Tuesday, November 12. 2013
Steam Department Update 11-09-2013 Posted by Nigel Bennett
in Steam Department at
10:34
Comments (2) Steam Department Update 11-09-2013It is a rather brief update this week. I made it back to the shop on Sunday after spending Saturday travelling back from New Zealand. A lot of activity was apparent from Saturday and continued on Sunday. After a week, 1630 no longer looks like an operational locomotive. The main activity on Saturday was to thoroughly drain her and then winterize (primarily running on air to blow any residual water out of the system). A number of parts have been removed to facilitate work over winter. This is not unexpected. The intent had always been to carry out test running to identify anything that needs to be dealt with as maintenance activity during the winter. The main objective of my trip to Union on Sunday was to work with Brian Davies before he leaves to produce a full list of work identified during the test running. While there is nothing particularly threatening it is a long list that will keep us busy over winter. The work also needs careful planning as, for example, it is important to deal with everything that may require us to pressurize the boiler to allow testing before we move on to things that require removing items that allow air to escape from the boiler !. The boiler lagging already looks substantially less complete. The securing bands must all be removed to allow painting of the sheet metal and this was started on Sunday. Visitors to the shop will notice that the end covers have been removed from the valve chambers. It is not planned that work will be done on the valves this winter but it was apparent during running that the valves are leaking significantly. While this is not essential for 2014 running, we will measure everything up for ring replacement perhaps in the following winter. On Sunday, Brian was removing the air tanks for painting while I worked on removing sheet metal and insulation to locate a small leakage of steam from the lubricator heater line along the boiler. In other areas, Tom, Jim and Cameron were working on the brake shoe holders for #428. The first of these was test fitted and looked good. So work started on the remaining 7. Mike was working on the plumbing for the planer. This is an interesting 3 dimensional jigsaw puzzle with a number of copper pipes, all with the same size connections, coming out of the hydraulic system into the machine. Now is a very good time to reflect upon how nice it would have been if someone had taken some good photographs of the set-up 20 odd years ago when it was taken apart !. So if, like me, you missed seeing 1630 as a hot steaming machine last weekend, it will be some months before you will be able to see her even looking complete again. However, the feel in the shop is very different. After two years fighting toward the objective of a working steam engine we now have one and must tackle the various winter maintenance tasks to make reliable operation the normal routine in 2014. One further important piece of information – SAVE THE DATE - The 2014 Steam Department Benefit at the Sanfilippo Estate will be on Sunday 29th June 2014. Nigel Monday, November 4. 2013
REVISED Steam Update 11-2-2013 a ... Posted by Nigel Bennett
in Steam Department at
21:08
Comments (2) REVISED Steam Update 11-2-2013 a successful season !Thanks to Phil and Cameron we now have some good photographs of the test running on Sunday. Good to see the weather was a LOT better than the evening of the steam test. Based upon input from Brian Davies, it sounds like a pretty successful week in the steam shop with the major objectives on 1630 for the year now achieved. This is both good and bad from my perspective. I might have hoped for a few problems to fix and test next weekend when I will be back!!. It had been the target to do a little running before the winter to ensure that we were able to identify potential issues to be addressed over winter. That was achieved over the weekend. After the steam test on Wednesday, Brian and others spent the next couple of days adding items such as the petticoat, that were the minimum needed for significant running. There was some disappointment on Saturday when the planned running had to be abandoned when a leak was detected in a steam union in the cab. The rest of the day was spent replacing the unions and, to ensure no further issues, the whole pipe involved. This may have been “over kill” as close inspection of the pipe suggested that it was sound and the leak affected only the threads at the end. However, with a steam engine you cannot be too careful and the objective is to locate and fully correct any issues before next season. With the leak fixed, the locomotive was successfully steamed again on Sunday. Much of the most important testing was around the rear driving axle. It was the work on the axle boxes here that caused her to be stopped in 2005 and she has not run since this was done. The results were good. There had been some concerns about the reduced flexibility when running around the “Y” but, while she is noticeably tighter than in the past, this was not a serious problem. A number of runs were made up and down the main line. This allowed accessories and controls that have not been in routine use for nearly ten years to be exercised normally. The results were good and it also enabled a lot of the team, who have put in so much work, to experience a ride on the result of their efforts.
The new rear axle bearings run warmer than the existing ones but not excessively so. It looks as if these are good and should settle in as more grease works into them with additional running. There are probably a few minor items for the over winter work list but it does not seem that anything major was detected. So, I rather suspect that this will be the last run for 2013 as it is coming time when it would be safer to have the locomotive and water system winterized. The testing was done with some work not completed. Various missing lagging and bare metal is apparent in the photograph but it is a great relief to see her operational on the main line and looking good in the Fall sunshine. Only the essentials for test running were completed in the last few days so, for example, the brick arch and smokebox sheet work and spark arrestor mesh are not yet in place. This is no problem for a few test runs but required before the season. Then of course there is the big job for the winter – the application of a whole lot of paint!!. It looks like a busy winter but the clear expectation that she will be fully ready for the 2014 season. So I am looking forward to getting back to Union and seeing what she looks like after a spectacular month of effort – great work guys!. Nigel Friday, November 1. 2013Frisco 1630 fired up and tested!
Smoke at Smokey Hollow! The air smells good again down at the steam shop! Yes folks, for all you Fans of Steam, your waiting is almost over. On October 30, 2013, the 2-10-0 was test fired, and operated under its own power! But, the work is not done on the 1630!. It is just the beginning. Plenty yet to do. Please come out to help!!! There are not enough "THANK YOUS" and "pats on the backs" to truly describe the work, planning and money that has gone into this restoration project. Thank you, Tom Schneider and fellow volunteers!! I hope when you are out at Irm stop by the steam shop and thank the guys and gals for their devotion and efforts. They will appreciate it. Their work is never done. Please THEN make a donation to the Steam Restoration Fund, or the UP 428 fund or the Shay 5 fund. They are the next to get running. Thanks.... Roger Kramer, a steam fan and friend.
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Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...