There is nothing like hunkering down for a big Winter storm
to create time to update the blog!.
There was a very good turnout at the steam shop yesterday (and I suspect
a nil turnout today judging by the white out that can be seen on the
webcams!!). As we reach the end of January
a lot has been done in the steam shop so far this Winter ….. and there remains
a lot to be done before May!.
Obviously the absolute priority is #1630 and getting her
ready for the new season. While she was
out of service the critical focus was on rebuilding the axle boxes on the
trailing axle and the 15 year boiler inspection. Known or suspected issues were addressed
during this time but we did not do a complete “tear-down” of areas that were
within tolerances and had given no indication of problems.
So, for some years to come our Winter program will include
the annual maintenance items and a program of inspection and remediation where
required of some other areas each year.
The annual inspection work has progressed steadily. This is essentially in four stages:
Work in preparation for hydrostatic testing;
Hydrostatic testing;
Internal inspection after hydro testing; and
Testing under steam.
The large majority of the inspection work is now done. Among other task:
annual
check of all the tell-tale holes in the stay bolts is now complete (sounds
simple until you realize just how many of the darn things there are!). Jerry has made major progress developing a
technique with small cutting heads on a Dremel tool that has proved very
effective at removing obstructions from the tell-tale holes;
drawbar
was removed and inspected along with the pins that secure locomotive to tender;
gauge
glasses and water column have all been removed, cleaned or replaced and then
refitted;
main
and auxiliary air reservoirs have been removed, hammer and hydro tested then
refitted. This weekend the ES air tank
was repainted and complete. One of the nuisance
items is that the inevitable damage to paintwork when removing and testing
means the tanks must be repainted every year;
arch
tubes have been thickness tested;
wash
out plugs have all been removed, inspected and, this weekend, refitted.
We now have to test the gauges and finish checking of the
arch tubes and we will be ready to carry out the hydrostatic test when the
weather permits.
The other areas where major work is taking place this
Winter include:
The
rods of number 4 and 5 axles where some knocking was detected during the
running season;
Couplers
where some issues were apparent with smooth coupling and releasing;
Flexible
stays below the footplate, which were due for periodic inspection;
The
air filter system which needs regular cleaning but is mounted in such a way as
to make this extremely difficult;
Replacement
of the steam feed line to the air compressor which was found to be
significantly corroded;
Work
is being done to make the mechanical stoker operational although this is not
targeted for 2015 completion.
In
the normal way when dealing with and elderly steam locomotive none of these has
proved as simple as initially hoped!.
The rods between #4 and #5 axles have been removed and the
dimensions carefully checked. The clear
issue is excess wear in the FS #5 rod bearing.
Material has been obtained and a new brass bearing will be machined and fitted
to the rod. The other peculiarity is the
disk that sits behind the securing nut and forms the outer face of the ES #5
rod bearing. The peculiarity is that it
differs from the other similar disks and bears the number of a long gone Frisco
mikado!. It is suspected that the
difference can lead to steel on steel contact where the original pattern would
always bear brass on brass. It may be
that this was why this bearing was always the one that had a tendency to run
warm. Dennis can add brass that will
then be machined to match the original #1630 parts.
This
shows the stock ready for machining the new rod bearing and, on the bench
behind this, the disk that will be built up then machined to better match the
original #1630 pattern.
An
intensive inspection of the couplers has indicated no cracking of any of the
large parts but some damaged internal parts that go a long way to explaining
tricky operation. The good thing is that
these are standard couplers so spares should not be an issue. The trouble is that removing the couplers has
led to detection of more work needed on the draw gear.
Under
the tender significant wear was found in the mechanism that provides “shock
absorption” when backing onto or pushing a train. While not an immediate concern with the
weight of trains handled at IRM, it was decided to give this area a thorough
overhaul.
The
following pictures show the work involved in detail
This is what you are used to seeing
Behind this, under the tender, the coupler is backed by
this assembly. The coupler is attached
to the cage assembly by a substantial pin that is inserted or removed from
below and held in place by the bolt that can be seen at center in this picture.
Looking further back (actually toward the front of the
tender) you can see the cage and, substantially hidden above it, the outer edges
of the shock absorber.
First the bolt is removed, the pin dropped and this allows
the coupler to be removed. Here you can
see the hole thru which the pin fits to secure the coupler to the drawgear. The pin is actually a substantial rectangular
block with rounded ends.
Having removed and separated the cage and shock absorber the
empty cage clearly shows how the pin secures this to the coupler.
And
here we have the “problem child”. The
heavy frame of the shock absorber still has the massive springs in the wider
part of the casting. Information
suggests that these huge springs are compressed about an inch when fitted and
you do not touch these without special equipment!. The empty end of the casting is the location
of the smaller springs that were removed in many pieces.
Dennis
will build up the mountings under the tender where there is significant
wear. Meanwhile there is a lot of
discussion on how to deal with the shock absorber. The original unit has two groups of springs,
one fairly substantial and one VERY large.
The clear intent seems to be that the smaller ones provide an initial
softening of the impact while the big ones take the load after these are
compressed. In our case, the smaller
springs were smashed to pieces and clearly had been for a long time. Two avenues are being investigated for
repairs. A source has been identified
that could produce replacement for the broken springs while the original
manufacturer is still in business and does produce modern equivalent units that
are still used in freight cars (as those fitted to #1630 were in 1920). Initial feedback from the spring supplier is
interesting, suggesting that the (1918) design is defective as the smaller
springs would have a very short life and be likely to fracture pretty quickly
in exactly the way that had happened on #1630!.
We have no idea if the design was changed but it does suggest that, if a
modern equivalent can be installed without major modification to the tender,
this would be the best solution.
The
flexible stays hidden under the footplate behind the stoker riser have all been
inspected cleaned and recapped. A good
deal of rust damage was found in the footplate supports. It is interesting that much of the corrosion
stems from modifications made to fit the stoker, probably in the late
1930’s. The center of the cab floor has
to be raised to provide space for the coal delivery to the stoker. To provide a level floor to the cab raised
sections were installed on both sides of the cab sitting on top of the original
floor to provide a surface about 3 inches higher. This created a double skin in which a lot of
corrosion has occurred. Much of this has
been repaired and the remaining action will be to rebuild the center section
around the stoker delivery pipes. This
places a lot of pressure on getting the hydro done as soon as possible. We do not want to re-install the stoker
delivery pipes until we are satisfied that the flexi caps have passed hydro testing. But we have a lot of work on rebuilding the
cab floor that requires these pipes to be back in place!.
After
a great deal of work this weekend the area under the ES footplate is clean and
partly reassembled. Here you can see the
fabrication that sits below the grate shakers and converts the rotation of the
shafts in the cab floor to a back and fore movement of rods attached to the grates.
The
air filter site behind the compressor under the smokebox and on top of the main
frame. It is basically a large cartridge
filter where you release a bolt securing the housing, drop the housing and
cartridge, then re-install with a new or cleaned cartridge. Simple!, except that it was mounted so that
the housing has insufficient space above the main frame to allow it to be
dropped. We know that 2 years ago we did
manage to get it off but this year a large number of us in 4 hours work could
not find a way of doing so. Eventually
we decided to cut the bar on which it is mounted and modify it to have bolts
that can be released to remove the whole filter. Interesting. When cutting the bar it was apparent that we
were following the line of a previous cut and weld. So it seems that this is not a new problem!.
The
stoker motor is now in the shop awaiting attention when essential work for this
season has been done. Last weekend a few
of us opened the cylinders, applied lots of oil and then tried turning it with
substantial bars. Actually, while it
took a good deal of effort to get initial movement, once it started to move and
oil spread on the bores and rings, it now moves very smoothly and easily.
As time permits some work continues on the other projects.
On the Shay,
Collin worked on lapping the valves on the
turret. It was lucky that this was
started now!. On close examination of
the valve heads during lapping cracks were discovered. It looks very much as if some clever person,
finding that the valves did not close to their satisfaction, tried to get a
better seal by using a pipe wrench on the valve stems!!. New valve heads are required but at least we
have the drawings and the material has been ordered for machining.
Phil has made considerable progress applying and enhancing
the technique that Jerry developed on #1630 for clearing blocked
tell-tales. Thru his efforts a
substantial number of stays previously assessed as requiring replacement (due
to inability to achieve the minimum length of tell-tale) have been cleared well
beyond the required length. The plan is
now to work on this over the next few weeks and then assess what stays there
are that are still not clear to the required depth and must therefore be viewed
as broken. The critical factor will be
whether we can avoid removing the motor (and potentially lifting the
boiler). Wish us luck!.
On #428
Stu and his team have started riveting the
cab. In two Saturdays they have set
about 30 rivets replacing the temporary bolts that have been holding the cab
together since the new plate work was fitted.
Once the cab is riveted (and the new footplate floor fitted) it will be
possible to replace the cab on the locomotive.
Dennis has put in a lot of work building up parts of the
brake and spring rigging as well as the axle box keeps to make good years of
wear. These will now be machined to
bring them back to original dimensions.
Many new parts are being machined. These are new pins for the rigging.
So. A lot of progress has been made but there remains
a lot to be done to ensure that #1630 is ready for running in May. We will be hard at work each weekend and some
weekdays. We are always looking for new
people willing to get their hands dirty!.
Let’s
hope we do not get many storms like the one today. I suspect that it will be a couple of days
before it is practical to get back to Union!.
Nigel