A very busy month in the steam shop that can best be
described as “so far so good”.
In the last blog I outlined the plan for work on #1630 this
Winter. Thru January we have worked
steadily on this plan. The discovery in
December that the valve chambers were worn to the extent that both need to be
re-bored turned the program for this Winter from one that looked relatively
simple in comparison the last year into one that will be a challenge to
complete for May.
However, we have now completed re-boring the first valve
chamber (engineer’s side), which is a huge step. In this entry, I will describe what has been
involved in getting this far. What we
have found so far does suggest that, once this work is completed she will be substantially
more capable than at any time since she arrived from Eagle Pitcher.
The detailed measurements of the two valve cylinders
revealed a great deal of wear. The valve
moves over a relatively limited proportion of the overall cylinder length (over
and either side of the port openings.
This means that the wear is very uneven over the length of the
bore. In our case the worst area of wear
(on the fireman’s side) was approaching 1/8th inch larger in
diameter than the unworn areas of the same bore. This is well beyond tolerances that would
have been acceptable during overhaul in steam days.
Each valve is a quite complicated assembly. This shows one complete valve just detached from
its rod.
The seal between the valve and the cylinder at each end is
made by two pairs of spring loaded rings.
Each ring is made up of 4 equal segments. Between each pair of rings is a solid iron
bull ring. It is the bull ring that
forms the bearing between the valve and the liners of the valve chamber. When new the clearance between the raised
section of the bull ring and the liner should be 1/32 inch. Not visible when the valve is assembled is
the fact that the bull ring has extensions on either side of the visible
bearing surface and about ½ inch below it.
These form the base of the channels in which the spring rings fit.
At each end of the valve is a cast “spider” which has a
central hole thru which fits the valve rod.
The spider has a machined cylindrical body the end of which fits into
the fabricated valve body. The spring
and bull rings are fitted around the cylindrical body of the spider. When the components are fitted to the valve
rod and the not tightened the bull rings set the spacing between the spider and
the valve body and so set the critical width of the slots in which ride the
spring rings. This is a very significant
dimension as the spring rings must be free to move to maintain the seal but, as
they are prevented from coming out of the valve only by small lips, excessive
play can lead to a ring segment coming free and damaging the cylinder. The machining of new bull rings will be a
careful and accurate exercise!.
The whole valve is assembled on the valve rod. The back of the valve assembly sits against a
ring firmly attached to the rod. When
the rods are separated from the valve, the retaining ring can be clearly seen
When assembled as below the ring is hard against the spider
at the back of the valve.
The various parts of the valve are fitted moving from back
to front and then the other end of the assembly is clamped into place by a nut
threaded onto the front of the valve rod so holding the parts together as a
single assembly. Here you can see the
large castellated nut and cotter that clamps the assembly from the front.
Once the clamping nut is removed
the front spider can be carefully driven away from the valve body. The amount of force needed varies depending
upon the extent to which carbon has built up around the parts. Comparing this view to the previous one, the
spider has moved far enough away from the valve body to open up the slot which
traps the rear pair of spring rings sufficiently to allow the spring and rings
to be removed. At this point the front
pair of rings are still trapped in their slot between the bull ring and the
spider.
Considerably later, the bull
ring has been pulled off the spider releasing the front pair of rings and the
old bull ring is now shown on top of the cast iron that is being prepared for machining
to make the replacement.
With all rings removed the
spider sits on its own and is in process of thorough cleaning to remove all
carbon and allow the new bull ring and spring rings to be assembled onto it.
Similar cleaning is required on the
valve body, here seen with both spiders removed.
Both valves have now been stripped to their components and
cleaning of the valve bodies and spiders is well under way. We have new spring rings of various sizes
that were obtained with the locomotive in the 1970’s. These were made in 1/16th inch
increments between the nominal bore size (12 inch) and the maximum allowable
re-bored size (12 3/8 inch). We do not
have a complete range so the actual size to which we bore the cylinders will be
determined by both what is required to remove the wear and reach a smooth, true
bore and the rings we have available.
The likely size is 12 3/16 as this is both slightly above the worst
measured areas of wear and a size for which we have adequate new rings.
So far the ES valve liners have been bored. First the substantial mounts, that hold the
bearing ion which the boring bar rotates, must be firmly bolted to to each end
of the casting.
Once the mounts are in place,
the boring bar itself must be carefully slide into the mounts. This is a fun exercise!. The bar must be very rigid as the objective
is to hold the cutters so that they maintain accuracy of cut to within
thousands of an inch along it whole length.
This requires a bar of about 3 inch diameter. It took 6 guys to move it along the
shop. So gently positioning and sliding
it into position is no small task!. Just
to make it more fun, the cutter head must be placed over the bar as it is
fitted thru the rear bearing and before the bar can be pushed along the length
of the cylinder.
Success. Here the end of the bar projects thru the
bearing at the other end of the cylinder.
The boring itself is very
difficult to capture. The gears that
allow the cutter to be manually advanced and retracted, then locked to the
screw mechanism to make the cut, have been attached to the shaft at the front.
An air motor then turns the shaft,
with the cutter head attached, while the gears slowly turn a geared shaft
running the length of the boring bar to which the cutter head is geared. In this way the cutter head is advanced a
fraction of an inch at each rotation.
Each cut takes about 30 minutes but it takes at least that long to
accurately adjust the cutter head to required depth for the next cut
Once the actual re-bored size is determined, we can start to
machine the new bull rings. These are
required to be 1/32 under the bore size on their flat surface.
The bull rings and cylinder liners are made of cast iron,
the wear properties of which were found most suitable for this
application. This makes the first stage
of producing replacements unusual. I
suspect that, in steam days, blanks, from which the bull rings would be
machined, were specially cast for the purpose and requiring limited machining
to complete. Nowadays that is not economic on a small scale. Suitable rings are not available so we must
start from a disk. The first step is
therefore to produce the ring, of a suitable size for final machining, by
cutting probably 75% of the total weight of the disk out of the center to
produce a ring. This is a long and
tedious process on the lathe, taking several hours for each ring. Brian has worked at this for several days and
has now produced the 4 rings needed. All
this was accomplished amid a deal of comments from the rest of the team around
him going into the mass production of iron filings!.
In other areas
Works continued on producing the bracing that will allow us
to rivet the smokebox of the Shay.
Good progress has been made on completing the cab of #428 to
the extent that it is now being fitted with windows.
The large compressor for the new air system is now wired and
was recently run in test mode. This was
the first time that this compressor has run under load since it was salvaged
from the Milwaukee Road shops many years ago.
Testing allowed a number of adjustments to be made but also indicated
the need to replace one valve and install an unloading mechanism. This will take a couple of week but then we
should be ready for inspection and commissioning.
Nigel