It continues to absorb a lot of time to run #1630 but we have now started to see more jobs moving in parallel with the operations.Recently #1630 has run as
scheduled. Unfortunately we will now be
running less frequently, generally every other weekend due to the shortage of
trained crews. Brian came up from
Florida for two weeks and allowed us to run all weekend days in the last two
weeks but now we have guys on vacation and it is more difficult.
Last week required a lot of
effort to get ready for the weekend.
It is becoming clear that the
water is source of a significant problems.
A good deal of time has been spent on the water softener which does now
seem to be operating after a fashion. The
specialist has advised that trying to fix this equipment would require
significant spending with no certainty that it would be reliable. The museum Board has therefore approved the
acquisition of a new system as an alternative to trying further repairs. The supplier has agreed to install when
required so, if the existing system will hold together for the rest of the
season with some TLC, we will likely install the new one for next year rather
than fit it and then quickly take it apart for the Winter.
However, while all the tests
show that the water is very acceptable in terms of carbonate hardness, it does
seem to have a lot of other dissolved solids.
By the end of the July 4th weekend the water in the boiler was frothing badly despite
frequent blow downs when running.
During the next week Brian and others
completely drained the boiler and collected samples for testing. It certainly did not look nice. The fact that you could see bubbles form
where it hit the ground and float away on the stream could explain the issues
when running.
On Wednesday we washed out with
clean water, refilled both boiler and tender, then loaded the tender with
coal. The coal is also an issue. The random mix of some new (2013) and some 10
year old material in the coal stack keeps the firemen on their toes. You never know if you are going to have a
good trip or be shoveling like crazy to survive!. With the old and dusty stuff you have to put
a LOT into the box every trip.
Anyway, the good news is that
she has run reliably despite these issues and the coal pile is now down to not
much more than one week’s supply. After
that we can get some new stuff and hopefully get beyond the uncertainty.
Work has progressed in a number
of areas and plans for the next projects are becoming clearer.
Jeff, assisted by Phil, JD and
others did great work in clearing out and reorganization the shop. Most of the parts not belonging to locomotive
snot currently in the shop has been moved out into box cars. The re-usable tubes form #1630 have now all been
trimmed, bundled and stored in the box car.
We can now get to most parts of the shop with the forklift.
We also met with Dave to agree
the plans for the building extension to house the air compressors. The hope is now that this will be in place by
the Fall at which point we will have both a lot more powerful and flexible air supply
and a substantial amount of useful space in the middle of the shop.
Aside from the Winter work on
#1630 our main projects will be the Shay and #428. Much of the work on the latter is welding and
machining so most people will be working on the Shay.
In addition, before #1630 comes
in for the Winter, the objective is to get a coat of paint on #938. This is the first of a whole lot of static
display engines that sorely need such treatment.
On #938 good progress has been
made on removing loose rust and debris in preparation for priming. Kevin has put in a solid couple of day’s work
on the tender chipping off old paint but he usually works mid-week and
photographing!.
On Saturday, Jane was hard at
work with Phil preparing the cab roof for painting. She asked me to point out that we steam guys
sure know how to put a girl on a pedestal!
On the Shay, the big issue is
the stays that may need to be replaced behind the frames and motor
mountings. Tom will be confirming with
the FRA exactly which stays require replacement to be acceptable.
Brian and JD have been working
on the removal of stays from this area from inside the firebox. The outcome of these discussions and trials
will determine if we need to remove the motor and lift the boiler. At the moment it looks likely that this will
be the next task.
Work has progressed on preparing
the front truck for re-installation. The
truck has now been painted, the springs installed and the bolster refitted.
Ben put in a lot of good work on
cleaning the universal joints of the drive shaft ready for painting.
Last weekend the guys were hard
at work cleaning the frames in the area that will be less accessible once the
truck is back.
So a lot has been happening and
there will hopefully be more in the next few weeks when we are able to run
#1630 rather less.
Nigel
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]