March was a month of great activity in the steam shop. Recovering from the set back at the end of
February we have made great progress in preparation for the operating season.
Obviously the focus in the shop is on #1630. However turnout has been good during the
month and this has allowed substantial work on other projects as well.
Looking first at #1630.
By end of day yesterday she
was ready for the formal hydrostatic test of the boiler which is planned for
next weekend.
The stay that was found to
be broken at the end of February was removed.
The old stay was ground off flush inside the firebox, heated and a large
wrench applied to the domed head in the socket.
It came out smoothly making the rethreading for the new stay relatively
easy.
A new one was machined.
We are getting relatively
practiced at this process. The worst
part of this particular stay was forming the domed end once it had been screwed
into place. The ball end must be bucked
to prevent the stay moving as the end is hammered into shape. This one was a bear to position the bucking
tool and more of the cab floor had to be removed to position the bucker.
Inside the firebox Jason
used the air hammer to form the end of the stay.
The finished result is a
neatly domed head. … and there was never
any leakage under testing.
The weather improved at a
critical time in mid-March so that we could safely run the water heater. So for the last couple of weeks we have been filling
the boiler, heating the water and pressure testing. It is the nature of the beast that that high
pressure water will reveal leaks that do not necessarily happen under steam due
to the different temperature and expansion factors. Also, given that all the plugs and a number
of stay caps have been removed as part of the annual inspection, there are
likely to be points that have not sealed completely. So we have carried out a number of cycles of
filling, pressuring, identifying leak points and then draining, fixing
identified issues and repeating.
A couple of valves (one test
cock and the rail washer) have nuisance leaks that Tom will aim to fix during
the week but otherwise she looked good by end of day.
Subject to success of the
test next weekend, we will then need to remove the hatch, carry out the
internal inspection, and then we can start preparation for the steam test.
As suspected last month, it
did proved necessary to remove the axle box shoes from number 5 axle for
machining. Phil has become our expert at
removing and refitting shoes and wedges.
This is a horrible job, involving working in the confined space under
the firebox with Portapower cylinders to drive the shoes out and then back in
to position.
It is frustrating as they
are not actually attached but just slot into place. However, since they are a fairly close fit on
the frames and between the substantial weights of the frame and axle box, a
good deal of encouragement is required to move them against the adhesion
created by the grease. And this
encouragement is not easy to apply in the very confined spaces under the
locomotive. The absence of an inspection
pit is REALLY noticed in a job like this.
Hopefully this is a development that we can make in the next couple of years.
Anyway, by end of month both
shoes were machined and back in place..
The plan is now to pull the axle forward, refit the rods and then test
fit the wedges. It is not certain yet if
we will need to put shims onto the wedges but the material has been obtained to
do this is necessary.
We have done a good deal
more work than initially planned in this area but this actually covers work
that was tentatively scheduled for next Winter so overall it is a gain and
should result in a significantly smoother running locomotive.
Having proved that the stay
caps on the backhead are all free of leaks, it was possible to stay
reassembling the footplate and great progress was made on that. The major
elements of the stoker delivery system were refitted and most of the footplate
is now re-installed. (No pictures of the
stoker installation as I had to operate the fork-lift)!.
Another major area of work
has been the tender draft gear. As
discussed previously, a lot of damage was found in the spring mechanism of the
draft gear. One big benefit was that it
had been manufactured by Miner Enterprises in Geneva, who still manufacture
such equipment and were extremely helpful in identifying options. After a lot of measuring and comparison it
was agreed that a later pattern could be fitted into the space and Miner very
generously offered a reconditioned unit of the later type in exchange for the
1918 original that will go into their museum.
The new draft gear looks
quite different but has the same essential dimensions. One small anomaly is that it has a projection
caused by the casting process in a place that would foul when installed in #1630. Miner’s advised that it was of no
significance and could be removed …. So it was!.
Dennis has done a lot of
build-up work on the yolk and coupler.
What remains is the weld build
-up of the support brackets under the tender.
Once Dennis can complete this, we will have the “fun” of refitting the
whole assembly under the tender.
The drawbars that link the
locomotive and tender have been annealed and then inspected. A lot of hard work is required to thoroughly
clean the drawbars to allow the inspection for cracks.
Once the footplate is
completed, they are available to reconnect the locomotive to its tender. However, this will likely not be done until
the draft gear is completed as it is difficult
to move the tender accurately until the coupler is back in place.
The reverser cylinder was
finally disassembled. This proved
extremely difficult as it is clearly many years since this was last done and
bolts securing the cylinder end to the cylinder were in very tricky locations
and seriously frozen to their threads.
Snag is that you can repack
/ add additional packing to the piston gland for a long time but eventually you
need to clean the whole gland out and repack.
This year was eventually!. It is
now being reassembled and will hopefully be another “catch up” job that will
not need to be done again for a generation.
Work has accelerated substantially on the Shay.
We have used donated funds
to employee Phil for several days each week primarily to complete work on the
firebox. The result of his efforts,
along with JD and Cody, is that all stays now either have tell-tale holes
cleared to the required depth or have been removed.
The major success from this
work is that all the stays that could not be accessed without motor removal
have been cleared. We can now progress
on the basis that the project will not require removal of the motor. Plans are now being made to fit new stays to
replace those that had to be removed and then to re-tube the boiler this
year. The sequence may look a little
strange as we will likely fit the tubes before rebuilding the smokebox. While you would normally fit the tubes from
within the smokebox, the small diameter of the Shay’s smokebox makes this an
uncomfortable job. So the thinking is to
take advantage of the absence of the smokebox floor and refit the tubes before
it is refitted.
A lot of other work has been
progressing on the Shay.
Air tanks have been hydro
tested;
Interior of the water tank
has been cleaned and prepared for painting;
Work has started on
preparing the timber for the front beam and running boards. Unfortunately the plan of obtaining the
timber for the beam some years back and allowing it to season has not worked
out as intended. One of the timbers
twisted a good deal more than anticipated in the process so we now have some
tricky calculations to determine if it can be trimmed square and still be big
enough for the purpose.
On 428
Ed has worked steadily thru
the refitting of pipework. This has now
moved on from the cab to other areas.
The “riveting team”, led by
Stu, has worked a number of days on the cab and has made substantial progress.
After a lot of effort, Mike
and the team have the planer substantially operational ready for work on the
axle boxes. This has been a huge effort
as it is probably about 50 years since this complex machine last operated. The documentation is not very detailed and a
long period out of use, coupled with uncertainty over any defects it may have
had when last used, make for a few challenges!.
It is now clear just how complex the processes achieved thru the
hydraulics are. The huge table moves
back and forth, travelling slowly on the cutting stroke but substantially
faster on the return. At each end of the
stroke, the movement slows (to avoid a hard stop and reverse). At the end of the cutting stroke, the cutting
heads are tilted upward to clear the work as the table returns. At the end of the return stroke, the
traversing shaft rotates to advance the cutting head for the next cut by an
amount that can be varied by the operator.
Seeing all these actions being carried out smoothly is fascinating and a
number of us spent time watching in awe!.
So wish us luck in April.
We have made good progress but still have plenty to do in order to be
ready to run in May.
Nigel