A sharp but, if the forecast is to be believed, brief improvement
in the weather allowed us to do a series of moves of material in and out of the
shop this weekend. Spare tubes and flues
were moved out of the shop into the boxcar and the fire bricks that make up the
arch in 1630’s firebox were brought in from the water supply car. This gives us more room in the shop and jobs
that we can continue if we have to hunker down in the shop for a few weeks!.
·
Cameron had finished and fitted the stud during
the week and we were able to ensure that it is leak free. This enables the boiler to be opened up and
thoroughly dried for the Winter and also means that the insulation can be
refitted;
·
Jane was hard at work much of the day painting
many different things including mounting brackets for the equalizing reservoir
and a lot of infill sections for the sheet metal. This is one of the jobs that will require
quite a bit of work over Winter. Wherever
a pipe or bracket projects thru the lagging there must be a hole in the sheet
metal. It is rarely possible to simply
have a hole in the big sheet metal section to tightly fit around the projection
(as the sheets must be moved around to fit them). So smaller sections of sheet metal must be
fitted around the projection under the main sheets to stop water getting in and
damaging the insulation. The tests
indicated a lot of areas where we need to seal small holes;
·
Jerry put in a solid day on the insulation. He has refitted all the insulation that was
removed to trace the steam leak from the lubricator line and has made
substantial progress on the panels each side of the firebox.
These are an absolute pain as they
must be removed annually to inspect the ends of the rigid stays. So there are areas where the insulation blocks
are secured to the sheet metal rather than the boiler. To add to the challenge, some of the sheets
cover areas where part of the insulation is fixed to the boiler and part to the
panel so the insulation must be cut so that the insulation must interlock when
the sheet is fitted ………. while maneuvering it around and behind various
fittings. My guess is that this is a
modern problem. From memory of working
with asbestos matting in the early 1970’s (yes I did that that apparently
survived !) is that it had much more strength than the modern “safe”
insulation, which tends to fall apart very easily;
·
Ed worked on cleaning the water glasses which
were noted as not showing clearly during the test. (The glasses have a reflective surface that
provides a clear indication at night under limited illumination and so need
occasional “deep cleaning”);
·
Jason and Trevor removed some wash out plugs and
the inspection hatch.
The air blower was then fitted so
that a constant air flow will be maintained thru the boiler for a week or so to
ensure that it is thoroughly dry for the Winter;
·
Cameron had painted the equalizing reservoir during
the week so Phil and I set out to hydro test this ready for refitting. Set up for pressure testing is always slow as
you have to find / make a suitable combination of fittings to link from the pump
to whatever fitting happens to be on the tank that you want to test. Having done this and connected the air and
water it became clear that the main pressure hose from the pump has developed a
leak !!. Ho hum !. That is now a job for next week once the hose
has been professionally repaired;
·
The fire bricks were moved into the fire box in
preparation for another fun task. The
arch is built from a number (I currently think 4) differently shaped bricks
that fit between arch tubes, from arch tubes to firebox wall etc. We need to plan out exactly how many of each
are required and identify any that we are short of so that we can have a
suitable supply on hand for next season.
It is likely that we do not even have a pattern for one type so will
need to make the wooden pattern from which the bricks are cast using one of the
existing bricks as a model;
·
Jason started removing the blower line in the cab. This had a small leak detected during the
test run so is one of a number of the pipes in the cab that we plan to adjust
and refit during the Winter.
With 1630 in reasonable shape, Brian, Cameron and Phil did
quite a lot of work on #428, where much of the current focus is on the brake
gear:
·
Brian and Cameron have been working steadily
thru the brake shoe holders. These have
now all been drilled out for fitting of the mounting pins. As with much of this locomotive, years of
wear and limited maintenance meant that holes had become substantially oval. The repair has required filling the hole, by
welding in new material, and then re-cutting the holes to the original size. In this case 8 brake shoes , two hole per
holder so 16 substantial holes to be filled and re-cut;
·
With this done, focus is now moving to other
components of the brake rigging. The
second of the main shafts was removed (from the engineer’s side) so that both
can be worked on together. This sounds
easy but the things weigh more than 100 pounds and had to be extracted from its
mounting under the locomotive then rolled / man handled over the track between the
wheels to get to the fork lift (no pictures as I was operating the fork lift !);
·
Trevor was working on the frame that is required
to support the pistons so that the heads can be built up with braze metal.
On the Shay, Jason and Trevor finally managed to remove a
wash out plug from the belly of the boiler that we have been fighting with for
a long time. We do not know when it was last
removed. It is above the front truck and
not easy to reach. History suggests
that, when the loco was last running, it was impossible to remove as it was far
too tight to extract in the confined space above the truck. Having finally extracted it using heat, lots
of penetrating oil and very long cheater bars !, we can now understand
why. Someone long ago must have put it
in wrongly threaded and solved the problem of leakage by tightening with great
force. Absolutely what you should not do
with a brass wash out plug!. Oh well, it
will now be remade and fitted gently.
Bob, Ed and Jane continued work on the planer. This is now just about fully painted and
looks really great.
Much of the effort was directed to pumping degreaser thru
the various oil passages to remove as much debris as possible before filling
with oil. Much of the effort was
directed to trying to see as much as possible of the interior passages to
determine how effectively the debris had been removed!. The same oil is used to lubricate the machine
and provide the hydraulic power that moves the bed back and forth so removing
debris and placing filters is rather important.
Most of the shop are now waiting with great anticipation to see the machine
work. The team seem to be non- committal
about when they will bite the bullet, fill it with oil and see what happens !!.
So a day of steady progress in a number of areas.
Nigel