Another month of intense activity. Yesterday there was a substantial flood
outside the steam shop. Far from being a
problem, this was a cause for celebration, marking another major milestone
toward operation.
The focus thru April has been upon completing all the tests
necessary prior to steaming. Most of
these involve pressuring the boiler completely full of water (hydrostatic
testing). The core principle is that pressurized
water expands little when the pressure is released. So, should the boiler fail under 225 psi of
water pressure, there is no explosion.
Were it to fail under 180 psi of steam pressure, the force would
substantially destroy a city block!. So
the requirement is to test the boiler at 125% of operating pressure (225 psi
for our 180 psi boiler) with water before you can put it into steam.
We have been filling the boiler, heating the water (testing
is done with warm water to reduce stress on the boiler) and applying pressure
with our antique water pump throughout April.
Yesterday we reached the key milestone where, having done the last check
with water, we were able to pump the water from the boiler and tender to
waste. The work is complete so we no
longer need the untreated well water we have been pumping between the tender and
boiler all thru April. Next time we fill
the tender it will be with treated water to be used in steaming.
There were several stages to the testing.
First we carried out a
couple of days testing to identify leaks, correct them, and test again to
ensure that we were satisfied that the boiler was fit for inspection;
Once this was done the
formal test at 225 psi was carried out observed by the FRA inspector.
With this done the boiler
was completely drained, the inspection hatch removed, dried and ventilated to
allow people to work inside. The
interior of the boiler was then inspected (with the FRA inspector observing for
the second week). The key objective here
is to ensure that nothing inside the boiler (particularly braces) has been
loosened by applying the 125% pressure.
This was carried out successfully, with one question raised on a few
flexible stays that sounded dull on hammer testing. Once this is complete it is essential that
the boiler is not pressured above operating as the internal inspection must be
carried out whenever the boiler has been raised above operating pressure.
During the week, thickness
measurements were made of the dry pipe, which is in good condition, and the
hatch was then reinstalled to seal the boiler.
Yesterday the boiler was pressured to 180 psi and thoroughly checked. All stays were hammer tested. This indicated that the flexis, that sounded
odd when empty, ring perfectly normal under pressure and all rigid stays also
ring true. No significant leaks were
detected so we are ready to move forward to steaming.
Reaching this milestone opened up all sorts of activity
this weekend.
The firebox was cleared of
all tools and the last of the grates re-installed.
The fire hole door has been
prepared for refitting.
Dennis completed welding in
the cab floor.
The hydro fittings were all
removed from the boiler and the auxiliary dome cover fitted.
The lagging was re-fitted to
the firebox sides.
Mesh was re-installed in the
smokebox
Despite all the activity, there is now serious doubt that
we will be ready for our first planned steaming (May 16/17). We have made great progress overcoming the
set-backs but there are still significant tasks to complete.
The biggest task is refitting the tender draft gear. This
must be done before we can move the tender forward, recouple it and move the
locomotive to refit the last coupling rod.
Dennis has put a lot of work into building up the mounts under the
tender and others have been hard at work in the unpleasant space under the
tender grinding the surfaces smooth after welding. This is close to completion and then we have
the fun job of squeezing the large and very heavy draft gear assembly back into
its narrow pocket above the axle.
The shot above gives some idea of the work required, That draft gear fits up between the large castings that hang down from the tender. The draft gear has been displaced to the right in this view for many years causing excess wear on that side. Dennis has added the new metal that can be seen on the right an we are in process of grinding off the excess to produce a smooth surface of the correct profile to match the left hand side before the gear can be lifted back into place.
The wedges for the trailing axle box must be shimmed and
refitted. Phil test fitted one
yesterday. This proved that the required
shim was exactly as predicted by Jason’s measurements before the shoes were
machined. The shims now need to be cut,
riveted to the wedges which can then be refitted.
Both injector starter valves need to be serviced and
refitted. There was leakage last year
and this needs to be corrected before they are refitted for this season.
The reverser cylinder must be reassembled. The cylinder was prepared yesterday for the
piston to be refitted. All the parts are prepared so it is now a case of
fitting. Unfortunately this and the
injector valves have been delayed as Mike, who had been working on these, has
had to go to Arizona for family reasons.
The “tear drops” securing the grate shakers must be fitted
and welded in to place.
Additional plate work must be welded into the tender above
the stoker helix to replace plate that was damaged and allowing coal to fall
into the stoker channel last year.
Around these key tasks are the more obvious ones of
reconnecting the tender to the locomotive and refitting the coupling rod. The issue is that we have many people who can
do these tasks but only a few who can do the key tasks.
1630 has absorbed most of the effort in the shop during
April but work has continued on the Shay and 428 when possible.
On the Shay, work is focused on preparing the boiler for re-tubing.
On 428 Eric has made good progress on machining the frame
spacer and work has continued on riveting the cab.
So we will be working as much as we can during the week as
we go into May with the objective of steaming as soon as we can.
And now a big plug for a very important event for the Department!. Tickets are now available for the Steam Department Benefit that
will be held again this year at the San Filippo Estate on Sunday June 28th. The estate with its unrivalled collection of
music machines and the great Wurlitzer organ, on which Dave will provide another great
concert, is spectacular and can only be visited thru events such as this. This is a great afternoon out and a major
opportunity to support the work in the Steam Shop.
http://www.irm.org/events/steamdeptbenefit.html
So watch this space.
I hope that, by the end of the month, I will be able to report 1630 in
steam. However we have a very busy month
ahead to achieve this.
Nigel
Comments
Fri, 03-29-2024 21:26
We're slackers and spend more time working on the equipment in the shop than keeping all you readers updated. We'll work on it, but I'm sure updates [...]
Thu, 03-14-2024 08:02
What happened to the Department Blog? It's been over 2 years and I still regularly check for updates, but nothing comes...
Mon, 12-27-2021 16:28
Happy New Year to all the Departments at the Illinois railway Museum! Thanks for all the good work you do in railroad preservation. Ted Miles, [...]
Wed, 10-13-2021 13:33
Was the CB&Q 1309 every transported to IRM?I’ve been reading old issues of Rail&Wire and the car was mentioned several times.
Mon, 06-07-2021 22:40
I was wondering if in the model layout display what scale would you guys be using and would you be displaying model train history as well? Just [...]
Wed, 06-02-2021 17:27
Nice to see 428's cab back on. Looking forward to when it is operable!
Tue, 06-01-2021 16:47
I hope the work will continue on the UP #428. Now that they are the museum's connection to the national railroad network; she would be very [...]
Sat, 04-17-2021 23:07
What is the status of 126, the Milwaukee Buffet car that is in S. Dakota? Any guess on when or if it will get to IRM?
Wed, 04-14-2021 21:09
Perhaps it is time to scrap the remains of the c, B & Q 7128 to make room for the Villa Real. Ted miles, IRM member
Wed, 04-14-2021 15:26
Hi IRM my name is Jason and I was wonder If you guys would be willing to save a CN Dash8-40cm they are currently being retired by CN and being [...]
Fri, 04-09-2021 19:56
Bear in mind that the Nebraska Zephyr is an articulated train set, so cars cannot be inserted at will. Although cars and/or a second engine could be [...]
Wed, 03-31-2021 11:37
I believe Silver Pony is currently on the back burner, and has been put into storage in one of the barns. The car needs a lot of work done to it's [...]