Here is a very late update on the progress on GB&W 2407 from February 12th, I had drafted it before I went on vacation for a couple of weeks and forgot to publish it. We had a pretty large group out Saturday afternoon, including Frank DeVries, Marcus Ruef, Warren Lloyd, Kyle Merkel, Kevin Hennessy, Greg Ceurvorst, Dave Fullarton, Jeron Glander, Jim West, Dan Currens, Rich Schauer, and myself. The main tasks were to get the rest of the water system tight. The previous weekend and during the week we had made a number of repairs, but did not have a chance to water it again. The electrical system, governor, and air compressor were also worked on.
Dan Currens started by digging into the electrical system, verifying everything was connected and functioning properly in the cabinet, and with the governor and such. Kyle and Jim worked on refilling the governor and pump with oil. We will have to flush the system again at a later date. There was some minor raccoon damage, but the majority of the electrical system was in pretty good shape.
Meanwhile Dave and Kevin were working on checking all the injection pumps, seeing which ones were free and which were sticking. They found a bunch that were very tight and began working on lubricating and freeing them up. Warren, Kyle and Rich joined in as well.
Frank and Marcus made a gasket to replace the leaking one on a cover on the air compressor, and then changed the oil in the compressor. We started watering again to verify the latest repairs and was very surprised at how well it was holding water. We did mark a few more water elbows that we had not marked the last time, along with some additional pipe couplings. Frank noticed a crack on a low pressure cylinder liner that was leaking water. There were a number of other leaks in this area the last time, so we didn't notice it. We are looking into some ways to fix this without changing the liner as it looks like the only damage is this area on the outside of the water jacket.
Greg joined Marcus and Frank, and they made some more gaskets to replace the leaking ones along with some hoses on a few of the water elbows on the engineers side after draining the water. They made enough for all the ones that were leaking on both sides. Warren replaced two of them on one side of the loco while Marcus and Frank replaced a few on the engineers side. While draining, we noticed that the compressor and water cooled intercooler on the compressor did not have a drain as the pipe that should have gone to the main drain valve was removed and plugged. This was done sometime when it was on the railroad, and is probably why there were water problems on the compressor. We'll have to thoroughly check out the intercooler as well.
It was a very productive day and I'd like to thank everyone that helped out to move this project much further along. Be sure to visit the Photo Gallery of the current work going on. Also, donations to the RSD15 are still needed and appreciated.
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...