Another good day of progress.
Walking thru the shop, you would not see much change in 1630 but internally progress was good.
Eric and Collin cut and hammered another 40+ tube ends from the firebox tube sheet. Hopefully this can be completed in another couple of weeks and then we can progress to cleaning, by wire brush and sand blasting, of all the internal surfaces. This will enable the inspection, which is the key objective of the whole exercise.
Mike and Bob continued with the firebox patch by starting the removal of one of the patch screws securing the outside wrapper in this area. It is hoped that this is the only one damaged to the point at which it will have to be replaced. Other tasks on 1630 itself are largely on hold until the tube ends are out. It is pretty difficult to work on the locomotive when someone is using an air hammer in the boiler which acts as a big sounding board!
Away from the locomotive, a lot of progress was made on clearing material out of the shop to the boxcar. Two large air tanks and other parts of #26 were successfully transfered to the boxcar and we now have a work space on the East side where we can work on large parts during the winter.
We now have the area for the swaging operation clear and can hopefully start the set up next week.
On the Shay Dennis, with help from the "removals crew", made good progress on setting up stands to ensure that the locomotive is completely stable so that he can start welding the new smoke box plates into place. Funny, he seems to have a strong desire to see the thing completely supported. It may be to do with the fact that he will be working under there for days on end!!.
Good progress was made on cleaning the bolster from the truck. It makes an interesting comparison with the "before" picture of the bolster last week when first removed from the truck.
However, a great deal more remains to be done when you look at the area where the springs sit in the truck. The steam shop is never short of big cleaning opportunities!!.
On 428 several jobs were progressed:
We got input from an external advisor on the repair of the riveting furnace that we need to complete the cab riveting. When this repair is done, we can rivet the cab which will have a double benefit. 428 will look a great deal better with its cab back on and a large area at the South end will become available for fabrication when the cab is off the floor.
Another group worked on the air compressor. A lot of carefully measurement was required to identify exactly what size of piston rings we need. With this done, we can now order them and move forward to reassembly once we have them.
Cameron was working with Tom on machining bushes for 428.
In other areas, Rick continued the covering of the lathe and Glenn worked on the radiator fitting on the Bay City crane. We are holding our breath on this one!. Weather permitting, it may be that next weekend the cooling will be in place and crane will have a working traction motor for the first time in 20+ years.
So another productive day.
Nigel
There was a large crew on hand, following the holiday hiatus, and we passed another milestone in the restoration tasks for the Cleveland PCC.
A large number of parts had been sent out to a contractor for painting. These represent a lot of the trim and detail parts removed for repairing the body and getting that painted. Now they are back, in record time. SOME of them are seen staged in the shop in the above view. More are expected later this week.
In short order, Eric Lorenz and Alex Randow turned to the task of starting to install them. Tricky business, and you almost had to be a circus contortionist, but the front bumper was installed. Actually there are three such pieces.
Before I knew it the rear bumper parts were appearing on the car. Eric and Alex watch as Nancy Ring tests the location of the rear retriever mounting ring.
Several volunteers spent some time during the day continuing to clean up and restore the myriad of side window sash. Julio Mojica joined the crew scrubbing off years of corrosion and dirt, and Alex and Nancy put in some time there also.
As each sash resumes wearing its clean bright finish, we are applying a protective clear coat. Nancy tried her hand at that, and perhaps six were so coated by the end of the day.
The remarkable changes to the appearance of the car are giving the project team a big boost, and those following the progress admire the transformations.
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...