On Tuesday, Jeron G and I made it out after work, with the goal of trimming the profile of the #4 axle on Milwaukee Road 760. Some years ago the #4 developed some flat spots. We started by removing the brake shoes and installing the cutting shoes. We used full tread and flange cutting shoes so the entire profile is taken down equally. The cost of the shoes was far less than I had expected, only $120 for a pair, so that was a pretty inexpensive way to deal with the problem. Although it was time consuming, it did address the issue. We then ran the loco over to the main line and went back and forth between the tower and the bridge. The first 30 to 40 minutes was just getting the shoes to wear in and seat so the full width was cutting. It was a lot of slow, boring, back and forth moves. We called it a night about 9:30pm. The flat spots were about half gone at that point.
On Thursday, Jeron G, Roger B, and I were out after work again. Jeron got to work with a few more hours of running the 760 back and forth. Meanwhile, Roger started disassembling and recovering some pipe fittings from the 9255. There is an air pipe under the cab floor that was rusted through in a few places, which will be replaced with new schedule 80 pipe, reusing a few of the old unions and such that are still in good shape.
I went and got the Joy 2 to drag the 8537 near an outlet to charge its batteries, and then dragged the BN1 to the nearest crossing to change out a bad battery. The BN1 uses eight 4-cell 25 plate per cell batteries. A few years ago, a bad one was changed out with one that was really old, but still holding a charge. Its all we had at the time, and no budget to fix it. It finally cracked its case and was completely open, literally and electrically. I picked up a like new used battery for $300, that was the same model as the other 7 batteries. Roger and I dragged the old cracked battery out of the box and shoved in the new one in, wired it, and put the loco on the charger after shoving it back in the yard.
We put the Joy 2 away, started the 8537 after its batteries charged enough to start it. We met up with Jeron to see how the truing shoes were going on the 760. The flat spot on the fireman's side was about gone, you couldn't measure it, but just a little visible. There was just a little bit left on the engineers side. Not sure if we'll live with it as it is or go for another few hours, its certainly A LOT better than it was when we started. We called it a night again, Jeron put the 760 away while Roger and I put the 8537 away.
I stayed another half hour to mask off the numbers on one side of Santa Fe 92, to spray some red so the numbers are readable on the sides of the cab once again. If you are a Santa Fe 92 or SD45/FP45 fan, come out on Sunday as the 92 will be leading, as a cab car, the WC 7525 and Coach Train. No pictures this time, actually, I did take one of the numbers being masked, but didn't upload it yet. We'll try to add more pics with this weekends work.
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...