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Sunday, April 29. 2012Steam Department Update 4-28-2012A rather brief update this week, not because of lack of progress but because I spent most of the day in the rules and safety sessions so was not directly involved in the work in the shop. While this was a day away from the shop for a number of us it is essential that we have a team able to control movement of equipment and these sessions are critical to ensure that this is done safely. Work progressed steadily on 1630: · Collin, Eric and Jason made good progress on cleaning and preparing the tube sheets. Both front and back tube sheets have now been extensively cleaned and checked. The good news is that no signs of cracking have been found. Work is progressing on smoothing and preparing the holes to take the new tubes. This will take several weeks to complete but good progress was made today. · Dennis, Bob and Mike continued building up of the mud ring ready to for fitting of the corner patch. Over the next couple of weekends this will move out of sight as the section inside the firebox is built up and the rivet holes on that face are rebuilt. · Plans are in place to do the thickness testing next Saturday. This weekend we were marking out the points at which measurements will be taken. Each section of the boiler plate work must be measured to assess its minimum thickness which then forms the basis of the calculation for the form 4. Clearly each part of the boiler is only as strong as its weakest point so the calculation is based upon the thinnest point found in each section. Measurement points are identified in a random pattern across each plate with a focus on the areas likely to be weakest such as the belly. Here the guys are cleaning off and marking measurement points ready for next weekend. Nigel Sunday, April 22. 2012Steam Department Update 4-21-2012A successful day at the steam shop. We now expect the ultrasonic testing to be done weekend of May 5th so yesterday was an opportunity to progress other activities in preparation. 1630 saw the light of day for the first time in nearly a year when we pulled her out to remove the throttle valve and allow cleaning of both the locomotive and the shop area where she has been sitting. Eric and his father made good progress in testing the tell tale holes in the firebox stays. The engineer's side is now largely complete. By midday Jeff had the BrownHoist de-winterized and running and we were ready to shunt 1630 out of the shop. Once outside we worked on the removal of the throttle body, which will be lapped to ensure a good seal when reassembled. This is an awkward piece that sits in the dome. However, with some help removing cotter pins from inside the boiler, it was removed and taken to the shop. It has apparently been removed and refitted in the past with all the tubes in place. I have a lot of respect for the guys who achieved that !!. It was good to see 1630 in steam again !!. Seriously though, it was an opportunity to do some steam cleaning and the locomotive now looks a good deal better and easier to inspect. The opportunity was also taken to clear the area around and under the locomotive, that had accumulated the most amazing collection of insulation debris and other muck as well as odd items that had fallen while working. By end of day she was back in the shop and ready for ultrasonic testing. In other areas, Paul and the lads made good progress on needle chipping and wire brushing the Shay truck. Glenn over came a problem, that has developed in recent weeks, of the fork lift battery failing to hold a charge. Far from the suspected defective battery he found that a loose terminal and blown fuse in the line from the alternator meant the battery had not been connected to the charging system at all for the last few weeks!!. Next weekend will probably be quiet as many of us need to attend the rules exam. Nigel Sunday, April 15. 2012Steam Department Update 4-14-2012A very productive day thanks to a good turnout. We did not move 1630 as Dennis was available to do welding on the mud ring for the firebox patch. Good progress was made on this. The metal has now been made good around all the rivet holes from the outside. Once the last of the holes is re-drilled accurately from the inside the metal can be made good on the inside. (One side must be done at a time so that there is always a pilot hole to ensure that the finished rivet holes are accurately aligned). Now that the sand blasting and associated dust are finished several other jobs could be progressed. · Collin and Jeff C thoroughly needle chipped and wire brushed the back head so that is now ready for inspection and ultrasonic testing; · Eric and Jason cleared and checked the tell tale hole in the stays on the engineer's side. This is a dirty and tedious but essential task as we must prove that these holes, which would leak water and provide an indication should the stay break, are all clear to the required depth; · Matt finished removing the blasting medium from the firebox crown and Bob cleared it from the sides of the firebox so it is now clear in most areas; · We continued the detail measurement of the super heater flues and should soon be ready to start preparing the material for safe ending; · Jason and Eric moved on to cleaning up the inside of the tube sheet for final inspection and preparation to refit the tubes. The sheet must be closely examined for any cracking between the tube holes then the edges of each hole must be made good where necessary and smoothed to ensure a snug fit when we use the rollers to expand the new tubes into place. We are now scheduling the long awaited ultrasound testing that will provide the basis for the critical form 4 calculations in support of the new certification. Work continued in a number of other areas progressed in previous weeks such as the planer and the boxes for 428. In addition, Rick and Ed cast the firebrick for the riveting furnace that we need to complete 428's cab. That is an important mid-term objective as refitting the cab to 428 would free up a very useful area of the shop for other fabrication work. Jeff worked on lubrication of the Brown Hoist crane in preparation to pull 1630 out. We will do this as soon as weather and other jobs, such as the welding and the ultrasound testing, permit. We also managed to largely clear the area between the shop approach and barn 9. B & G are planning to grade this once it is clear, reducing the risk of flooding and hopefully providing a more stable surface. This area is a long standing problem as parts of it are no more than fine sand or dust not far removed from quicksand. It proved its capability again yesterday when the forklift became bogged and we spent an hour extracting it!!. Nigel
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Comments
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]