Saturday Report from Adam Robillard and Sunday Report from Frank Devries:
---------------
Today was just one of those days things just seemed to go right. It's about time I'd say.
The
day started early with Frank and myself and the first order of business
was to make a run to Farm & Fleet for some hydraulic oil and
parts. While we were away, JD Marzec and Greg Frech both showed up
willing to work! They did some invaluable work 'derusting' and lubing
track bolts in the shop and did a fine job. Upon our return we hit the
machine maint. work. Frank filled the hydraulic on the switch tamper
and began testing the new pump he had installed previously.
Unfortunately it turns out the pump is pumping the wrong direction... a
bit more trouble shooting and adjusting will be needed to hopefully get
the machine back to 100% soon. JD, Greg and I topped off the hydraulic
on the 6000 tamper and about that time Tom Hunter joined the gang. We
did some QC bolt work on the 6000 and cleaned up the tool boxes and
prepared to tamp.. The original plan was to do a walking inspection of
the main line but the hit or miss weather was enough to keep us close
to home.
During lunch we formulated a plan for the rest of the
day. Frank, JD and Greg set to do an oil/ filter change on the Amtrak
Ballast regulator which desperately needed it. The air filter is the
color of dirt and as Frank put it "hasn't seen daylight since the
Carter Administration..." Tom and I ran to Napa for oil and filters
and Frank, JD and Greg prepped the machines in Yard 11. While that
gang was doing the oil, Tom and I switched out the 6000 tamper and
began tamping the Streetcar line between Electric Park and the
S-Curves. The initial goal was to test the machine from its winter
work and break it back in. Amazingly everything seemed to work well
and only a few minor adjustments will have to be made. We spent the
next four hours tamping the carline and after the Regulator was
finished Frank, JD and Greg ran it around to our work area and began
regulating the freshly tamped track. Jeron Glander joined the gang
later in the day and did a great job running the regulator after JD and
Greg needed to leave. The four of us worked well into the evening
hours surfacing the track with our recreation of an Amtrak surfacing
gang. The ballast regulator made it through the day but the backlog of
work continues to pile up. A few things fell off the machine
unexpectedly but nothing to stop the machine from working. By the end
of the evening we had the track fully tamped and a majority of the
regulating complete. Some more work will have to happen in the
daylight but otherwise it is mostly complete. Its amazing how much
work can be done with a few good machines and a great crew. Next up
we'll begin tamping the mainline... There is plenty of surfacing work
there to keep us busy for a while. Thanks to all who helped today. We
accomplished an incredible amount of work, far more than any of us
expected. Thanks, Adam Robillard
--------------------------------
More of the same......
Today started late, with the time change and all. I arrived at about 10AM and was joined by Jeron around 11.
The first task was to determine the electrical short on the regulator.
When the lights were knocked off during the barn 11 project, the one
light was hanging by the wire. Seems during our work on Saturday, it
came in contact with the muffler, burned through the insulation and
shorted. Jeron had noticed the high amp readings Saturday night. A
quick clip of the wire resolved the short. The light bulb was broken in
that light anyway. I noticed most of the lights are burned out on the
machine. Next trip out I will pick up some spares from Napa.
We fired up the regulator and resumed the plowing and brooming of the
carline between Electric park and the S curve. After a short period of
time Jeron noticed a hydraulic leak. I sent him back to yard 11 to put
the machine away. Jeron found the leak was a loose hydraulic hose, and
with quite a bit of trouble, tightened up the loose connection.
Apparently like all track machines it was not as easy as putting a
wrench on and tightening. From what I understand it involved a
hydraulic power pack unit, and a lot of contortionist like moves. Once
fixed, it was back to work. Brooming and plowing continued until
another leak was noticed. Seems the valve for the oil pan had worked
itself loose. When the leak was noticed we shut down quick, and
resolved the leak. So that machine had it's second oil change this
weekend. I will hit up the hardware store to get a plug for that valve
to avoid a similar issue from happening again!!! By the end of the day
the track looks really good. There is still a bit of box work to be done, but it is a huge improvement.
While Jeron was fixing the hydraulic leak, I went for a walk. Track
walking that is... I was able to inspect from East Station switch to
Signal 251. During that walk, I found several loose joints, a couple of
hanging joints that will get fixed when we tamp, but no breaks, no
other defects that will affect opening day. I also marked several piles
of OTM and scrap along the main for pick up with the 50. Brush through
this stretch looks good. A touch up could be in order around Karsten's,
but that's about it. I also marked ties for replacement between E.
Station and Karsten's. I think the total was around 140 ties. I marked
5 ties off the bridge to ensure we have good support going into the
bridge.
Photos have been posted of the Carline results in the gallery below. A few shots of things from barn 10 as well.
http://www.irm.org/gallery/album240
Frank D.