Sunday, December 1. 2013
Steam Department Update 11-30-2013 Posted by Nigel Bennett
in Steam Department at
12:51
Comments (0) Steam Department Update 11-30-2013A sharp but, if the forecast is to be believed, brief improvement
in the weather allowed us to do a series of moves of material in and out of the
shop this weekend. Spare tubes and flues
were moved out of the shop into the boxcar and the fire bricks that make up the
arch in 1630’s firebox were brought in from the water supply car. This gives us more room in the shop and jobs
that we can continue if we have to hunker down in the shop for a few weeks!. ·
Cameron had finished and fitted the stud during
the week and we were able to ensure that it is leak free. This enables the boiler to be opened up and
thoroughly dried for the Winter and also means that the insulation can be
refitted; ·
Jane was hard at work much of the day painting
many different things including mounting brackets for the equalizing reservoir
and a lot of infill sections for the sheet metal. This is one of the jobs that will require
quite a bit of work over Winter. Wherever
a pipe or bracket projects thru the lagging there must be a hole in the sheet
metal. It is rarely possible to simply
have a hole in the big sheet metal section to tightly fit around the projection
(as the sheets must be moved around to fit them). So smaller sections of sheet metal must be
fitted around the projection under the main sheets to stop water getting in and
damaging the insulation. The tests
indicated a lot of areas where we need to seal small holes; ·
Jerry put in a solid day on the insulation. He has refitted all the insulation that was
removed to trace the steam leak from the lubricator line and has made
substantial progress on the panels each side of the firebox. These are an absolute pain as they
must be removed annually to inspect the ends of the rigid stays. So there are areas where the insulation blocks
are secured to the sheet metal rather than the boiler. To add to the challenge, some of the sheets
cover areas where part of the insulation is fixed to the boiler and part to the
panel so the insulation must be cut so that the insulation must interlock when
the sheet is fitted ………. while maneuvering it around and behind various
fittings. My guess is that this is a
modern problem. From memory of working
with asbestos matting in the early 1970’s (yes I did that that apparently
survived !) is that it had much more strength than the modern “safe”
insulation, which tends to fall apart very easily; ·
Ed worked on cleaning the water glasses which
were noted as not showing clearly during the test. (The glasses have a reflective surface that
provides a clear indication at night under limited illumination and so need
occasional “deep cleaning”); ·
Jason and Trevor removed some wash out plugs and
the inspection hatch. The air blower was then fitted so
that a constant air flow will be maintained thru the boiler for a week or so to
ensure that it is thoroughly dry for the Winter; ·
Cameron had painted the equalizing reservoir during
the week so Phil and I set out to hydro test this ready for refitting. Set up for pressure testing is always slow as
you have to find / make a suitable combination of fittings to link from the pump
to whatever fitting happens to be on the tank that you want to test. Having done this and connected the air and
water it became clear that the main pressure hose from the pump has developed a
leak !!. Ho hum !. That is now a job for next week once the hose
has been professionally repaired; ·
The fire bricks were moved into the fire box in
preparation for another fun task. The
arch is built from a number (I currently think 4) differently shaped bricks
that fit between arch tubes, from arch tubes to firebox wall etc. We need to plan out exactly how many of each
are required and identify any that we are short of so that we can have a
suitable supply on hand for next season.
It is likely that we do not even have a pattern for one type so will
need to make the wooden pattern from which the bricks are cast using one of the
existing bricks as a model; ·
Jason started removing the blower line in the cab. This had a small leak detected during the
test run so is one of a number of the pipes in the cab that we plan to adjust
and refit during the Winter. With 1630 in reasonable shape, Brian, Cameron and Phil did
quite a lot of work on #428, where much of the current focus is on the brake
gear: ·
Brian and Cameron have been working steadily
thru the brake shoe holders. These have
now all been drilled out for fitting of the mounting pins. As with much of this locomotive, years of
wear and limited maintenance meant that holes had become substantially oval. The repair has required filling the hole, by
welding in new material, and then re-cutting the holes to the original size. In this case 8 brake shoes , two hole per
holder so 16 substantial holes to be filled and re-cut; ·
With this done, focus is now moving to other
components of the brake rigging. The
second of the main shafts was removed (from the engineer’s side) so that both
can be worked on together. This sounds
easy but the things weigh more than 100 pounds and had to be extracted from its
mounting under the locomotive then rolled / man handled over the track between the
wheels to get to the fork lift (no pictures as I was operating the fork lift !); ·
Trevor was working on the frame that is required
to support the pistons so that the heads can be built up with braze metal. On the Shay, Jason and Trevor finally managed to remove a
wash out plug from the belly of the boiler that we have been fighting with for
a long time. We do not know when it was last
removed. It is above the front truck and
not easy to reach. History suggests
that, when the loco was last running, it was impossible to remove as it was far
too tight to extract in the confined space above the truck. Having finally extracted it using heat, lots
of penetrating oil and very long cheater bars !, we can now understand
why. Someone long ago must have put it
in wrongly threaded and solved the problem of leakage by tightening with great
force. Absolutely what you should not do
with a brass wash out plug!. Oh well, it
will now be remade and fitted gently. Bob, Ed and Jane continued work on the planer. This is now just about fully painted and
looks really great. Much of the effort was directed to pumping degreaser thru
the various oil passages to remove as much debris as possible before filling
with oil. Much of the effort was
directed to trying to see as much as possible of the interior passages to
determine how effectively the debris had been removed!. The same oil is used to lubricate the machine
and provide the hydraulic power that moves the bed back and forth so removing
debris and placing filters is rather important.
Most of the shop are now waiting with great anticipation to see the machine
work. The team seem to be non- committal
about when they will bite the bullet, fill it with oil and see what happens !!. So a day of steady progress in a number of areas. Nigel Sunday, November 24. 2013
Steam Department Update 11-23-2013 Posted by Nigel Bennett
in Steam Department at
13:39
Comments (0) Steam Department Update 11-23-2013Wow!. The Winter temperatures have certainly arrived with a bang this year. This time last year we were happily moving tubes in from the boxcar. This weekend anything outside was done quickly and in heavy clothing. At 20 degrees with a strong wind most work was done inside. However, we did manage to ensure that the drop pit pump and anti-frost heating are working and move the Sullair into the shop so that it should start if required. On 1630: · Matt and Jim produced new washers for the water connections between the tender and the injectors. The filters baskets were passed to Dennis to work on the brazed surfaces. Hopefully the combination of these two actions will provide a long term fix for these connections that have tended to leak for some years. · Rick made good progress on fitting the sheet metal screws to secure the radius pieces of the sheet metal on the back head. Once this and a couple of other jobs are done we should be able to paint the firebox in the cab. That promises to be great fun working around all the pipes and fittings!. · Eric did some hours of laborious needle chipping to remove paint from the driving wheels. Kevin did a lot of this some months ago. Now that the locomotive is in a different position, the rest of the wheels can now be cleaned off ready for painting. · Ed and Bob remade the copper pipe connection for the steam heat line; · Matt refitted the reflectors to the gauge lights. These should now be a lot brighter; · The last of the three air tanks below the walkway was removed for painting. In addition, I worked with Collin and Matt to remove the small equalizing reservoir from under the cab floor so that it can be hammer and hydro tested. This is small but a real pain as it is surrounded by a bunch of pipes that run just below the cab floor. In the photograph below you can just see the end of the reservoir in this view under the cab on the engineer's side.
Here Collin is squeezed between the locomotive and tender working on the nuts that secure the reservoir to the back of the locomotive. Anyway, after much cussing and tricky maneuvering, it was extracted. By end of day, I had successfully hammer tested and primed it. · Jerry made good the insulation on the fireman's side, that was removed to fix the leaking lubricator line. He then started on the lagging of the firebox side sheets. These are unusual when compared to all the other insulation. As they need to be removed annually to inspected the firebox side stays, the insulation is attached to the sheet metal rather than the boiler; · Dennis continued work on the sheet metal for the smokebox. · Cameron and Brian worked with Tom to machine the new stud. In other areas: · Phil prepared the bolster of the Shay by removing the last loose spring locator. Once Dennis welds in the new locator we can start planning to put the bolster and springs back into the truck. · Tom completed machining the first wedge for the axle boxes on #428; · Brian and Cameron continued drilling the brake hangers for #428; · Cameron worked on the moulds that are required for the casting of the babbit bearings for the cross heads; · Bob and Ed worked on preparing the oil system of the planer for filling. The challenge is the best way to get debris out of the system before filling it with the approximately 80 gallons of oil with which it will operate; · Brian brought in the replacement switch for the forklift and this was fitted. So it was a successful weekend as we continue to work thru the Winter maintenance tasks. Next weekend will provide a good opportunity to work off the effects of the turkey !. Happy Thanksgiving Nigel Monday, November 18. 2013
Steam Department Update 11-16-2013 Posted by Nigel Bennett
in Steam Department at
22:04
Comments (0) Steam Department Update 11-16-2013This weekend we started in earnest on the over winter work program, primarily on 1630. The biggest overall job will be painting the locomotive. Brian and Jane worked on understanding exactly how best to apply the paint that will be used. It is a two part type that we have not previously used and some significant planning and preparation is required. Two of the air tanks were removed and these will be the first items to be painted to provide experience and testing of the best methods of preparation and application.
Dennis was hard at work on the plate work and mesh screens for the smokebox. These are now approaching completion.
We also worked thru the items that we needed to do while we can still pressurize the boiler. · One key item that worked out well was the tracing of a small steam leak that appeared around the handrail stanchion juts behind the sand dome. Steam appearing from behind the lagging is always troubling as it can indicate all sorts of things, some more troubling than others. We had suspected (and hoped) that it might be as simple as a loose connection on the lubricator steam line. Much to our relief it was found that this was exactly what it was. After removing a good deal of sheet metal and lagging to locate the union, soap solution revealed a very obvious leakage where the union had not been fully tightened when a new pipe was fitted.
· Matt, Jerry and others worked on the cab lighting. 3 lights in the cab were not working during the test running. A mixture of defective bulbs and a loose connection were found and by end of day, all lights on the locomotive were fully operational when the generator was run on air. They did also find and correct the issue of "dim" gauge lighting on the engineer's side!. The lights sit in little dishes that direct the light toward the gauges. The dishes have a white enameled surface to direct the light. The years have reduced this thru rust and smoke to a nice matt black!!. Cleaning and repainting have fixed that issue. Jason, Cameron and Phil spent much of the day winterizing the water supply in the boxcar. This is a tricky job involving a lot of blowing compressed air thru the system to ensure that it is water free and then taking apart the water softening system. The weather did not help with wind and rain making the job more unpleasant than usual. Good job guys!. So it was a successful day working toward having 1630 in top condition for 2014 operations. Nigel
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Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...