Monday, June 30. 2014June 25, 26,and 27 report
This last week Gary and I finally installed the last replacement panel in the area that once was the temporary "Potty." We are also installing the last two long bench seat frames. Now the interior is looking like the coach should have looked in the 40's and 50's. Have you noticed I am describing the "LAST" of a number of tasks!Gary is installing the third bench seat frame. We had three frames manufactured new by R and B Welding of Woodstock,Ill Sunday, June 29. 2014June 16, 17,18,19,, and 21 report
This last week we were again out working on the 2612, but this time the weather was so beautiful Gary and Austin and I decided to work for five days. We didn't sit around much but put in a decent days work. Our efforts are finally paying off! John Mckelvey is busy and productive at reupholstering seat cushions and backs for the coach.Eric Lorenz and son volunteered for a day on Wed and sanded the eastern door bulkhead above the door so that I could prime it the next day. Friday, June 27. 2014
Steam Department Update 06-27-2014 Posted by Nigel Bennett
in Steam Department at
17:15
Comments (16) Steam Department Update 06-27-2014
An interesting couple of weeks as we get used to supporting the operation of #1630 while starting various jobs that have been in the background while we focused on the overhaul. I am struggling with when best to write a blog these days. Much more work is taking place on Sundays and mid-week. So my practice of writing a blog each Saturday would largely reflect work in progress with the key being to have everything complete for running the next Saturday!.
Father’s Day was, to say the least, frustrating!. I was not at the shop on the Saturday as my son from the UK was over with his wife and our little grand-daughter. Like a lot of other people our plans for the Sunday went awry when we got to Union expecting a trip with #1630 and found her stopped. The crew on Sunday morning found excessive leakage overnight from a union in the cab and she was not fired up until this was fixed. Unfortunately it was early afternoon before the union was suitably tightened and late afternoon before test runs were carried out. At least these were successful so she was fully operational by end of that day.
This weekend (21st/22nd) was scheduled for maintenance and Saturday was a busy day working thru a list of minor issues that had been identified by crews over the last few weekends.
There is a surprising amount of running maintenance required on a steam engine providing a good reason why we need a weekend out of service every few weeks to cover all these “little” jobs. One surprising routine job is cleaning grass and stalks off the FS rods. We seem to have a crazy bird that seems intent on building a nest behind the small air tank. Seems like a pretty stupid bird as it does not get beyond a loose heap of vegetation behind the tank each week. This gets removed or falls off but the fact that it steams and goes away for a while does not seem to stop it trying again the next week!.
In other areas quite a lot has been going on.
On #428 several activities have got under way.
On the Shay, work has resumed on the front truck. This is now being painted in preparation to refit the springs and allow it to be refitted to the locomotive.
Nigel.
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Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]