It was a crazy week in the steam department. Passing the hydro test last weekend opened up
a mass of new work on 1630, while the 60th anniversary event provided a great
opportunity to operate as well as many demands for moving equipment in
preparation. Luckily Brian Davies has
been visiting from Florida so we have had steam department capability on site
every day.
On 1630 many tasks are now under way and the critical ones
have been progressing quite rapidly:
·
After the hydro test, the dome cover was removed,.
the water was drained and the boiler ventilated. This enabled the second important FRA
inspection. When a boiler has been
subject to excess pressure (such as the 125% operating required for the hydro)
it must be internally inspected to assure that it has suffered no ill effects,
such as loosened braces. By Friday it
was dry and the inspection was undertaken when the inspector was on site to
check Leviathan. Everything was as it
should be. So we are now cleared to move
forward to steam test. One key thing to
note is that you will see reference to pressure or hydro testing in the next
couple of weeks as we finish beading the tube ends. From here on it will always be at no more
than the 180 psi operating pressure and just to ensure that we have not created
any seepage at the tube ends. We have
proved the basic integrity of the boiler and it must not be over pressured,
else we would need to do a further internal inspection.
·
During the week, Jerry had re-installed the
support bars and grates on the engineer's side so she now has a complete and
operating grate system again. Yours
truly comes in on Friday and wonders why we now have air pipes snaking up the
cab steps and thru the cab instead of neatly thru the ash pan as they were
before. (Because the grates normally
separate the ash pan from the firebox dummy !)
·
The dome lid was replaced on Saturday to enable
testing of tubes as they are beaded.
Unfortunately some work is required on the throttle body so that could
not be refitted and the lid will need to come off at a later point to refit
this.
·
Jane was hard at work painting parts ready for
installation. All the bands that will
hold the cladding sheets in place are now done.
Now if only we can get her the paint for the air tanks we can get those
fitted again !.
·
Beading the tube ends has proceeded well. As
shown later, beading requires the 1/4 inch projection of the tube to be rolled
over tightly against the sheet. In the
front not all the tubes are beaded. The
super heater flues and the small tubes beside and immediately below them are
beaded to provide additional longitudinal bracing to the tube sheets. In the rear, everything is beaded to protect
the seam between tube and tube sheet from the direct flame burn.
Progress was maybe not quite as fast
as we had hoped but the weather conspired against us !. Brian Davies has done most of the work but
has now trained Brian Krause in the technique, which makes describing who did
what complicated !!.
During the week Brian D beaded all
the required tubes in the front tube sheet.
On a couple of evening he apologized for not moving as fast as he had
hoped. When I worked in the shop Friday
I fully understood. At 90+ degrees and
high humidity, doing anything physical was tough. How he did as much as he did I can barely
imagine.
In the picture above you can see
the distinction between the tubes higher up, that have a smooth rounded profile
overlapping the seam between tube and tube sheet, and those lower down, where
the tube is simply expanded into place.
This is the effect of beading.
On Saturday and Sunday Brian K
worked on the firebox tubes during breaks from the 60th anniversary
operation. On Sunday I observed the
process and took the photographs below.
At the start, the end of the tube
is expanded into the sheet and, if necessary, reduced to a projection of 1/4
inch. The specially shaped tool in the
air hammer has a small extension outside the tube and a longer one inside.
Having started to
hammer the edge of the tube is rolled outward.
Working steadily
around the whole circumference of the tube, Brian forms the rounded profile all
around the tube end.
A little tidying up
to ensure it is smooth all around, the rolled edge is tight against the tube
sheet and another one is done.
·
The other major piece of work now under way is
lagging the firebox in the cab. This
apparently simple task is going to be a censored nightmare !. First blocks of insulation have to be secured
all over the surface of the firebox.
This varies from fairly large intact blocks on the lower sides, thru
pieces that have to be laboriously cut to fit around stay caps higher on the
sides to irregularly cut pieces, that will need to be squeezed into narrow
spaces between fittings and pipes, high up on the top. The material is an unpleasant mix of fiber
and silicates that is very brittle when cut.
So getting it located and intact is a most unpleasant challenge. Once areas are in place we then have the fun
of squeezing pieces of sheet metal between the pipes and into a position where
they can be secured. This will have to
be done as soon as possible since the exposed blocks of carefully located
insulation are very fragile and will tend to break up on contact until they are
covered.
Bob Milhaupt, who was a regular
volunteer until he moved to Michigan, visited for the weekend and worked
steadily at this job. By Sunday the insulation
was in place well up both sides of the firebox.
Dennis repaired one of the cladding sheets that had to be cut to remove
it so we have the metal ready to install as soon as we can cover the top of the
firebox.
·
Another activity related to the lagging was
identifying the route of some pipes that have been disconnected or replaced so
that we are sure they are in the correct place before lagging is put over them.
·
On Saturday the firebox door casting was lifted
out of the tender so that work could begin on preparing this for fitting. Rick managed to safely remove a couple of
badly burned bolts that secure the distribution plate and all the loose fire
clay. David made good progress in
removing accumulated rust in preparation for repainting. Once the beading is complete in the firebox
this casting can be re-installed. (You
can still get into the firebox with the door casting in place but it will be a
LOT more difficult).
·
Another major stream of work started with Jeff
bringing in from the boxcar the various pieces of sheet metal and mesh that
form the table plate and spark arrestor around the blast pipe in the
smokebox. As you may imagine this is a
harsh environment so the whole construction needs to be assessed to determine
which pieces can be reused and which replaced.
So Dennis needs to start on this to ensure that we have it ready once
the blast pipe is installed.
In other areas
within the shop:
·
Phil and Cameron
worked with Tom on machining the bolster for the Shay;
·
Tom continued
machining shoes for the axle boxes on 428.
There was a lot of
work outside in support of the 60th anniversary:
·
3007 and the
Centennial were moved out of barn 9 for display. This is a very time consuming exercise as a
lot of equipment that does not move often had to be moved to enable this. A number of people were involved in
lubricating the equipment so that it could be safely moved and then assisting
in the switching. When you move pieces
that are normally static great care is required as stiffness may make them much
more prone to derailment.
·
It was great to see
steam in operation with both 126 and Leviathan on site. While Leviathan was fully crewed, the
department provided crews for 126 thru the weekend. This was a great opportunity to get some
operating experience ahead of 1630 coming into service. I thoroughly enjoyed a short spell firing
126. However, when spreading a few part
shovels of coal around her firebox, you became rather aware that the box on
1630, that you had just crawled out of, will present some rather different
challenges !.
·
We observed the FRA
inspection of Leviathan on Friday which was useful as it confirmed what the
inspectors will want to see in the steam testing of 1630.
·
On Friday, 126
provided a chastening example of the exposures in operating a steam
engine. The piston rod worked loose and
detached from the crosshead when switching.
This allowed the piston to be fired forward, smashing the front cylinder
head casting. Luckily Barney had a spare
on another locomotive in process of restoration so, with lot of driving over
night to fetch it from Indiana, she was repaired and back in service on
Saturday. But it certainly highlights
how easily major damage can occur to a steam engine. Repairing something similar on 1630 would be
huge.
So a lot of progress. Much more must happen to enable the steam
test but the objective is now in sight.
Nigel