Sunday, May 27. 2012Steam Department Update 5-26-2012A second hand update this week as I was not there. It sounds like a good day's progress despite (or probably because of .. !!) my absence. Thanks to Phil for the input. Steady progress on 1630: · Bob and Phil worked around the UT measurement points to ensure that those where we could not get a clear signal last time are ready for retesting. We have confirmation that Tom will be back next Saturday to do this; · Bob now has the measurement packages for several of the sheets to allow work to progress on the form 4; · Eric was able to depth check most of the stays on the Fireman's side except for a small number where heavy lifting to remove grates will be required; · Bob needle chipped the wrapper sheet around the turbo generator and removed the last of the insulation in that area; · Phil cleaned off the top to the tender. Next we will need a spell of needle chipping to prepare it for painting. This is not an area that is visible to the onlooker but, being flat, it gathers water and needs to be well primed and painted to avoid rust; · Cameron and Phil started work on preparing the ends of the super heater flues for safe ending. These have to be ground to provide a taper into which the tapered end of the extension tube is fitted and welded. (These are not simply butt welded as it is important that, should the weld fail, the flue would not simply drop into two pieces); · Unfortunately the Sullair developed a problem which prevented sandblasting of the tube section that we need for the safe ending.. In other areas: · Paul continued needle chipping the truck of the Shay; · Ralph machined the last of the bull rings for 428; · A large team worked on the rivet furnace and the fire brick for the base has now been poured in situ. It looks as if this is now getting close to ready once the concrete has dried and will then need to be carefully fired to prevent cracking. Nigel Sunday, May 20. 2012Steam Department Update 5-19-2012Another good day in the shop although I think most people were moving a bit slower due to the 90 degree temperatures. Work on 1630 continued as planned: · Despite the heat, Dennis put in many hours in the firebox and has now built up the inside face of the mud ring. Now Mike has a lot of work to carefully drill the rivet holes thru the new weld, at which point the mud ring will be ready to receive the patch. This will be a slow and tricky job requiring the accurate drilling of small pilot holes that must be steadily enlarged as creating an accurate hole thru the weld is never easy; · Work continued with Bob on the form 4. We now have a detail plot of all the measurement points and a few new ones marked up for the next UT testing session (hopefully 6/2); · Several of us worked on completing the diagrams that Bob will need in support of the form 4 showing the location of each thickness measurement point on the particular boiler sheet. Boring work but at least it is good to see the book that will support the form 4 starting to come together; · Part of Phil's extensive sand blasting effort was the dome cover as noted last week. Now we have the "after" view ready for inspection and testing · We located a length of tube suitable for safe ending the super heater flues so now we can progress with this when resources are available; · One unfortunate set back was that the piston rod of the McCabe flanger broke during test bending of steel for the patch. Several of us spent quite a bit of time checking the storage for a spare but this proves to be one of the parts for which we do not have a spare. The broken rod has been stripped out and sent for analysis. Once we have this a similar steel rod will be acquired and machined. Phil did a solid day of sand blasting and, aside from the dome cover for 1630, also did all four of the axle boxes for 428 and the bolster for the Shay. This was quite an effort given the heat. Unfortunately one photograph I missed was Phil after working most of a hot day in a cloud of black dust. The trouble was that, like most of his sympathetic colleagues, I was too busy laughing and joking about his appearance to hold the camera!!. Sorry Phil. The results of his efforts can be clearly seen on the bolster for the Shay. This now looks very different and, aside from the improved appearance, appears free of any cracks after detail inspection. In other areas: · Ed and Rick worked on setting up the rivet furnace to cast the new brickwork. · Stu and Cameron continued work on the planer. · Bob operated the water supply to provide treated water ready for Leviathan. I will not be providing an update next week as I will be out of circulation for a hopefully minor operation. Nigel Sunday, May 13. 2012Steam Department Update 5-12-2012Generally a successful and productive day in the shop. The best news is that Tom was sufficiently recovered to be back at the shop. A lot was progressed on 1630: · There was a change to the plans for the thickness testing as Ralph's brother will not be able to come back to complete this for several weeks. However, this is not necessarily an overall delay as we already have enough information to start reviewing the calculations for the form 4 (engineering analysis of the boiler) with Bob Hunter, who will prepare it; · We did an initial review with Bob, who is now working with the previous form 4 data to determine what operating pressure we should consider. I now have a bunch of "homework" to plot all the measurements on diagrams of the sheets. One benefit of the second set of measurements being later is that we can review these with Bob and decide if we need any additional data points on the main sheets before Tom next comes; · All the remaining sections of the boiler are now marked up with points for testing aside from the dome top. In view of the successful sand blasting set up noted below, it was decided that this part would benefit from sandblasting before we test it; Hopefully we will have an "after" view soon !! · Collin and Jeff did close examination of the back head braces using a boroscope. These braces are of particular interest as it was calculation of the loads on these that resulted in the reduced operating pressure from 2001. They are very inaccessible (running from the top of the wrapper to the back head above the inner firebox and among a forest of crown stays). The conclusion is that their condition is excellent. The camera shows no sign of wastage and, where we can get to them with a micrometer, they are still pretty much at the size shown when the boiler was built in 1917. So, if the conclusion is that these are not considered sufficient for 180 psi operation, it will be due to requirement for a greater safety margin than historically required rather than any wear or damage; · Jeff and I worked on the firebox stays. All the stays must be proved to be sound either by demonstrating that a tell tale hole is clear thru to the head of the stay or by removing the cap and hammer testing. Most have tell tales that we have ensured are clear but a number are solid so must be hammer tested. This was a job approached with considerable concern as the caps look very rusted and, should they break as you try to remove the caps, the stay must be replaced. Each replacement would be a substantial job. Much to my surprise this task proved not to be as bad as feared. Having identified the outer ends of the stays to be examined we started heating each one and then tried to remove the cap with a wrench. To our great surprise, once heated, each cap unscrewed smoothly from its socket. The rusting is far more superficial that appearance suggests and, once heated and the cap removed, the stay head looks relatively clean. Building on our success in removing the required 9 caps on the engineer's side wrapper we tried some on the back head. While these do have good tell tales we were concerned from appearance that the sockets were so rusted as to require replacement. Again the experience was not only that the caps removed without issue but that the sockets are actually much thicker than they appear so few if any require replacement. Altogether a lot of potential work avoided. The three lower stays, now with the caps released, looked like the row above earlier in the day. Amazing how much of the apparent rust damage is actually superficial. Elsewhere Stu, Matt and Glenn fitted the new cast face to the small rivet furnace. This is now ready to cast the fire brick interior. Once this is complete we can hopefully complete the cab for 428.
Bob has de-winterized the water supply ready for Leviathan, which is expected next weekend. Jeff and Phil set up for sand blasting parts outside using material recovered from the boiler cleaning. After a few issues with screening the used material, the process was established and proved using the hood of the Bay City. Now it is proved we can set up quickly and next week should be able to work on parts of 1630 and 428. Paul and Bob continued on the Shay truck. One small but time consuming job is caused by the fact that a number of the raised metal washers that stop the springs moving are missing. In this view you can see what should be two rows of 5 spring retainers. The wear around each shows where the spring resting against the bolster carried the weight of the locomotive. You can see in this view two washers missing leaving just a broken pin. These prove to be held in place by rivets driven into a blind hole. This is no great problem where the rivet has pulled out but "great fun" where the rivet has sheared off and must be carefully drilled and then removed in pieces to make the recess into which a new rivet can be driven. One that was removed, as it was loose, shows the way in which the rivet expands into a groove to hold the assembly into place. Significant progress was made on the bull rings for 428 where Mike was finalizing the machining of the third ring while Tom and Ralph were starting the fourth and last one. Nigel |
Blog AdministrationCategory TreeCalendarQuicksearchSyndicate This Blog |
Powered by s9y.
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]