Monday, June 22. 2009
Weekend Track Report - June 20/ 21 Posted by Adam Robillard
in Track Department at
00:01
Comment (1) Weekend Track Report - June 20/ 21
The heat this weekend reminded me just how much I like early spring and
late fall... anything over 65 degrees is just too hot. But the high
humidity Saturday didn't stop us from working. The gang this weekend
was Tom H, Steph J, Steve L, myself and special guests JD Marzec, Greg
Frech both from the steam shop and John from the carshop who was
attending for regular membership. As advertised, most of us arrived on
time and prepped for a trip to Four Mile Siding to replace the
switchpoint on the turnout side of the new power switch. We split into
two groups to start out. Steve, Steph and John got the J580 A8
Motorcar, Welding cart and hydraulic cart switched out of Barn 2 while
Tom, JD and Greg got the Model 50 Burro, CNW flat and EJ&E 529
caboose together in Yard 11. I ran around gathering fuel, water and
ice and got the forklift out to load the new switch point onto the
flatcar.
We made it out to Four Mile and were joined by Julie J and Bob O from the signal dept to replace the point. We made quick work out of the job and had the new rods on, including the 'new' #2 rod within an hour. It seems this point is indeed correct and will work fine. We made the slow trek back to the property a bit after 1PM and had everything put away around 2PM. I'm glad to report that all of our machines worked very well and the only thing that required a jump start was the forklift...sigh The rest of the day we spent mostly in Yard 11 cleaning off the C&NW flatcar and continuing to load our scrap gondola. The old switchpoint was set up near B&G for Volkmann. JD was able to cut frog bolts with our oxy/ acetelyne torch making quick work out of that. Everyone did a very good job and I appreciate all of the help. I think everyone had an enjoyable day but I've been known to be wrong.. Sunday was only slightly lower key. Tom, Steph and I made up the Track Dept while Steve L spent the day helping the Electric car shop in Barn 4. The goal was to cut brush near Karsten's crossing with the Amtrak brushcutter before operations got underway. Tom and Steph arrived on time and got the machine out and on the rail early. After the Electric car shop finished testing of the overhead on the main it was our turn to get on the line. I showed up just as they were finishing up the first section of cutting and just as the machine developed an air leak... An old air line under the machine came loose from its fitting which put us out of service on the main until we could come up with a fix. An hour or so later, after numerous trips to the property and failed attempts at a repair we ended up changing the entire hose. We got ourselves back in service and cleared the mainline for revenue service shortly after. There is still a little bit of cutting left to do near Karsten's but the worst area has been taken care of. It was a warm weekend and proved how important it is to carry water with us on the line. We have a cooler in Barn 2, lets remember to keep it full. In the next few weeks we will need to take care of some housekeeping chores. The fire inspector will be coming soon and we have a list of things to clean up ASAP. All of the plastic hanging from the ceiling in Tk24 will need to come down and the aisles need to be clear. Until next time... Adam Robillard Roadmaster lzeje657@msn.com Sunday, March 29. 2009Weekend Track Dept UpdatesSaturday Report by Frank DeVries: Tom, Adam, and myself made up the crew. I arrived early and resolved an air leak problem in the mower, I found one of the air lines had gotten out of place and rubbed against the drive shaft. I replaced two hoses with a quick trip to Napa, and pulled them up into the cab and had the machine running again. While at NAPA, I also retrieved the hydraulic filter for the same machine. Tom and Adam were out next. Tom took the mower to get fueled, and was back on the main to finish mowing. Adam went to barn 2 to finish draining the fuel out of the 585.I continued to work on bolts to remove the two failed motors off the Jackson 6000 tamper, but decided north winds and 33 degrees, this was a job better left for another day. Off to the barn. After Adam drained the fuel and re-filled the tank with fresh gas, Adam and I tackled the leaking brake calipers on the 585. We jacked and cribbed the front of the car to allow access to the underside. Since the bolts didn't want to budge, we employed the blue wrench and quickly had the old calipers off the car. In short order we had the new calipers on, and bled, and tested. This car should stop on a dime, and give nine cents change. About this time, Tom was coming back to the property, having finished mowing the main. After a minor derailment, we had the mower put away. That machine will need to be greased again after it's winter workout. After lunch, Adam got the fork lift out to sort material back by yard 10/11. Tom and I switched out 24 track to get the tamper and tie crane first out. Monday Wes and Warren Lloyd are going to again do the track department a huge favor and go retrieve the engine for the tamper. If they have time, and the snow isn't too high against the door, they will once again put this engine back on the frame of the tamper. Hopefully Fischbach has it right this time. Next weekend we will have to get this baby out and break her in. After the switch move, it was back to the 585 to get the engine running again. I left our heroes improvising a new rubber fuel line to the fuel pump. I'll run to Napa next time and get some replacement 1/2" ID fuel hose to complete that job. Frank D. ------------------------------------ Sunday's Report by myself: Today started out kinda dreary; snow on the ground, drizzle and lots of clouds. Today's gang was myself, Tom H, and Frank D. Frank got out first and replaced a fuel line on the EJ&E 585 taking care of a small fuel leak. I joined shortly afterward and we headed to the Model 50 burro crane in Yard 10. Our goal was to test the recently repaired transmission and decided to dig two cars out of Yard 13. We needed the C&NW flatcar for Four Mile Siding and the gondola for scrap loading. With Frank as the operator we found out just how much the crane can haul. We were able to move 1 load and 5 empties at once... Not bad for a smaller crane. Playing it safe we cleaned out Yard 13 and moved everything to Yard 14 in three car cuts. We got our two cars and brought them over to Yard 11. We expected to take the entire day digging out the cars in Yard 13 but in fact we were done a lot sooner than planned. By the time Tom arrived we were finished and decided to head back out to Yard 13 to start shuffling track panels around to build Track 134. We used the Burro crane to dig out all of the 100-25lb panels and set them roughly in place. We got six set in place and there are four more 100lb panels to set. One at the bottom of a stack in Yd13, two are on the Rock Island flatcar and one is on the connector track under the switch timbers. Those four should put us within a few rails of the end of track. Yard 13 is clear so we can come in with the rail saw and drill and crop the panels together. Complete, this will add about 600' of storage space to the yard. Frank did a great job on the crane today and the machine didn't have any failures to report.As soon as Barn 11 is ready for us to work in, we will. Within the next few weeks we'll try and get the three 112lb track panels to Four Mile Siding and set in place, just as we did in Yard 13. By the time we left the sun was out in full force without a cloud in sight with temps in the mid 40's. The property was almost entire void of other life, but it was well worth the trip out. Check out the rest of my photos from the day in my Member's Album: http://www.irm.org/gallery/album144 Adam RobillardRoadmaster lzeje657@msn.com Monday, March 23. 2009Recent Track Dept UpdatesMarch 13-14, 2009 Last Saturday's gang was Tom, Frank, Steve and myself. The original goal for the weekend was to get the mainline walked and inspected for defects and Tom continue to brush cut on the main. Frank and I ended up getting out early and spent the entire day walking from MP0 to MP 4.8 marking defects along the way. We came up with 3 full pages of issues to correct, mostly loose bolts and missing washers, but a few other important defects like sink holes near 4 culverts... A day of repairs will be necessary very soon, but for now the line is open to 40MPH without any speed restrictions. Tom spent all day on the mower cutting brush from Seeman Rd to Four Mile Siding. He made huge progress cutting areas with very heavy brush. The improvement is very noticeable. Our third gang, Steve, worked on property all day. He worked all day getting the EJ&E 580 motorcar cleaned up and running, which he ended up getting started later in the evening. It hasn't run in years. Before we got the EJ&E 585 motorcar this was Frank's project. The 585 sidelined this project and has sat dormant since. We now have two A-8C Motorcars operable for the first time. Way to go Steve!Sunday was Frank, Steve and myself. We hit the main early with the EJ&E 585 motorcar, hydraulic power cart and tie crane and headed to Four Mile Siding. Frank ran the crane prepping the siding extension for three track panels... This involved picking up about 50 ties laid out and clearing the area for weeds. In the meantime, Steve and I drilled two bolt holes at the end of a rail that had never been drilled on the siding. We now have bolts in both rails and the joint put back together. There is no reason Four Mile can't hold revenue trains now. We greased the new power switch at Four Mile, and continued greasing all of the spring switches as we headed back to the property for lunch. After a trip to pizza, I headed back out on the main with a bucket of switch grease and hit all of the spring and power switches on the mainline and station areas. Frank and Steve headed toward the 580 and worked on the brakes. Saturday the 580 ran, and Sunday the 580 stopped! The brakes hadn't worked correctly for years, and now it runs and stops. The only issue holding up a test run is that it's buried behind about a million freight cars and engines in yard 10 - 100 track. Until the diesel guys get a large loco running to move everything it'll hang in limbo. Again kudos to Steve and Frank for the work! -------------- March 21-22, 2009 This weekend we had a different focus. Saturday we picked up the transmission filter for the Model 50 Burro crane from NAPA we had previously ordered. Getting that and a complete set of filters for the 6000 filters set up the day's tasks. Frank was out with Trackbolt (Frank's daughter Emily) and Tom was out with Tyler. Frank and Emily did wonders getting oil changed and filters replaced on the 6000 while Tom and Tyler did a great job cutting the mainline. By dark Tom had the entire line cut from one end to the other! Only a few chainsaw jobs left and we are 100% done with brushcutting. As promised, the line is tree free by regular ops next month. Tyler and Emily helped me top off the transmission fluid in the Model 50 burro and we tested it out with much success. A few hickups, but it seems with the proper amount of ATF and a clean filter the crane hauls very well. We tested it by moving cars around Yd 11. The diesel guys had a bunch of trucks that needed to be rolled into storage at Yard 13... Long story short, 3 axle trucks don't roll well through streetcar curves.... We assisted by re railing those trucks about 10 times in a span of 3 hours... We had one set of trucks tucked away and another set half way to it's storage spot when the main radiator coolant line on the 50 Burro blew apart leaving the crane paralyzed with a passenger truck hanging from the hook.. This was around 9PM and we called it a day until we got parts due to lack of options to lower the trucks... Sunday Tom and I made it out mid-afternoon armed with 5 gallons of antifreeze and a new hose. By the time I showed up Tom had the new hose installed and antifreeze topped off and we fired up the crane. We finished re railing the passenger truck with the crane and Tom hooked it up to the Jeep with a chain to drag it into it's storage spot a few rail lengths down. It was a sight to see and got the job done without any more derailments or broken windshields...thank goodness. The rest of the day was moving equipment around for the next project and getting the Burro Crane put away. Thank you everyone for all the hard work so far this year. Soon we'll wind down the machine maintenance and focus more on projects. Coming up soon we are going to try to get Four Mile Siding extended another 150', repair defects on the main and prep machines for tamping and tie work. Machines that still need a fair amount of work is the Jackson 6000 tamper and the Model 30 Burro crane (X-17). We are out nearly every Saturday and help will be appreciated more and more as we get into the operating season. Let me know if you can join in the fun! Adam Robillard Roadmaster lzeje657@msn.com |
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Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]