It has been an awfully long time!.
The Summer is always a bad time for blogging about the steam
shop. Operating is very time consuming,
leaving relatively little time for other work and after that, things rather got
away from me.
So what is happening now in the steam shop?.
Everything is winterized and positioned in the shop for the
off-season work program. However, the
layout in the shop is unusual and this hopefully indicates a big change. #428 remains at the South end but next to her
is #1630 with Shay #5 at the North end.
In part this is because the (limited) planned work on #1630 this Winter
is best done over the small area of deeper crawl space but mainly because it is
hoped that #5 will be the first locomotive into steam in 2017!.
So, what is the status of the locomotives and plans for this
Winter.
#1630
The decapod had a very successful running season after the
incident in June with the broken truck Spring.
Thereafter all planned running days were achieved with only very minor
incidents. The most significant was
probably the breakage of a lubricator line to the crosshead guide. Some rapid brazing by Brian meant that we
only missed a couple of trips that day.
The valve and running gear work over the last couple of
years seems to have much improved the locomotive. She is now probably stronger than at any time
since she arrived from Eagle Pitcher.
With other aspects of the running gear now better adjusted, the most
obvious unwanted noise was from the rods on the fireman’s side. So the non-routine work for this Winter is
primarily the replacement of the rod bearings of the drive axle on this
side. The rods were removed promptly
once she was in the shop and the bearings are now in the machine shop. Measurement has demonstrated that they are
indeed worn beyond acceptable railroad standards. So replacements will be machined and fitted.
Aside from this the annual inspection is in progress. All the normal “fun” tasks are being
progressed.
·
gauges and safety valves are off for testing and
setting;
·
drawbars have been removed thoroughly cleaned,
inspected for any cracks and will shortly go offsite for annealing;
·
the locomotive has been resounding to the
tapping and banging as we crawl all over the inside and outside of the firebox,
clearing the telltale holes in the stays and then checking that they are clear
to the required depth. Good
progress. The outside is done and the
inside is well advanced;
·
cleaning and inspection of the smokebox and
front tube-sheet is well advanced.
It is also planned to do some “improvement” work on a couple
of the drive box wedges. One has had a
distinctly questionable adjusting bolt for many years that makes adjustment
awkward and another is believed to be just about at the limit of its
adjustment. So the plan is to correct
this over Winter.
Shay #5
Work on Shay #5 has progressed steadily and is now hopefully
approaching the point where an intensive spell can be scheduled to get her to
operating condition.
Major activity has included:
·
Dennis welding the new smokebox bottom into
place. Recently he was relaxing in his
purpose-built hammock structure! to complete the grinding of the joint on the
engineer’s side;
·
Jerry has substantially completed the lagging
and installation of the cladding is well under way;
·
Substantial progress has been made on the next
big step, which is installation of the blast pipe into the smokebox. On a Shay, that has had a rebuild of this
scale, this is a 3 dimensional jigsaw started knowing that some of the pieces
are missing!.
Obviously, as with any steam
engine, the blast orifice must center below the petticoat of the chimney to
ensure the most effective drafting.
Also, it must bolt thru the floor of the smokebox and into the exhaust
casting. However, unlike a rod driven
loco, the exhaust casting of the Shay is not the top of the cylinder casting,
firmly fixed into place, but a heavy casting that joins with some flexibility
to the exhaust pipe and is bolted at several points to the smokebox. The game is that, once all the attachments
are made, there is just about zero flexibility in how the exhaust casting must
sit and attach to the exhaust pipe and blast pipe and, to ensure the smokebox
is sealed as well as possible, all the mounting holes need to be a good
fit. Since the smokebox bottom is
entirely new (and the original was so rusted as to be useless as a template)
the game is to juggle and test fit these heavy and awkward parts accurately
into position so that the mounting hole scan be marked for drilling and cutting
with a fair degree of accuracy. The acid
test will come in a couple of weeks when we offer it up again and try to bolt
everything into place!.
·
The air pump was finally reassembled as
well. Mike has thoroughly stripped and
reconditioned this unit, so this should now be pretty much ready to go.
·
A big exercise completed over recent weeks, by
Dennis, is the fire-grates. This was not
a planned exercise. #5 was an oil burner
that was converted to coal on arrival at IRM.
The original conversion, in the 1970’s, was less than satisfactory and
part of the rebuild planned when she came out of service in 1998 was to fit a
new and robust grate system. This was
designed in advance and parts were obtained ready to fit, including the cast
grates complete with rocking levers, that were produced by a supportive (and
now defunct) local foundry. The finding
that the tube-sheet required repair turned the overhaul from a 2-3 year job to
nearly 20 years. The grate castings sat
unused for more than 10 years and it was only when they were pulled out of
storage, to build the new grate mechanism, that it was discovered the foundry
had misread the drawings and cast the rocking levers facing the wrong
way!!. Since they are cast iron, you cannot
simply cut the levers of and weld the back facing the other way!. The solution for now has been to fabricate
steel sections that can fit thru the grates and allow the levers to be attached
in the correct configuration. Time will
tell how well this will stand up to operation.
It is hoped that it will allow at least a couple of years of service but
there is no doubt that we will need to gather the money (estimate about $6,000)
to have new grates cast correctly to the drawings. The good thing is that the grates that Dennis
has modified are now exactly the shape that the design specified so, once we
can get grates correctly cast to the pattern, it should be a routine
maintenance activity to substitute them.
·
There is still much to do, including:
o
Rebuilding the front beam once the exhaust
assembly is finally installed;
o
Fitting the grate rocker assembly;
o
Sealing /lining the inside of the water tank;
o
Plus the myriad of once smaller tasks that are
always involved in bringing a locomotive back into operation.
However, the expectation is that she will be ready to test
in the Spring.
#428
Various work has continued on #428. The biggest has been work on the valves. It was decided to progress the valves while
the experience of the work on #1630 was fresh in the mind. While the detail of these valves is earlier
than #1630 and differs in some ways the basic structure is the same. Extensive measurement has been done to
identify where it is necessary to build up the spiders and ends to allow them
to be machined to critical dimensions.
Based upon this, the plan is to repair and machine to specification and
then get the valves reassembled.
#938
During the Summer, Phil and others continued the laborious
task of removing rust and repainting.
She now looks better than she has in many years and is now back into
barn #9 following completion of repair work on the barn walls.
#2903
The commissioning of the renovated Santa Fe sign provided an
unusual opportunity to see one of our large locomotives in the open. She was posed behind the sign along with the Warbonnet
#92 for the dedication ceremony. Sadly,
she aroused less than happy memories for one of our honored guests, a retired senior
Santa Fe executive. As a young man, she
was memorable for having barfed a large quantity of black gunk all over his
good suit during a re-railing operation!.
Oh well.
So we reach the end of another year. I am away to the UK for a couple of
weeks. It will be a busy Winter but it
promises to be an interesting New Year with the prospect of two running
locomotives. Please consider supporting
the Steam Department projects this year end. Money is always a limiting factor in all of our projects and will be critical in ensuring that the Shay does run as planned as well as ensuring that we can continue the improvement work on #1630.
Happy Christmas
Nigel