Again, we must thank Nigel Bennett for forwarding another Steam Report. The department is active and moving ahead every week, and I for one, cannot wait for the next news and progress to be reported.
"Saturday 10/29 was another good day of progress in the steam shop.
On 1630, Collin and Eric soldiered on with the air hammer on the tube plugs in the front tube sheet. They are now down to about 15 of the the small plugs plus the larger super heater plugs to remove. Then, rather than relax, they have the same exercise to do on the the firebox end. A measure of their success can be seen below.
Every one of the plugs on the floor of the smoke box has been hammered out by the guys inside the boiler and, if you look closely, the only ones remaining to be done are the few in the top left.
Meanwhile, being too big to fit into the boiler, I was working with Vince on stripping the boiler back head. We have now removed all the cladding and insulation along with a horrifying amount of pipe and fittings that must come off to allow the cladding to be removed. So this is what the engineers side of the back head looked like two weeks ago.
And as of last night!!
This proved to be a really unpleasant job. The covering is a complex array of sheet metal covering hundreds of blocks of insulating material. Removing it requires removing enough pipes, valves, fittings, etc. to be able to free the sheets, removing these, and then removing the insulation. Years ago this would have been asbestos but obviously this is long gone and Tom Schneider tells us the current material is a mix of cellulose and wool. The trouble is that after exposure to damp and steam this can become a solid mass that breaks into powder and dust as you remove it. A key reason that there are no pictures of the intermediate stages is that I was not prepared to risk my camera in the dust cloud!!
So, good progress, but it will be really nice when we can start to report some repair and reassembly as opposed to taking things apart.
In parallel with the work on 1630, other members of the team were able to clear the shop by storing all the parts removed in the loft, and prepare the all door box car to receive more parts as they are removed. Others continued on the axle boxes and wedges being rebuilt for the UP 428."
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...