A fairly short update this week. It was a long and hard day's work. But, while we made reasonable progress, not much of it was visible.
On 1630:
· Most of us focused on the issue, identified last weekend, of the flues that moved forward as the ends were rolled into the front tube sheet. All but one were moved sufficiently to provide the required projection at the rear to allow beading. The one that could not be moved was removed and will be reworked. Having reduced the issue to one flue, we should be able to keep the delay to a couple of weeks.
· The remaining flues were rolled additionally in the rear sheet to reduce any likelihood of movement when these are rolled at the front end.
· Sean made great progress on priming the cladding sheets. After his efforts, a satisfying number were standing in the shop to finally harden before being put back into storage ready for refitting.
· Tom was working on the lathe to produce the guides that will be used to drill and tap the holes for the two stays that are to be fitted into the firebox patch. These screw into the caps of the flexible stays, that are already part of the outer firebox wrapper. They guide the drill to make an accurate hole in the inner firebox sheet, into which the stay is then threaded.
· Having checked to confirm that everything is working correctly in the water supply boxcar, Ed was working on refurbishing the pipe work for the boiler backhead fittings.
· The specially made seals for the bucker have arrived at last, so, once they have been softened by soaking in oil, work can begin during the week to get this reassembled and ready for the riveting to begin.
In other areas:
· Dennis completed the boom for the fork lift. Here it is upside down to allow the main beam to be welded to the frame that fits over the forks. This will hopefully be used before long to lift parts such as the dome cover back on to the locomotive.
· Bob and Mike continued work on the planer.
· Glenn continued building the guards for the drive belts on the new air compressor.
· Jerry did a great job on clearing the front of the shop. For those visiting us, we can no longer be identified as the shop behind the stack of debris, drums and disused "A" frame !!.
Next week I will be in New York on vacation, so I am looking forward to finding a lot of progress when I get back in two weeks time !.
Nigel
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...