Tuesday, October 29. 2013
RI 2612 10-19-13 update I was ... Posted by Roger Kramer
in Passenger Car Department at
11:01
Comments (0) RI 2612 10-19-13 update I was out numbered
This was a first in the coach dept. Saturday, October 19th saw 4 volunteers working on the 2612 but I was the only male volunteer in the group. Yes, I was happily outnumbered by three ladies working in the coach. Jane Blackburn, Nancy Ring and a new volunteer, Sarah Meuller all worked on 2612 project. Sarah's friend, Dave, volunteers in the Steam Shop. I, not to be outdone, was disassembling one of 32 brass window frames. Removing two window latches from each frame is quite time consuming. It would be easy if they were fastened to the frame with brass screws but that is not always the case. Many times when they were repaired by the RocK Island maintenance crews they use anything they could find. That includes the steel screws which, now, I am having so many problems. The screws are rusted into the frame. Its very time consuming and difficult to remove. To date almost all the latches have been removed. Happy Halloween to everyone! I hope all of you came out to enjoy the " Terror on the Train" this year! It was sccarry!! When your out visiting Irm please stop by the 2612 project. Thanks for reading, Roger
Tuesday, October 29. 2013Wood Shop Update - October 26, 2013It looks like this will be another long entry but it should get us current with shop and restoration work. We have repainted our large Great Northern tank car, it is the largest tank car in our collection at 20,000 gallons. Now, on to the lettering the car. I traced what remained of the old lettering before it disappeared in the painting. Then I re-drew and cleaned up those tracings. Step three was to cut out the letters, and some might think this is to be used as a stencil. But no, I use it mounted and aligned on the car and trace the outlines onto the car using the mylar sheet as a TRANSFER PATTERN. Then it is off to the slow task of painting to the above outlines. Here is the result showing the Great Northern name PROUDLY. I then moved on to add the number and identify the car. Great Northern X-1390. Eric Lorenz is finishing up some of the hardware for hanging the four large ceiling panels in our Cleveland Transit System 4223 PCC car. The view and effect is quite a transformation and a testimonial to the hard work of the crew. Rich Witt is applying epoxy sealer to some new rear seals for a freight car truck. We have had quite a tutorial on freight car trucks as we work to remediate and make repairs to our DODX tank car following filming of the Chicago Fire episode. These seals are no longer available so we are making our own. Is this a new saw? Or better described as a 90 year old saw that is new to operation in the wood shop? Either way, Tim Peters makes use of it as he continues wood work for restoration efforts on Chicago Rapid Transit 1024. I have finally manged to scoop the Hicks Car Works website with this photo of Randy Hicks cutting new roof moldings for the Chicago Aurora & Elgin 319. And while all the other work goes on, the crew on our Chicago Great Western X 38 snowplow quietly goes on about their work. New lumber for the interior lining was recovered from storage, and Victor Humphreys is prime painting it before cutting and fitting for the new ceiling. A good deal of the exterior black paint was applied to the right side during infrequent breaks in the bad weather. Tuesday, October 29. 2013
Steam Department Update 10-26-2013 Posted by Nigel Bennett
in Steam Department at
00:49
Comments (0) Steam Department Update 10-26-2013A great deal of work was done in the steam shop during the week and over the weekend. Unfortunately, on Saturday, we hit a snag that may hold us up significantly. The information this week is provided by Phil and Brian as I am far away on vacation. Thanks guys. On 1630, Brian Davies is now working full time and, with JD, Jerry, Cameron, Jeff, Jason and others all spending time working with him during the week the locomotive has seen a lot of changes: · The air system was all back together with the exception of the compressor by Friday. After a few fits, the brakes work! · Mike was working to finish that on Saturday ready for testing. Later in the day the house air was hooked up and the air pump was tested. At first the high pressure steam side moved once and then it froze up. The stuffing boxes were loosened and oil was put on the pistons. A second attempt was made. It worked beautifully. So, it was good to see that something be confirmed as done and working on the locomotive. · All of the sheet metal in the cab is on. Some screws still need to be added. With the exception of attaching and plumbing the stoker jet manifold, the cab is basically complete!! Even the electric is hooked back up pending testing. · Cylinder cocks have been cleaned and inspected, and a new pipe nipple installed after one broke. They should be good to go. · Jim and Brian are added the last little bits of insulation around about the last foot of flexible stays on either side of the wrapper sheet. · Sheet metal, minus the bands, was completed across the barrel. · On Saturday much of the banding was fitted. · The final normal hydro was performed yesterday to hammer stay bolts. This proved good so no issues with these. · The blow down muffler was installed. · Preparations have been made for the steam test including: o Setting up a large steam valve on the pipe coming off of the auxiliary dome lid to allow a gauge to be fitted for testing the safety valves; and o Making two gags that will allow individual valves to be held closed to allow the others to be tested. · Unfortunately the key objective on Saturday, which was to apply hydro pressure to the front end to test the sealing of the super heater elements into the header, ran in to significant problems. This relies upon pressurizing the whole front end (cylinders, valve chambers, exhaust passages etc. with water to about 50 psi). This involves minimizing water leakage thru a whole lot of areas, such as the piston glands, that are not wholly tight under steam and are a lot more problematic using water. · A large team spent the morning preparing for the test and the first filling was carried out in the afternoon. This indicated a lot of leakage around the piston and valve glands as well as the junction where the exhaust steam from the air compressor and stoker enter the cylinder casting. · Water was them lowered so fixes could be made to seal the water better. While some progress was made on the glands it was found that the exhaust steam connection, which is in a really awkward place under the boiler, could not be sealed in a way that allowed a pressure of anything like 50 psi to be achieved. This is a complex threaded assembly on which the threads proved to be damaged. · To progress the test it will now be necessary to machine a replacement part. At the same time further work will be done on the packing glands of the piston and valve rods. After this we can again try to pressurize the front end and test the sealing of the super heater elements. On 428: · Tom has finished most of the machining on the wedges. All that is left to do is to drill several hole in them so that they can be adjusted when they are put on the locomotive. Brian and Cameron made a mount that will align for the drilling of these holes. · The mounting brackets for 428's air compressor received a coat of paint. In other areas: · Stu, Bob, and Jane worked on painting the planer. It looks quite remarkable now that it has green paint on it. Bob also worked on assembly of some more small pipes.
So a lot was accomplished during this week. If we can successfully test pressure test the front end, we are just about ready to steam test. Sitting here in Australia!!, I will wait with bated breath for updates on progress with the front end testing. Nigel
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Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]