Another month of steady progress in the steam shop. There is rather less detail this month as I
was away for three weekends visiting family in the UK.
Obviously the central focus is on getting #1630 complete in
time for the start of operations in May.
The regular work for the annual inspection continues in parallel with
the major project of the valve overhaul.
The boiler and other work for the annual inspection is now largely
done. A couple of weeks back, Phil
cleaned and checked the arch tubes. After
that the last of the wash out plugs were re-installed. Yesterday the testing of the pressure gauges
was carried out so these can now be re-installed. The boiler will then have everything in place
for the hydro-test.
We will now schedule this test with the FRA inspector. Once this is done we can conduct the internal
inspection and, subject to any issues detected in testing, plan on steaming.
Obviously one essential part of the annual inspection is
correcting those items that are considered out of or close to allowable
tolerance. In this context, the spring
loaded buffer on the front of the tender is was overhauled and the upper cross
head bearing on the fireman’s side is being re-metaled.
The buffer has been cleaned, spacers made to take up the
slack in the springs and painted.
Yesterday it was re-installed onto the tender.
The tender is now complete and all that remains is to
re-couple it to the locomotive by refitting the main drawbar. This has been removed, thoroughly cleaned and
inspected for any cracks as required for the annual. Recoupling will be done as we prepare for
steaming as this is best done by pulling the tender out of the shop and lifting
the drawbar into place outside, where we have space to use the fork-lift.
A big job completed recently was casting the new Babbitt
bearing for the crosshead. What does
this mean?. Babbitt (alloys of tin or
lead with copper and antimony) has been used for nearly 200 years to create a
bearing surface against steel or iron. A
favorable combination of relative softness, compression resistance and
porosity, which facilitates the distribution of lubrication, mean that it is
widely used for bearing surfaces to this day.
However, while modern usage is usually as a thin layer in a
backing shell of a harder material, the more traditional usage made use of
another property, low melting point. The
metal melts around 400-500 degrees and casts well at 800-900 degrees. It will adhere well to iron or steel that is
treated with a flux but not to a dirty surface.
The principle is then simple. One
iron or steel surface, normally a casting, does not need to be machined and is
over-size versus the shaft or rod that moves against it. Molten Babbitt is then poured into the
over-sized space in which it solidifies to form the bearing surface.
In the most basic form, the bearing is cast in situ. A smoky flame is used to soot the surface against
which the bearing will slide, any gaps thru which the molten metal could escape
are blocked and the molten metal is poured in.
The contraction of the Babbitt as it cools provides a small clearance
and the bearing should be ready to go with no machining necessary.
The bearing that we must replace is that in the top of the
crosshead which bears on the slide bar.
In theory this could be cast in place.
However it was felt to be considerably safer and more accurate to cast
the Babbitt in the crosshead shoe with some excess and then machine it to final
size on the planer.
To do this the shoe, with a tray positioned in the center
to make the “U” shaped channel, forms the mold.
The whole assembly is heated in the furnace so that the Babbitt
remains liquid when it is poured into the mold.
The shoe is tinned to help the Babbitt to adhere while the tray is soot
coated to help it release after cooling.
Once the babbit had completely cooled, the tray was removed,
the crosshead shoe was mounted onto the planer and Tom has started machining
the babbit to its final dimensions.
Meanwhile the valve overhaul has progressed well.
Both valve chambers are now bored to size and the boring rig
has been removed.
The valve rods were sent out to a specialist for surfacing
to remove areas of wear that form over time as they run in the gland packing. These are now back and ready to start the
reassembly of the valves.
The four cast iron blanks to make the new bull rings have
now been machined to final internal and outside diameters. Needless to say, each of the spiders proved
to be of slightly different diameters, so each of the blanks is now unique to
one particular spider and therefore one of the four positions in the
locomotive. They have also been tested
in the bores and proved to be the required fit on the external diameter.
These are now off-site being machined to produce the
finished bull rings.
Many happy hours have been spent in cleaning the spiders and
valve bodies. It is essential to remove
the hard carbon built up on these but, each has a small lip that secures the
spring ring. So it is a long and careful
process to carefully remove the carbon without causing wear to the lip.
In preparation for re-assembly the studs that hold the
cylinder ends have been inspected and around 50%, that were excessively corroded,
have been replaced. This provided interesting
confirmation of the history of #1630. On
the engineer’s side 15 of the total 20 required replacement but on the fireman’s
side only 4 needed replacement. This is
explained but the fact that, in the late 1930’s, she was involved in a head on
collision with a Mikado, suffered heavy front end damage, and the FS cylinder
casting was replaced. So the casting and
studs on the ES are mostly 20 years older than those on the FS.
A minor set-back has been the conclusion that the bores need
to be honed before the valves can be refitted.
As with many things in the steam shop, this needs unusual equipment. Honing a 12inch cylinder requires a pretty
slow turning motor. While we have such a
motor, it has not been used in many years and proved to need overhaul before it
could be used. That is nearly complete
so the honing can hopefully be done soon.
Once this is done and the bull rings are completed, we
should be able to start re-assembly of the valves.
Meanwhile work has progressed slowly but steadily on the
Shay.
One major step is that the form #4, engineering assessment
of the boiler has been completed and submitted for FRA review.
Most of the holes for rivets in the smokebox have now been
reamed so we are getting close to being ready to rivet.
Phil has been working on fitting the grates. This is a significant job as the grate
assembly is new. Prior to overhaul she
ran with a less than satisfactory arrangement fitted when she was converted
from oil burning. This time she is being
fitted with a new grate set up that should be more satisfactory ……………… once the
new castings are carefully adjusted and fitted to newly installed bearers. With a lot of work Phil has now got the grate
bearers fitted and the grates themselves are now being test fitted.
Mike has been replacing some broken studs in the cylinder
heads.
Jerry has been making good progress on lagging the boiler.
Work has continued steadily on the cab for #428. The riveting team have been making good a few
final missing rivets. Dennis has been
filling holes and shaping the roof to remove a few non-standard curves that it
had developed and John has been painting and fitting the window guides.
In the shop.
Collin has made considerable progress on the large
compressor despite having to be away a couple of weeks on business. (Two weeks at ore loading facility in
Northern Canada in mid-winter. Temperatures
heading to -40. He does get the nicest
assignments!). One damaged valve was
replaced and he has made significant progress on lapping the other valves. The compressor now runs much more smoothly,
sucks intake air with considerable force and pumps the reservoir up to the
150psi operating pressure pretty quickly.
From testing yesterday, the reservoir safety valve operates
correctly. We were also able to identify
two leaking gaskets that will need to be replaced. Once these are replaced, the compressor
should be serviceable. Two other key
steps were agreed. Everything on the
compressor is now installed enabling Dennis to finish and install the guards over
the drive belts and the method for unloading air pressure to allow the
compressor to start when the reservoir is under pressure was agreed. Parts for this will now be ored3er and fitted
while we wait for the replacement gaskets.
Hopefully we should be able to get to readiness for the system to be
inspected in about three weeks.
There was sudden major movement on another long standing
project. The control cabinet for the
wheel lather arrived. John and Bob
started to install this. They have now
identified exactly what parts are required for the low voltage control circuits
so this is coming together at last.
We have also had donated an excellent large band saw that
will be most useful in the shop.
So a lot of progress but still quite a lot to do for the
start of the season. Watch this space.
Nigel