Sunday, May 13. 2012Steam Department Update 5-12-2012Generally a successful and productive day in the shop. The best news is that Tom was sufficiently recovered to be back at the shop. A lot was progressed on 1630: · There was a change to the plans for the thickness testing as Ralph's brother will not be able to come back to complete this for several weeks. However, this is not necessarily an overall delay as we already have enough information to start reviewing the calculations for the form 4 (engineering analysis of the boiler) with Bob Hunter, who will prepare it; · We did an initial review with Bob, who is now working with the previous form 4 data to determine what operating pressure we should consider. I now have a bunch of "homework" to plot all the measurements on diagrams of the sheets. One benefit of the second set of measurements being later is that we can review these with Bob and decide if we need any additional data points on the main sheets before Tom next comes; · All the remaining sections of the boiler are now marked up with points for testing aside from the dome top. In view of the successful sand blasting set up noted below, it was decided that this part would benefit from sandblasting before we test it; Hopefully we will have an "after" view soon !! · Collin and Jeff did close examination of the back head braces using a boroscope. These braces are of particular interest as it was calculation of the loads on these that resulted in the reduced operating pressure from 2001. They are very inaccessible (running from the top of the wrapper to the back head above the inner firebox and among a forest of crown stays). The conclusion is that their condition is excellent. The camera shows no sign of wastage and, where we can get to them with a micrometer, they are still pretty much at the size shown when the boiler was built in 1917. So, if the conclusion is that these are not considered sufficient for 180 psi operation, it will be due to requirement for a greater safety margin than historically required rather than any wear or damage; · Jeff and I worked on the firebox stays. All the stays must be proved to be sound either by demonstrating that a tell tale hole is clear thru to the head of the stay or by removing the cap and hammer testing. Most have tell tales that we have ensured are clear but a number are solid so must be hammer tested. This was a job approached with considerable concern as the caps look very rusted and, should they break as you try to remove the caps, the stay must be replaced. Each replacement would be a substantial job. Much to my surprise this task proved not to be as bad as feared. Having identified the outer ends of the stays to be examined we started heating each one and then tried to remove the cap with a wrench. To our great surprise, once heated, each cap unscrewed smoothly from its socket. The rusting is far more superficial that appearance suggests and, once heated and the cap removed, the stay head looks relatively clean. Building on our success in removing the required 9 caps on the engineer's side wrapper we tried some on the back head. While these do have good tell tales we were concerned from appearance that the sockets were so rusted as to require replacement. Again the experience was not only that the caps removed without issue but that the sockets are actually much thicker than they appear so few if any require replacement. Altogether a lot of potential work avoided. The three lower stays, now with the caps released, looked like the row above earlier in the day. Amazing how much of the apparent rust damage is actually superficial. Elsewhere Stu, Matt and Glenn fitted the new cast face to the small rivet furnace. This is now ready to cast the fire brick interior. Once this is complete we can hopefully complete the cab for 428.
Bob has de-winterized the water supply ready for Leviathan, which is expected next weekend. Jeff and Phil set up for sand blasting parts outside using material recovered from the boiler cleaning. After a few issues with screening the used material, the process was established and proved using the hood of the Bay City. Now it is proved we can set up quickly and next week should be able to work on parts of 1630 and 428. Paul and Bob continued on the Shay truck. One small but time consuming job is caused by the fact that a number of the raised metal washers that stop the springs moving are missing. In this view you can see what should be two rows of 5 spring retainers. The wear around each shows where the spring resting against the bolster carried the weight of the locomotive. You can see in this view two washers missing leaving just a broken pin. These prove to be held in place by rivets driven into a blind hole. This is no great problem where the rivet has pulled out but "great fun" where the rivet has sheared off and must be carefully drilled and then removed in pieces to make the recess into which a new rivet can be driven. One that was removed, as it was loose, shows the way in which the rivet expands into a groove to hold the assembly into place. Significant progress was made on the bull rings for 428 where Mike was finalizing the machining of the third ring while Tom and Ralph were starting the fourth and last one. Nigel Friday, May 11. 2012
B&O Boxcar Update - May 9, 2012 Posted by Robert Kutella
in Baltimore & Ohio 374065 Wagon Top Boxcar at
10:57
Comments (2) B&O Boxcar Update - May 9, 2012Spring is here and that means on good weather days, the Freight Department crew is at work in our outdoor 'shop'. Here is a sort of photo essay (not much text) on work this week, lots of participants and onlookers encouraged to learn and get a 'feel' for this sort of blacksmith work and tools involved. Gerry Dettloff is getting ready with an acetylene torch with Dick Cubbage and Simon Harrison looking on. Some sections of the side at the bottom were badly rusted out. The first step here is to use an acetylene torch to burn off the old rivet heads. Gerry is using the torch and Victor Humphreys ready to help as needed. The metal is being peeled back by Victor, Gerry, and Dick. After cutting the rivet heads form the outside, shards of old metal siding and layers of rust are removed. Some additional grinding of the torched off rivet stubs might need to be done. Then out with the small sledge hammer and a punch pin to poke the rivet out the back. Not much left after the torching, but some medallions of remaining metal sides need to be peeled away, pried away, or otherwise coaxed to leave. Then on to the satisfying part of punching out what remains of the rivets. Sort of like an 'aggression therapy' session. Jim Leonard takes a turn. That entire section is complete. The next step is to fit and cut a new metal patch, drill it for placing new rivets, weld it in, grind, fill, paint - you get the idea. Friday, May 11. 2012
TMS Project Update - May 9, 2012 Posted by Robert Kutella
in Two Milwaukee Streetcars at
05:37
Comments (0) TMS Project Update - May 9, 2012STOP THE PRESSES! THE WHEELSETS HAVE RETURNED TO IRM! Recall that the goal of this project is to restore two operating streetcars to service at IRM. As they say on TV, do it big or go home. The wheelsets are back at IRM with new steel tires applied, and they look spectacular. Here is a short summary of the project to date. New steel tires were ordered and custom made, enough to apply to both streetcars. The trucks were removed from the TM 972 and extensively rebuilt. One truck has had essentially a total rebuild as we found badly worn pins and bushings in the linkage, rods, levers and brake systems. This was not something anticipated and was discovered after the trucks were being dismantled. What is one to do, stop everything? In the true IRM spirit we had to repair these items while the truck was out and disassembled. Such is the life of a restorationist. We could have had the needed parts custom made and waited until September for delivery and another six weeks to install them. Instead we made these ourselves in the machine shop, and heat treated and hardened them on site. This saved us months on the timeline and saved us about $4000 in costs. See where this is going? It also added up to about $8000 in unanticipated expenses, so money in the fund is running very low, about non existent. We have spent money ahead on common parts for the CNS&M 354 to get the same treatment but need your support now to see the TM 972 running this season. We are ready to begin final re-assembly of the trucks NOW and will keep you updated of any 'new' discoveries. Please keep this major project on track and moving ahead with a donation to fund RTMS. We really need this and the money is not squandered. |
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Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]