We made some good progress with annual maintenance and inspections of our rolling stock.
CGW 601, MILW 01984, and UP 3786 arrived on track 41 outside Barn 4 for the work. All are now considered 'passed' and released for operations on our railroad.
Flushed with this success, we also got CNW 10304 for some work. The car has seen extensive restoration over many years. But we discovered a fatal flaw in a cracked coupler casting. This has taken some time over a few years and involved finding a new coupler and cooperation from the steam shop to fabricate a new cross key. Victor Humphreys and Dick Cubbage are ready for the 'real work'
And REAL WORK it was. After two tries the new coupler shank was installed, only to find the new cross key was a 'tight fit'. Actually an interference fit as it would not go through the slot. First, Victor tried grinding and after that proved not enough, Jeff Calandine went to the steam shop and used a milling machine to re-size it.
Dan Fenlaciki is trying mightily to solve a Knuckle Puzzle. The new coupler shank did not have five key parts for the innards. It really is not too apparent on how they might all go together and make the coupler work.
Victor Humphreys and Dan Fenlaciki have it all together and the uncoupling lever assembly is assembled to lift the pin and open the knuckle.
Meanwhile, Jeff Calandine, a big guy in a small space, made several trips underneath the car wrestling with the cross key. In the end, it has been assembled, the car inspection done, and another caboose 'passed' and ready for service. And one that has not seen any mileage for years, or maybe decades. NEXT???
There was a lot of work done and a lot accomplished in the last week. Stay tuned as I hope to find time to post extensive updates.
Dan Fenlaciki was at the big bandsaw cutting new stakes for a flatcar project being managed by Mark Secco. I think this is for CGW W 52 which acts as a crane tender car.
Gerry Dettlof and John Faulhaber are installing steel plates to either side of the freight door on Lake Shore Electric 810. Their purpose is to minimize damage, dents, and dings when freight is loaded or unloaded from this traction trailer.
Gerry continued with installation of the second steel panel to the left of the door.
I was caught in the act of painting the second Great Northern herald on our GN 70104 hopper car.
Frank Kehoe had his head in the clouds as I caught his good side in the viewfinder. L car CRT 1797 was 'modernized' in the 1930's with a drop ceiling. Years of crud, dirt and debris have accumulated, and he was diligently applying the shop vacuum to improve the situation.
Tim Peters, meanwhile, is applying the finishing touches to the completed roof of the 1797. A lot of work, a lot of parts and paint, and an uncommon persistence to finish the job. Usually the phrase "Petering out" means you are fading in the mission. Not so with Tim Peters.
A crew of three were on hand Friday to work on Vera Cruz 19. Mike Alterio, Frank Sirinek, and Mike Stauber were fabricating and fitting new metal at the base of the front dash. This is part of the often invisible work done by Frank and his crew for constant but incremental improvements to this car.
Also on hand for the above efforts was BUFFY who was acting as sort of a LINE SUPERVISOR or PROJECT MANAGER.
Dave Diamond has been leading a large volunteer crew assembling components and now constructing the playset. Kind of wet in the morning, but I bet a dozen or so were working in the afternoon and it is taking shape.
One of the steel CTA 4000 L cars has been in the barn 4 shop areas for a number of years. Today, Rich Block came on a visit and was fabricating and cutting metal to allow re-pouring of lightweight concrete MASTIPAVE for the end vestibules.
Victor Humphreys continues his almost one man efforts to restore the B&O wagon top boxcar. Here the first two sections of the south side have had all rust and old paint removed and now have been prime painted.
No pic for this news item, but late in the afternoon, Tim Peters, Rich Block, and Bill Wulfert crawled under the CRT 1797 L car. You have seen the work done by Tim and others on the carbody and now on to the underbody, mechanical, and electrical systems. The air compressor was inspected, and they then discovered it could be rotated freely by hand. Not bad for something that has not operated on its own for half a century. This was truly a piece of good news.
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...