Sunday, April 7. 2013
Steam Department Update 04-06-2013 Posted by Nigel Bennett
in Steam Department at
09:04
Comments (0) Steam Department Update 04-06-2013A much more successful day yesterday at the steam shop. On 1630: · We continued with loading the super heater flues. Suitable homes were found for the shorter flues and we should not need to do further welding. All but one are now in place. This one was fitted but removed to allow access to the adjacent (top right) hole for fitting the ring.
· For reasons that are not clear, the top right hole is over size and needs a steel ring to reduce the size to fit a flue. Tom had turned the ring on the lathe a couple of weeks ago and today we fitted it. This was not easy as the tube had to be passed thru and beyond the sheet and then the ring expanded into the hole. The expanders are designed to work on the end of a long tube rather than a narrow ring, so positioning this while expanding was tricky. However, this was achieved successfully and the tube is now seated into the hole with the new ring around it.
· Ferrules were fitted into the front tube sheet around all but 3 of the flues that will require them. So this is largely complete, although some of the ferrules still need to be ground flush before we can roll the tubes into place. The ferrule can be seen, around the tube, in the hole immediately below the empty hole in the picture above and compared to the one to its right which is still to be ferruled. · Set up is now well under way for rolling the super heater flues into place. As compared to the rollers used for the small tubes, those used for the large tubes require a BIG air motor weighing about 60 pounds. This cannot be hand held in use. For the rear tube sheet a staging is now in place on which the air motor will be set to drive the roller expanding the flues into the sheet.
· On the front of the smokebox mounts are being set up to hold the large gearbox thru which the air motor will drive the roller expanding this end of the flues by means of a long shaft with universal joints. The gearbox was earlier set up directly on the smokebox ring to assist in rolling the ring. However, for the tube rolling it will need to be mounted further forward on the brackets. · Most of the smaller pieces of cladding that have been primed were moved back on top of the machine shop and large sections that must now be cleaned and primed were brought down. These will be cleaned outside, now that the weather has improved, as there is a great deal of rust and remnants of insulation material that must be removed. · Unfortunately the contractor repairing the riveting hammers has had trouble obtaining materials for the seals so these are still not back and the riveting is on hold. · The patch screw is now in place in the firebox corner. (Despite the name this does not actually secure the patch in our case). This is a special screw threaded into the mud ring to secure the outer sheet to the mud ring at the corner. Once in place its head looks like another rivet. The need arises because of the sharp bend at the corner. The inner surface is much shorter than the outer so rivets tightly spaced on the inside would be widely spaced in the outer sheet. These blind ended patch screws are set between rivets on the outside. Once in place, they look like rivets. This one was damaged and is now replaced. Elsewhere: · Big progress thanks to the diesel guys. They switched the tender out into yard 13. It made an interesting combination with #9255. This was quite a long switch movement as it had to be pulled out with chains to the trolley loop, where #9255 could then run round the loop to get to the end that has a coupler. It then had to be run out thru the depot to reverse direction on the "Y" before it could be brought back around the loop to be propelled into yard 13. After all this the box cars could then be spotted where we could get to them. Thanks guys !
· With the box cars accessible again, Jeff and the team were able to move material around in the all-door car and get to the tubes for the Shay. These are now in the shop ready for swaging. This is half the total tubes for the Shay. The rest are on stands on the other side of the area, so all the tubes are now in the swaging area.
It is startling to compare the Shay tubes with those for 1630. This is one of the half dozen additional tubes we need to swage for 1630. amazing., I knew the Shay tubes were smaller but had not visualized the difference being this extreme !. Not only are they shorter, but there are far fewer of them.
· Bob has now wired a good deal of the control panel for the planer. During the week, Kevin had largely completed needle chipping it ready for painting.
So, good progress this week although the delay in being able to rivet the patch is becoming a serious concern. Nigel Sunday, March 31. 2013
Steam Department Update 03-30-2013 Posted by Nigel Bennett
in Steam Department at
11:12
Comments (5) Steam Department Update 03-30-2013The number of people in the shop was a bit reduced at Easter weekend and it was unfortunately one of those days when a lot of hard work did not achieve as much as was hoped. On 1630: · The main focus was on loading the super heater flues. Unfortunately this proved a great deal more tricky than had been hoped. When the tubes were safe ended each was carefully measured with the objective that it was matched to a specific location with a certain amount of excess length to be ground off after fitting. When the first few were fitted it became clear that there is a significant variation from the intended lengths with some shorter and some longer. Clearly, where there is excess length it can be cut off. But if we have any that are too short to be fitted we would need to get more welding done. The key objective became to ensure that the shorter ones can all be used without the need to get a welder in again to lengthen any. So, instead of simply slotting each tube into its numbered hole, it became an exercise in loading and unloading tubes multiple times to ensure that the shortest tube that provides the required projection at each end is used in each hole. As each tube is 17 feet long and 5 1/2 inch in diameter, they are heavy beasts to fit and refit so it was a hard day's work made worse by the fact that it was unexpected. The first part is easy. The fork lift raises the tube to height and in this shot, Phil and Sean slide the tube into the hole in the tube sheet.
The next bit is more tricky. Once the tube is off the forks it becomes a giant lever pivoted in the tube sheet. Here Dave is assisting by controlling the end of the tube to ensure that is slides smoothly thru the hole and can be located in the rear sheet without dislodging the ferrule at that end.
Once it is in place there is a careful process of gauging the projection at each end to ensure we have the required 1/4 inch minimum. Given the length issue, a number were then removed and the process repeated to ensure that the shortest suitable tube was used in each hole. Anyway, by end of day we had all 8 on the engineer's side in place and the first on the fireman's side and have managed to place the shortest tubes.. · With Vince's assistance, Mike finished the tapping for the patch screw on the firebox corner. When I left sparks were flying from inside the firebox as Mike did the final grinding of surfaces inside the firebox ahead of riveting. We are waiting on the return of the air bucker from overhaul and can then set up for the riveting.
· Ed and Richard substantially completed the pipe runs along the boiler sides and started work on the cab pipe work. · During the last couple of weeks Kevin has done more needle chipping to prepare for painting both on 1630 and on the planer. Elsewhere: · Bob continued work on wiring the control system for the planer; and · Dennis finished building up the grease keep for the truck axle box on 428. So next week we target fitting of the remaining flues and then we can set up to roll them into place. Nigel Sunday, March 24. 2013
Steam Department Update 03-23-2013 Posted by Nigel Bennett
in Steam Department at
10:18
Comments (7) Steam Department Update 03-23-2013Not too much visible progress in the steam shop this weekend but actually a good deal that is not very apparent. On 1630 · The first two super heater flues are now loaded. This involved identifying and learning how best to use a whole array of new equipment.
o Jason successfully expanded ferrules into all 16 holes in the rear tube sheet last Sunday. These were chosen from two alternate thicknesses to provide a close fit on the flue as it is inserted from the front of the boiler. o For the large flues the loading process is, of necessity, more complex. Ferrules will be fitted in the front sheet only where the hole is enlarged beyond 5 1/2 inches in diameter. From measurements made yesterday this will be 10 of the 16 flues. o Fitting the front ferrule is very much part of the loading process. Given the size and weight of a 5 1/2 inch tube 17 feet in length, there is no possibility of expanding the ferrule into the sheet in a way that would allow the flue to passed thru the ferrule without displacing it. So the flue must be passed thru the front sheet, into the back sheet and pushed several inches beyond its final position into the boiler, clear of the front tube sheet. The ferrule can then be fitted and the flue drawn back into the front sheet. So fitting the front ferrules is an integral part of loading the flues. o Initial progress was slow as the ferrules must be expanded to the absolute limit of our largest rollers, which meant that they were not very secure. During the day we made a spacing ring that overcomes the problem so, based upon experience with the two now in place, we believe the rest should be much quicker. · Jane continued priming the inside of the cladding sheets so that these will all be ready to install over the lagging. She has now completed the batch we have in the shop so we will need to store these again and get another batch for cleaning and painting. The cladding will not look good at this stage as the outer face will not be prepared and painted until it is in place. However, priming the inside where it is subject to heat and damp from the lagging, is essential to preserve the sheet on the locomotive. · Eric and his Dad worked from pictures of the backhead, that we took before stripping, to locate all the valves and controls, lay them out in the machine shop and start work on servicing, cleaning and painting them. · Dennis weld filled the hole for the one patch screw that must be replaced. Mike and Tom then produced a guide and started to drill out the hole for threading. · Dennis weld repaired the two super heater elements that failed under pressure test last Fall. (Actually Dennis did this a couple of weeks ago and Nigel did not notice !!). Anyway, these are now ready for hydro testing once we get above freezing outside.
On 428 · The first of the two guides for machining the shoes and wedges was competed and Tom is starting to finish the ends of the cast iron shows on the shaper. The second, which will enable the machining of the angle on the wedges is approaching completion. · Dennis was brazing the grease cellars for the truck axle boxes. In other areas: · We moved the turret covers for #265 up on to the top of the locomotive. Time is moving on and the museum opens to visitors soon. We would be deeply unpopular with Buildings and Grounds if large lumps of metal are in the walkways of barn #9 as opening day approaches ! · We had hoped to get some tubes for the Shay out of the boxcar but investigation proved that this can only be done with fork lift access to the car as other heavy material must be moved to get at the tubes. (For efficiency we want to swage the Shay tubes when we do a few extra required for 1630. It takes several hours to set up and test the swager so we want to do a full batch rather than 5 tubes when we do so). However, we will now need assistance to shunt the KCS tender and re-spot the boxcars before we can do this. · Glenn and Richard worked on the safety covers for the new compressor. · Glenn assisted the track department in trying to start their crane. Unfortunately this proved "non trivial" as it seems the fuel lines are blocked. So it did not start today. · Jeff was finalizing the air supply in the new shop. - Yes this is Jeff. The extent of the hair cut led many to question if we had a new volunteer this weekend !. Most of the new outlets are now in place. These are all being structured with a drain on each down pipe to avoid water carry over. · Bob carried on from last week, positioning the planer. It is now not only in position but pretty much level. So a good day's progress and hopefully we are now set up to move forward quickly next weekend. Nigel |
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Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...