Sunday, January 6. 2013
Steam Department Update 01-05-2013 Posted by Nigel Bennett
in Steam Department at
18:17
Comments (6) Steam Department Update 01-05-2013There was continuing progress this weekend although we did encounter some issues that made progress a good deal slower than we would have hoped. On 1630: · The central focus was on rolling tubes. A further 17 tubes were successfully rolled at the firebox end. However this was far less than we had hoped as a result of an occasional problem which causes the ferrule to move along the tube as the tube expands into the sheet. When this happens, the tube and the ferrule must be removed and replaced. This is very time consuming and cannot be allowed to happen often as we have only a limited number of spare tubes. · After a good deal of testing and investigation of possible causes we will acquire a new tube roller during the week and are hopeful that this will cure the problem. Once we can overcome this issue progress should be a good deal faster. We probably rolled the 17 tubes in less than an hour and the remaining six hours were spent in removing and replacing the damaged tubes a s well as trying to resolve the issue. · Ed continued fitting the replacement pipe work along the boiler and has now completed the most difficult runs. · The patch is now bolted into place and we are waiting on Dennis's availability to finally heat shape it into alignment with the existing inner firebox sheets ready for welding. · Work continued on cleaning out the cab for refitting. The canvas curtains are now off and will be measured for production of the replacements. Canvas has a finite life after which it falls apart very easily. I think we can safely say that the finite life of these curtains has been reached!!. In other areas: · Stu and Bob made good progress on the planer. Most of the major assemblies have now been cleaned and prepared. The bed is ready for them to be refitted and the new electrical control system is being assembled. The various connecting pipes were measured to order replacements. Let's just hope the guys have a good plan of what connects to what !; · The area around the new compressor was cleared ready for final positioning. Once we have it positioned we can install the vibration isolating mounts and prepare to wire it up. · Work also started on preparing the Shay truck for re-assembly. The bolster must be drilled as the central hole, thru which runs the mounting pin, had developed an interesting oval shape. Purists believe that a round pin is best located in a round hole so this has been built up with weld and will now be drilled to produce a hole of the correct diameter. So reasonable progress on a number of fronts. Hopefully next week we can get tube rolling to progress more reliably and move on with that. Nigel Sunday, December 30. 2012
Steam Department Update 12-29-2012 Posted by Nigel Bennett
in Steam Department at
18:36
Comments (2) Steam Department Update 12-29-2012It is a "second-hand" update this weekend, courtesy of Phil Cwikowski. I did not make it to Union this Saturday as we had family visiting. Unfortunately, absent anyone who had experience with the tube roller, we were not able to roll more tubes into 1630 but a good deal of other progress was made. On 1630: · measurements were taken to fit the ferrules for the super heater flues. It looks as if we have enough for the firebox but will need to find or make some more for the smokebox; · the flues are now alongside the locomotive ready for refitting when the fire tubes have been secured; · the scaffolding and spare tubes have now been cleared so that we have free access to the front of the locomotive again; · needle chipping of the cylinder covers was completed and primer was applied to protect the cleaned surfaces; · the valve chambers were checked for sand blast material that could have been carried over from the boiler cleaning. The good news is that they appear clean and free of debris. In other areas: · Major progress was made on the wheel lathe. Air pressure was applied for the first time in decades to release the lock holding the back head. With this done, attempts were made to move the back bead on its slides ........... and it moved!!. This is critical as the back head weighs several thousand pounds and, were it jammed, it would require very heavy equipment to free it. After this the gear for turning the shaft of the back head was investigated and this was also turned. All of this checking is critical as these parts are normally moved under the power of substantial geared motors. Since it has not operated in many years it is critical to ensure that these huge parts are free to move before we apply power as major damage could occur if they are jammed when power is applied. The tricky part is judging the difference between jammed and normal resistance when it is normally moved by a large motor thru substantial gearing !!. · Stu and Bob returned to work on the planer and further progressed the cleaning and reassembly of this machine; · We gathered the information to calculate the total weight of the new air compressor and motor assembly so that Rick can now identify the vibration isolators that we will need to mount it. So progress on a number of fronts. Hopefully next week we can continue with the tube rolling. Nigel Wednesday, December 26. 2012
Steam Department Update 12-22-2012 Posted by Nigel Bennett
in Steam Department at
18:03
Comments (0) Steam Department Update 12-22-2012With Christmas close it was a small but active team at the steam shop this weekend. The next major milestone on 1630 was achieved as planned. The last 17 fire tubes were loaded so all except for the 9 that will be installed along with the super heater flues are now in place. Then we moved on to rolling the fire box ends. As with each step, this was initially slow. It is critical that we fully understand the technique and can do it right each time before we start to do it on a large scale. However we made a good start, got more confident as the day progressed, and by end of day the first 15 were rolled. Looking closely at the view below you can see the effect. Comparing columns K, L and M to the adjacent columns, these are now tight in the tube sheet and set at a consistent 1/4 inch projection beyond the sheet. Once we have proved that everything is watertight the projection will be beaded over. All tube ends in the fire box are beaded to protect the joint from the direct effects of the fire. The rolling requires a team of three and is achieved by first setting the tube accurately with a 1/4 inch extension beyond the tube sheet. The team member in the smoke box then clamps that end of the tube to prevent movement. The roller is then inserted into the tube. Here you can see the construction of the roller. Three small hardened rollers are turned by the rotation of the tapered pin that is inserted thru the center. The air motor is attached and rotates the central tapered pin. The rotating pin is slowly drawn into the roller forcing the three hardened rollers out into the wall of the tube slowly increasing its diameter. When the tube is fully expanded against the ferrule and tube sheet the taper pin has been largely drawn into the roller. The motor is then reversed to free the pin and the process continues with the next tube. In addition to the work on the fire tubes: · annealing was completed on the 16 super heater flues, so these are now ready to load once the fire tubes are secured; · drilling continued on the fire box patch. The holes are now complete on the front face. Once holes are made in the side face it will be finally formed to the mud ring along its whole length. We also took advantage of reasonable, if cold, weather to jack the end of the KCS tender to remove the wood packing that was left between the rubbing plates when it was delivered. This should now be in a condition which will allow it to be shunted so that the box cars of parts can be relocated back by the road to allow access. Nigel |
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Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...