearings and more knocking than we would
like. So the plan is strip, measure and
carefully examine everything in this area and try to improve the running next
year.
Before we could even start the
work there were two busy weekends of preparation. First the locomotive had to be run on air to
thoroughly remove water from all the steam system in case of any freezing during
the Winter, Then there was the
cleaning!. I missed the air running but was able to
participate fully in the cleaning!. 3
hours with a high pressure hose in the
firebox blowing soot out of the tubes is an experience to be missed if
possible. The jokes of your “friends”
when you emerge black from head to toe are also to be avoided!.
With this done she was moved
into the shop and the locomotive and tender were separated. This provided some interesting views of the locomotive
cab and the way in which the tender is attached. The center drawbar is spring loaded and is
what pulls the tender and train. The two
outer bars are a safety mechanism should the drawbar fail in service.
Above the drawbar can be seen
the end of the auger of the stoker. This
is turned by a steam motor in the tender (of which more anon) to drive coal
along the large steel pipe from the tender to the locomotive. Looking again at the locomotive with part of
the footplate removed you can see the way that the cast pipe carries the coal
up toward the fire door.
In this view the fire-hole door
has already been removed. This large
casting would connect the end of the delivery chute to the fire-hole. Behind the closed door of the firebox, coal
would be driven up the chute to the delivery plate where steam jets would throw
it forward into the firebox.
After considerably more work, the
delivery system and the central footplate had been removed to reveal the back
of the firebox.
After several weekends of work
to do this stripping the actual inspection that necessitates it took only a few
hours. A group of flexible stays hidden
behind the stoker delivery chute do not have telltale holes and, as such, must
be inspected every 7 years. They all
proved to be sound so that part of the inspection is done. Unfortunately we found quite a bit of rust in
the supports of the footplate on the fireman’s side so Dennis will need to do
some rebuilding before we put things back together.
Another job being progressed is
the rebuilding of the stoker. This is
not essential but we would like the stoker to be operational at least for
demonstration purposes. It is not clear
how useful it would be in museum service where we need only a thin but even
fire. If it can be made to work we will
find out!.
First stage is to remove the
stoker motor. This is located behind a
panel in the tender on the fireman’s side.
Here it is being carefully eased out of the tender. This gives little idea of the effort that went
into this exercise. It was an extremely
tight fit and some modification of the hole was required to get it out with the
fork lift. We suspect that it may
previously have been fitted and removed on a greased plate so that it could be
turned first one way then the other as the hole was not big enough for it to come
thru directly.
Last weekend we carried out the
last major stripping exercise. The
locomotive was temporarily reattached to its tender so that it could be moved a
few feet back and then forward. The
objective is to remove the connecting rods between axles 4 and 5 to allow
measurement and checking of the rod bearings and alignment of the two
axles. The move is necessary because the
pins in #4 axle are removed by driving them back thru the wheel between two
spokes …. And you cannot remove the pins on both sides with the wheels in any
single position!. Here Jason and Phil
are removing the rod from the Fireman’s side.
By7 end of day both rods were removed.
A lot of other work is in progress
on 1630.
Most
of the strays have now been opened up (removing the fireclay that seals them in
service) and checked. (We must ensure
each year that the telltale holes are open).
Both
large air tanks have been removed and subjected to hammer and hydro testing. They are now ready for refitting.
Inspection
of the air compressor is under way. The
steam feed line has been removed and will be replaced. This line shows significant corrosion so the
decision has been made to replace it.
At
the end of the summer the tender and cab of #938 were repainted (Thank you
Roger!). She now looks a lot
better. In addition, Phil, JD and Brian
removed the tubes from the boiler. This
was largely an investigation exercise.
We really had little idea of the condition of the boiler of this
locomotive. The conclusion was that the
interior of the boiler seems to be in reasonable condition so there would be no
obvious barrier to rebuilding it. That
does not indicate any likelihood that this will happen any time soon. The fact that the boiler appears reasonable
indicates that it she is not a “no hoper”.
Given the work that would be required, all we need is a dedicated Rock
Island enthusiast with $500,000 or so burning a hole in his pocket and she
could run again.
The second big focus has been
the Shay and this will be our major project thru the Winter. The major jobs on the Shay are
Replacement
of a number of firebox stays;
Rebuilding
the front beam; and
Rebuilding
the smokebox.
Once these are done, we can get
on to the “more routine” jobs of re-tubing and re-assembling.
There is still some uncertainty
over whether we will need to replace some stays behind the motor. This would require removing the motor and the
bracket on which it sits, making the job rather bigger. While working to determine if the motor
removal will be necessary we are progressing other work that is independent of
this decision and ensuring that we are as ready as possible to do the motor
removal if required.
Over the Summer:
The
front truck has been prepared for remounting and placed back under the
locomotive. This may not be
permanent. Depending upon the need to
lift the boiler we might need to pull it out again to fit the new bottom of the
smokebox;
Everything
under the locomotive was cleaned and painted before refitting the truck;
JD
and Cody have been steadily removing stays that are identified as bad and in
need of replacement (generally due to blockage of the tell-tale holes);
The
parts for the front beam have been located and we are starting work on
preparing these. The coupler and its
mounting pocket have been moved down to the fabrication area for Jane to needle
chip and wire brush. Once they have been
examined for any cracks they can be painted and prepared for use;
David
and I worked on the grease nipples in the drive shaft and couplings. First conclusion – a Shay has a LOT of
these. All will need to be cleaned,
checked and replaced if not working correctly;
Work
was also starting on lapping all of the key steam valves. This led to the discovery that there were
cracks in the face of the main turret valve.
Clearly it was over tightened at some point. A new one will need to be made;
Work has also progressed
steadily on #428
Dennis
has been building up the axle boxes ready for machining. Unfortunately a problem developed with the
planer and we are waiting for parts that will hopefully make this operational
and ready to machine these axle boxes;
Work
was also progressed on repairs to the frame that will allow the rear spacer to
be refitted.
A
great deal of machine work has been carried out to produce new parts that will
allow the springs to be refitted.
Ed
has been working steadily at refitting the pipework of the cab. This is an “interesting” exercise. It is a 3-D jigsaw of pipes of various
diameters, shapes and end connections. I
will post a photograph next time but he has achieved remarkable progress in
turning what was a random jumble of pipework into a fitted backhead. It is all the more of a challenge as some of the
pipes link to the air pump – which is not there to check if that is what a
particular pipe should link to, and one or two seem to have been added to the
pile from other locomotives!.
So, overall a lot has been done
and there is much to be done in the next few months. If you are prepared to get
your hands dirty, there is no shortage of work if we are to have 1630 back in
service for the season and move forward with the Shay!.
I am now heading to the UK for
Christmas so will be away for a few weeks and look forward to more progress when
I get back and a busy Winter ahead in the Steam shop.
Nigel