March 13-14, 2009
Last Saturday's gang was Tom, Frank, Steve and myself. The original
goal for the weekend was to get the mainline walked and inspected for
defects and Tom continue to brush cut on the main. Frank and I ended
up getting out early and spent the entire day walking from MP0 to MP
4.8 marking defects along the way. We came up with 3 full pages of
issues to correct, mostly loose bolts and missing washers, but a few
other important defects like sink holes near 4 culverts... A day of
repairs will be necessary very soon, but for now the line is open to
40MPH without any speed restrictions. Tom spent all day on the mower
cutting brush from Seeman Rd to Four Mile Siding. He made huge progress cutting areas with very heavy brush. The improvement is very noticeable.
Our third gang, Steve, worked on
property all day. He worked all day getting the EJ&E 580 motorcar
cleaned up and running, which he ended up getting started later in the
evening. It hasn't run in years. Before we got the EJ&E 585 motorcar this was Frank's project. The 585 sidelined this project and has sat dormant since. We now have two A-8C Motorcars operable for the first time. Way to go Steve!
Sunday was Frank, Steve and myself. We hit
the main early with the EJ&E 585 motorcar, hydraulic power cart and
tie crane and headed to Four Mile Siding. Frank ran the crane prepping
the siding extension for three track panels... This involved picking up
about 50 ties laid out and clearing the area for weeds. In the
meantime, Steve and I drilled two bolt holes at the end of a rail that
had never been drilled on the siding. We now have bolts in both rails
and the joint put back together. There is no reason Four Mile
can't hold revenue trains now. We greased the new power switch at Four
Mile, and continued greasing all of the spring switches as we headed back to the
property for lunch. After a trip to pizza, I headed back out on the
main with a bucket of switch grease and hit all of the spring and power
switches on the mainline and station areas. Frank and Steve headed
toward the 580 and worked on the brakes. Saturday the 580 ran, and
Sunday the 580 stopped! The brakes hadn't worked correctly for years,
and now it runs and stops. The only issue holding up a test run is
that it's buried behind about a million freight cars and engines in
yard 10 - 100 track. Until the diesel guys get a large loco running to move
everything it'll hang in limbo. Again kudos to Steve and Frank for the
work!
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March 21-22, 2009
This weekend we had a different focus.
Saturday we picked up the transmission filter for the Model 50 Burro
crane from NAPA we had previously ordered. Getting that and a complete
set of filters for the 6000 filters set up the day's tasks. Frank was out with
Trackbolt (Frank's daughter Emily) and Tom was out with Tyler. Frank and Emily did wonders
getting oil changed and filters replaced on the 6000 while Tom and
Tyler did a great job cutting the mainline. By dark Tom had the entire
line cut from one end to the other! Only a few chainsaw jobs left and
we are 100% done with brushcutting. As promised, the line is tree free
by regular ops next month. Tyler and Emily helped me top off
the transmission fluid in the Model 50 burro and we tested it out with
much success. A few hickups, but it seems with the proper amount of ATF
and a clean filter the crane hauls very well. We tested it by moving
cars around Yd 11.
The diesel guys had a bunch of trucks that
needed to be rolled into storage at Yard 13... Long story short, 3 axle
trucks don't roll well through streetcar curves.... We assisted by re railing those trucks about 10 times in a span of 3 hours... We had
one set of trucks tucked away and another set half way to it's storage spot when the main
radiator coolant line on the 50 Burro blew apart leaving the crane paralyzed with a passenger truck hanging from the hook.. This was
around 9PM and we called it a day until we got parts due to lack of
options to lower the trucks...
Sunday Tom and I made it out
mid-afternoon armed with 5 gallons of antifreeze and a new hose. By
the time I showed up Tom had the new hose installed and antifreeze
topped off and we fired up the crane. We finished re railing the
passenger truck with the crane and Tom hooked it up to the Jeep with a
chain to drag it into it's storage spot a few rail lengths down. It
was a sight to see and got the job done without any more derailments or
broken windshields...thank goodness. The rest of the day was moving
equipment around for the next project and getting the Burro Crane put
away.
Thank you everyone for all the hard work so far this year.
Soon we'll wind down the machine maintenance and focus more on
projects. Coming up soon we are going to try to get Four Mile Siding extended
another 150', repair defects on the main and prep machines for tamping
and tie work. Machines that still need a fair amount of work is the Jackson 6000 tamper and the Model 30 Burro crane (X-17). We are out nearly every Saturday and help will be
appreciated more and more as we get into the operating season. Let me
know if you can join in the fun!
Adam Robillard
Roadmaster
lzeje657@msn.com