"GE Quality Builds Jobs" is what was printed on a placard right above the work area on Burlington Northern 5383 this past Sunday, as the reverser was removed to be repaired. Early last year, the reverser failed during a load box test that we normally do after the locomotives inspection. The steel of the top rear of the electrical cabinet had deteriorated, with a change in rpm during the load box test, the intermittent vibration throughout the locomotive caused a large enough piece of rust to drop from the top of the cabinet into the reverser while it was under load.
The loco was making about 1,800HP at the time based on the calculation done from the meter plugged into the multiplier card. The rust just happened to fall into the reverser on the center two lugs which are the main positive and negative feeds from the diode banks of the alternator. All the diodes were tested and all are in good shape. The damage was on the back side of the reverser as it was mounted and it was quickly determined that a repair wasn't going to be easy and not going to be done in place.
On the 15th, Dan C came out to tag and label all of the cables and start unbolting all the connections and bus bars. On the 21st, Wes L and Jim W removed it from the 5383 and placed it on a bench in the shop. Some pictures have been uploaded to a photo gallery.
The next steps are to start hunting down parts to replace the burned up insulators in the reverser. At the same time we'll need to take the torch to the fresh paint and start replacing the supports and top of the back half of the electrical cabinet. The estimated cost of the repairs at this point is about $1,500.
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...