Unfortunately not the update that I was hoping to be able
to write 24 hours ago!.
The steam team has worked steadily thru a record cold
February and made good progress, primarily on the Winter work on 1630. The work on the boiler was completed and the objective
is to carry out an initial hydro test as soon as possible to ensure that
nothing leaks on the backhead where it would be hidden by the refitting of the
stoker and footplate. We really need
some above freezing temperatures to safely run the heater that brings the water
up to a suitable temperature for the pressure test. This has held us up for a week or so but the
forecast suggests a “warm” day Tuesday so everything was planned. The tender was filled last weekend to allow
the water to reach at least shop temperature.
On Saturday the pipework was set up and a start made on filling the
boiler.
Unfortunately this revealed that one stay seems to have
broken during the process of clearing the tell-tale hole. A steady stream of water was apparent as we
filled the boiler. With this stay
plugged, we were able to fill the boiler and prove that this is the only stay
in this condition. However, we now have
a stay to replace. This was something
that was not in the plan.
By end of day, Dennis had cut out the cab floor under the
engineer’s area, the end of the stay in the firebox was ground flush and the
stay cap had been removed. This proved
rather reluctant and took a couple of attempts, otherwise we might have got the
stay out. Anyway, we are now ready to
remove it next week.
Replacing a flexible stay is something we did several times
during the overhaul and can be done in a couple of weeks, provided we do not
hit anything abnormal. However, it is
additional work and means that the target of running Memorial weekend is now in
some danger.
In parallel with the boiler work a lot of other work has
progressed.
Dennis has put in many hours
of work building up the yolk and other parts of the tender draw gear support
mechanism. We should be receiving a rebuilt
draw gear unit shortly and then the work can begin on making any modifications
required to fit this under the tender.
A new pin has been machined
for the front coupler pocket. The
original was heavily worn. Once new
bushes are machined and the support plate, that Dennis has rebuilt, is in place
we should have a coupler that sits horizontal rather than sagging as it has in recent
years!.
The air tanks are now
refitted. This has been a big job as we
have fitted new Teflon seals to the ball joints of the tanks. It sounds simple but replacing the very worn
seals that have been there for many years can slightly alter the fit of the
pipes. There is very little flexibility
in large diameter steel pipes!. So in
some cases we have had to cut and rethread the pipes to make the correct fit.
The new bush for the
connecting rod is now complete and in place in the rod.
Dennis built up the brass on
the securing disk. (My mistake. I said last month that the odd one came from
a Mikado. Actually it is from a
consolidation). Once that is machined we
will have all the parts to reassemble the running gear.
However, the first steps at
refitting suggest that, with the new bearing in place, clearance will be very
tight and it may be necessary to remove and adjust the axle box shoes. Measurements that Jason has made indicate
that the shoes are marginally thick and will need to be adjusted at some
point. It may be that point is now!.
Work has been proceeding on
the replacement of the gland packing on the air operated power reverser
mechanism.
After a lot of effort the
broken bolt in the smokebox front ring was successfully removed and a new one
is in process of being fitted. John Heid
joined us and was rapidly at work on this.
When the work on 1630 has relied more on welding and
machining, people have been able to do some work in other areas.
Progress has accelerated on the Shay.
The big determinant of how
quickly the Shay can be brought into service is whether we can clear the
tell-tale holes on all stays behind the frames and motor brackets from inside
the firebox. If all the tell-tales can
be cleared to the required depth, we then need just to replace a number of
stays in other areas that have been identified as bad and can then move quickly
to re-tubing the boiler. If any stays
need to be replaced behind the motor bracket, then we have a substantial
project to remove and refit the motor in order to replace them.
Several people have been
working on this as time permits but Phil is now working on the stays 3 days
each week and making good progress. A
lot of stays have been cleared so far.
We all wait with bated breath to see if any prove beyond clearance in
the critical areas. We should know
within weeks now if we can avoid removing the motor.
Various work has been
progressed to allow reassembly to move forward if the stay work is successful.
JD has been locating and
preparing the various parts of the running boards.
Brian removed the equalizer
air tank and cleaned it in preparation for hammer and hydro testing.
(Brian’s comment on this
photograph was very fair!. “You could at
least have taken a before shot to show just how much muck I had to remove”). Located under the cab floor, behind the
engineer’s footstep this tank gets buried is everything thrown up by the
wheels. Good job Brian!.
On 428
The riveting team, led by
Stu, has put in several days on the cab.
There are a LARGE number of small rivets to be placed but they are
progressing and the number of temporary bolts showing on the cab is steadily
reducing.
Once it is at temperature
the rivet is struck on the anvil to dislodge any scale and then put into the
hole.
The bucker holds the head of
the rivet in position as Stu uses the air hammer to form the other end of the
rivet inside the cab.
Although the basic method is
the same, these are far smaller rivets than we had to use on 1630. Rather than fighting to ensure that the rivet
is formed while still malleable, the risk with these is more that they can
easily be over hammered and have unsightly deformed heads.
The process of Dennis
building up with weld and Eric then machining to final dimensions has proceeded
steadily thru the many components of the spring rigging. With this now largely complete, work has now
started on machining the valve rods.
Mike returned this week
after being out of state for some weeks and work restarted on the planer in
preparation for the axle box work.
So
March looks to be a busy and critical month.
Wish us luck!. And if you fancy
getting your hands dirty ………!!