It will be a short and late update this weekend as I went on the Zephyr trip today. What a great day. Tremendous effort by the team. Well done guys for making it a such great experience for those of us who just had to sit back and enjoy ourselves.
As regards Saturday at the steam shop hopefully all the bad things for a while happened this weekend!!.
First, the most critical job now to be done is painting the interior of the boiler, which can only be done by a small number of our team who can fit thru the access hatch to work inside the boiler. Unfortunately one is facing a serious family health problem and the rest had other commitments so we were unable to progress the painting this weekend.
So we focused on setting up to prepare the tubes for fitting. Each tube must be swaged (reduced in diameter from 2 to 1 7/8 inch at the firebox end), annealed at the smoke box end and then cut to exact length. The original game plan was to complete the set up and then try a few test runs before maybe doing the first few tubes. Sadly this was not to be. We brought the first tubes in without problem
However when we tried to start the Sullair compressor, to drive the furnace and swager, the starter solenoid stuck causing the starter to burn out!!. Having disconnected the battery and put out the fire, investigation revealed that the nose of the starter must have fractured a while back and just got into a position where it caused the solenoid to stick.
So we wait one week to rebuild the starter and hope we can start swaging next week. Anyway, the area is now ready and the first 40 tubes were brought in and set ready for work.
Another piece of bad news was about the ferrules. As noted last week, we received ferrules but they were 2 inch ID versus 2 inch OD. The bad news proves to be that the supplier no longer makes 2 inch OD. Unless someone else makes them we will have another very tedious job. The alternative, if we cannot buy them ready-made, is to cut 150 5/8 inch long sections from 2 inch copper tube. A perfectly practical but dull and time consuming job.
To complete our woes for the day, Ed and Bob were continuing to the fit of the pipe work. The simple job of heating a nut to remove it from the stud to allow the pipe bracket to be adjusted to the new pipe took a good part of the day. What first seemed to be an empty acetylene cylinder proved to be a regulator than had gummed up and will need to be reconditioned.
On a more positive note we went thru with B&G the plans for grading in front of the shop and preparing to install the new air compressor to feed the new shop. This will allow us to rivet (and swage) without relying on the Sullair. We were also able to work with Jeff on the layout for the air supply in the new shop.
So some overall progress despite a number of setbacks. Let's hope for better this week.
Nigel
Comments
Mon, 09-08-2025 08:22
Good job on the Burlington Nortern 9976. OK.
Tue, 08-12-2025 12:56
No new news that I have heard of thus far.
Tue, 08-12-2025 12:53
I'll also be doing another update on it soon. Keep en eye out for that.
Tue, 08-12-2025 12:47
A little work was done to it for Diesel Days this year. You'll see photos floating around for the temporary short term job that was done to make it [...]
Wed, 08-06-2025 13:01
Is steam car CN 15444 going to be coming to museum several times it was to be moved to muesum
Sat, 07-19-2025 18:56
Yeah, sadly it's still there as of 7/19/2025
Thu, 06-12-2025 19:14
Its been 14 years guys, where is the unit? Like really? Did you guys misplace it? Or are repairs taking that long? At this point be might we will have [...]
Wed, 04-09-2025 17:40
Jamie Thanks for the update. She's gonna shine like every thing else you guys do! Smeds
Thu, 03-06-2025 16:28
Yes, there is a wye. Those two have been MU'ed on diesel days a year or two ago.
Wed, 03-05-2025 14:04
7009 number boards look good. Is there a way to turn a locomotive around at IRM? In case you ever had a mind to connect 7009 and 6847?
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...