Buzz Morisette wrote and took pictures for the following post:
With Bob K. out with a bad leg I thought I would update the Wood, Car, and Freight Shop Blog with a few photos from Wednesday.
The CGW Plow has seen a lot of progress even with the cold wet weather this spring. Exterior almost completely painted.
The stove is now back in place. Victor H, project manager, looks like he is waiting for the stove to produce some hot coffee. Dave R is coming up the ladder.
Dave and Chris R. checking their cameras, you can see the new toolbox and the completed car siding and ceiling work from this last winter.
On the way back to the shop I caught Randy Hicks in the pit inspecting CA&E 309.
Pete G. in the shop painting parts for Charles City Western 300.
He and his crew have rebuilt a 600 volt compressor this winter. Just checked out OK last week and ready to be installed.
300 looks great with fresh orange paint and rebuilt grids being wired in.
Over in barn seven I found Gery D. (L) and John F. (R) measuring TMER&L D-13 dump car roof for replacement car lines (Rafters).
The Gery and John team have also finished the 810 roof painting back in barn 4
Also busy in the shop today were Lorne T. prepping and painting interior panels for the Cleveland 4223 PCC. And last but not least Rich W. working up plans for the arch window frames we need to make for the Boston and Mane wood diner.
Tim was not around today but I don’t know when the CRT 1024 was last updated. The photo below shows the new sign roll box, roofing, end platform, beam work, and special cast running lights next to the sign box.
Tim and Frank just started cutting the new T&G car siding that’s set up in the shop. I need to finish the sign roll graphics for this project.
Thanks for looking, (get well soon Bob - I don’t like to type) Buzz Morisette, May 15, 2014.
Five volunteers came out to continue the progress. Ray Erickson, Brian Paterson, Dave Cook, Gary Sherman and yours truly. We continued sanding, needle chipping, sandblasting, masking and prepping for future painting, and removing of more corroded wall panels. Every little bit helps to reach our goal.
I have solicited for funds before on this blog site and I hope you again can help defray some of the upcoming costs of this restoration. Send your donations to the Restricted Fund RI 2612. Thank you Roger
A brief update this week as I
was away in Cleveland at the weekend.
The update is based upon input from Phil and Jim.
Unfortunately the key conclusion
from the week is that we will not be able to run next weekend, which was the
first that we had scheduled for operation this year. We are pretty much “day to day”. #1630 is complete and ready to steam aside
from refitting the smoke box front and the bell / lamp fittings mounted on it.
The key activities have been
repairing the cracks recently detected in the smoke box front casting. This is approaching completion but has been a
much slower job than anticipated as the casting proves to be iron rather than
steel. It must therefore be brazed
rather than welded (a much slower process).
Aside from other issues, brazing requires working from both sides so the
huge casting had to be turned over part way thru the process.
While Dennis was working on
this:
The steel and mesh work of the
spark arrestor was largely completed.
There seems to be some discussion over whether a handle will need to be
bent to provide sufficient clearance from the petticoat casting.
Eric and Jim worked on putting
lagging on the steam dome.
Jerry brought in the Frisco
stencils he had made that will be used to letter the cab side..
Tom lead a team of guys on rebuilding
the steam pipe from the governor to the air compressor. This pipe was seriously wasted and a new one
has been fabricated by an outside contractor to the intricate series on bends
required. A new union has been fabricated
to replace one of unique pattern at one end that was very eroded. The current activity is the final step of
threading the ends of the new pipe, fitting the unions refitting the new pipe
to the locomotive,
Brian worked on painting the
windows of the cab.
Mike over the last couple of
weeks has been working on the brake valves of the milk car to get it ready for
service.
A large group of guys worked on
cleaning up the rods of 1630. Although they will be covered in oil when in
service, they look a whole lot better if the oil film is on clean polished
steel!.
Track department finished fixing
the switch off the car line to the steam leads. The track is now back in
service.
So,
work continues during the week and we will be in service as soon as the
smokebox door can be refitted.
Nigel
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...