In many ways this is a depressing time of year in the steam
shop. In the Spring there is a
substantial buzz as you turn the large dead mass of steel that you have worked
on all Winter into an active steam engine.
The reverse process in the Fall is less fun but just as necessary. However, aside from the regular work on 1630,
a great deal has happened in the shop and it promises to be a very exciting
Winter.
The end of season was celebrated with a department cook
out. Everyone had a good time. Many thanks to Jeff who came up with the idea
and organized the food.
On #1630 a lot of work has been done since the last
operations at the showcase weekend. Over
the last three weekends:
tender was emptied and cleaned;
boiler drained and all the washout
plugs removed and stored;
brick arch taken down and removed;
smokebox, tubes and firebox washed
out. (This is a really fun job involving
a lot of time in confined spaces with a high pressure hose so that you end up
stiff wet and black. I did a lot of this
last year and was not sorry that I had to be in the UK when it was done this
year!);
the locomotive was run on air the
weekend of 10/10. This is an important
step to remove water from all parts of the mechanism and accessories. The boiler is pumped up with the Sullair
compressor then the locomotive is run back and fore a number of times to clear
the cylinders, valve chambers and super heaters. The all the accessories, injectors, air pump,
generator, etc. are operated on air so any remaining water is removed.
The remaining job is to finally wash out the boiler. Given the low temperatures this job,
originally scheduled for this weekend, was delayed. This is another job that guarantees the operators
a good soaking so not at all pleasant at 45 degrees!!.
#1630 will come into the shop in a couple of weeks once work
is finished on painting #938. For this
Winter we have scheduled the usual mix of annual inspection and mechanical
improvement work. This Winter is not
planned to be as demanding as last (time will tell!!). The main target, aside from the annual
inspection, will be an inspection and overhaul of the valves. Hopefully, unless something unexpected is
found, this will require fitting of new rings to the valves and casting of a
new babbit bearing for the fireman’s side crosshead, which is getting close to
maximum allowable tolerance.
This weekend there was a very good turnout and many jobs
were progressing at once.
Obviously the biggest focus after #1630 has been Shay #5 and
this will continue to be the case. Much
has been achieved in the last few weeks and Brian arrived this weekend for a
major work session over the next couple of weeks.
Substantial progress has been made
on the smokebox. The holes have been
drilled for the rivets into the front ring.
These are now bolted into place, which makes the fit so tight that the
smokebox bottom is largely watertight (as we found this weekend – see below);
The holes must now be drilled for
the rivets into the boiler barrel and then the process of riveting can begin;
Many valves, gauges, injectors and
the water glasses have been fitted all in preparation for the big milestone of
filling the boiler;
On Saturday the throttle body was
fitted into the boiler. This is a very
tricky task as the large and heavy unit is a close fit on the opening in the
dome and must seal where the long vertical pipe seats on the elbow of the dry
pipe. So moving the pipe as you try to
position it risks damaging the critical seal, on which the throttle body
sits. After much effort it was
successfully fitted and the next big step was started;
The boiler was filled with water
for the first time since 1999!!. With a
couple of stops, to address leaks as they were identified, the water level was
raised into the dome. Overall the result
was very encouraging. A major problem
with #5 was a number of badly blocked stays, some of which were behind the
frame or motor and would require a great deal of stripping to replace. Huge effort has gone into clearing these but
the risk is that this could have cracked some of them. To this point we have found one stay where
this has happened but it is in a nice accessible position, so no issue to
replace. Experience is that a stay
broken in clearing is most likely to leak even without pressure so the fact
that only this one revealed itself is a cause for growing confidence;
The broken stay was plugged temporarily
with a nail and a number of tubes that showed minor leaks were rolled to seal
them. In the next couple of days the
dome cover will be fitted and the water heated to test under pressure.
So a LOT of progress.
Watch this space!.
Glen and Stu were busy South of the shop and succeeded in
starting and testing the traction motor of the Bay City crane. That should now be close to being able to
move under its own power again. They
also replaced a union in the fuel line of the “critter” (the 4 wheel diesel
that can provide switching power at the South end of the shop). This is a useful unit but has been very
unreliable in starting. Glen has found
and fixed a whole bunch of blockages and defects in the fuel supply so that it
is becoming much more serviceable.
A number of us were working on the new compressor set
up. Jeff is hoping to spend a couple of
weeks on this to get it close to, if not fully, operational.
Max was running the conduit to
bring in power for lighting and outlets;
The 480V supply was disconnected
and made ready to move the ducting to bring it into the compressor shed;
Rick was completing the wall facing
to allow the pipes for the cooler to be mounted. The large compressor is sufficiently powerful
that a 60ft cooling run is suggested.
This will be on the wall inside the shop and will provide a useful
source of heat when this unit is used in the Winter;
The placement of the pipework was
agreed and a detail parts list developed.
This should be delivered in the next few days so that Jeff can move
ahead with the installation;
Dennis was working on the flanges
needed to connect the compressor to the cooling array and air intakes.
On #428 Ed has substantially completed his exercise of
identifying and fitting the myriad of pipes originating in the cab. One pair of copper pipes proved extremely
frustrating as they did not seem to relate to any identifiable equipment
although we did have some pictures that indicated roughly where they were when
the locomotive was stripped. The most
likely answer after much forensic work is that as late as 1947 the locomotive
had a hydrostatic lubricator but, when retired a few years later, it had a
Nathan mechanical lubricator, which it still has. Ed now believed that these pipes are part of
the feed from the old hydrostatic lubricator that were never removed as they
were under the lagging. No wonder we
cannot find anything that they connect to!.
The above picture shows both Ed’s recent task and his next
one!. After completing the pipework he
will start rebuilding the reverser air cylinder.
Throughout the Summer Phil, with assistance from anyone who
looks underemployed / he can rope in, has worked on de-rusting and priming the
running gear of #938. Huge progress has
been made and she is looking a great deal better. In the next couple of weeks the priming and
painting will be completed so that the areas that have been de-rusted do not
deteriorate again.
So a very busy time in the steam
shop with a lot of progress.
Nigel